Crash of a Socata TBM-850 in Raleigh

Date & Time: Apr 24, 2024 at 1008 LT
Type of aircraft:
Operator:
Registration:
N228CH
Flight Type:
Survivors:
Yes
Schedule:
Wilmington - Raleigh
MSN:
356
YOM:
2006
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On final approach to Raleigh-Durham Airport, while on a positioning flight from Wilmington-New Hanover Airport, the single engine airplane went out of control and crashed nearby the runway. Both occupants were quickly rescued and the airplane was damaged beyond repair. It was reported that the pilot was attempting a go around procedure when the accident occurred.

Crash of a Cessna 550 in Wilmington

Date & Time: Jan 4, 2009 at 0209 LT
Type of aircraft:
Operator:
Registration:
N815MA
Survivors:
Yes
Schedule:
La Isabela - Wilmington
MSN:
550-0406
YOM:
1982
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6914
Captain / Total hours on type:
1400.00
Copilot / Total flying hours:
1717
Aircraft flight hours:
11123
Circumstances:
During a night, northbound, international over water flight that paralleled the east coast of the southeast United States, the airplane encountered headwinds. Upon arrival at the intended destination, the weather was below forecasted conditions, resulting in multiple instrument approach attempts. After the first missed approach, the controller advised the crew that there was an airport 36 miles to the north with "much better" weather, but the crew declined, citing a need to clear customs. During the third missed approach, the left engine lost power, and while the airplane was being vectored for a fourth approach, the right engine lost power. Utilizing the global positioning system, the captain pointed the airplane toward the intersection of the airport's two runways. Approximately 50 feet above the ground, he saw runway lights, and landed. The captain attempted to lower the landing gear prior to the landing, but it would not extend due to a lack of hydraulic pressure from the loss of engine power, and the alternate gear extension would not have been completed in time. The gear up landing resulted in damage to the underside of the fuselage and punctures of the pressure vessel. The captain stated that the airplane arrived in the vicinity of the destination with about 1,000 pounds of fuel on board or 55 minutes of fuel remaining. However, air traffic and cockpit voice recordings revealed that the right engine lost power about 14 minutes after arrival, and the left engine, about 20 minutes after arrival. Federal air regulations require, for an instrument flight rules flight plan, that an airplane carry enough fuel to complete the flight to the first airport of landing, fly from that airport to an alternate, and fly after that for 45 minutes at normal cruising speed. The loss of engine power was due to fuel exhaustion, with no preaccident mechanical anomalies noted to the airplane.
Probable cause:
A loss of engine power due to the crew's inadequate in-flight fuel monitoring.
Final Report:

Crash of a GAF Nomad N.24A in Wilmington: 2 killed

Date & Time: May 4, 1990 at 0731 LT
Type of aircraft:
Operator:
Registration:
N418NE
Flight Type:
Survivors:
No
Schedule:
Raleigh - Wilmington
MSN:
89
YOM:
1980
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
2200
Aircraft flight hours:
3590
Circumstances:
During arrival, the pilot made an ILS localizer back course approach to runway 16 and was cleared to land. He reported he was initiating a missed approach. Approximately 10 seconds later, he reported the runway in sight and requested a visual approach to land on runway 34. The pilot was cleared to land and the aircraft was observed to maneuver to the right (west of the runway), then turn back left to a final approach. However, it crashed short of runway 34. An exam of the crash site revealed evidence that the aircraft was in a normal upright attitude on a heading of 340°, when it crashed. Initial impact was with the approach lighting system short of runway 34. A King Air pilot, who landed on runway 16 before the accident, estimated the cloud bases were about 400 feet agl. Minimum descent altitude (MDA) for the back course approach was 460 feet msl. MDA for a circling approach to runway 16 was 550 feet msl. The airport elevation was 32 feet. Both occupants were killed.
Probable cause:
The pilot's failure to maintain sufficient altitude during a circling maneuver for landing. Factors related to the accident were: weather conditions below minimums for a circling approach, and failure of the pilot to follow ifr procedures.
Final Report:

Crash of a Beechcraft A60 Duke in Manassas: 5 killed

Date & Time: Mar 11, 1989 at 1615 LT
Type of aircraft:
Operator:
Registration:
N98DS
Flight Phase:
Survivors:
No
Schedule:
Manassas – Wilmington
MSN:
P-227
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
25130
Aircraft flight hours:
1775
Circumstances:
Witnesses reported the aircraft took off and climbed to about 300 feet while in a wide left turn. According to witnesses, the wings were rocking and erratic engine sounds were noted. The aircraft was turning downwind when it abruptly pitched down, rolled left until inverted, descended and crash. Examination of the aircraft revealed no evidence of malfunction, although the left prop had less rotational damage than the right prop. Examination of aircraft records revealed the aircraft was inactive for about 9 years until it was returned to service less than a year before the accident. The aircraft accumulated about 17 hours since it was returned to service. The pilot stated to a witness before the accident that he had not done single engine operation in the aircraft. The aircraft was overloaded more than 200 lbs. All five occupants were killed.
Probable cause:
A loss of aircraft control due to the pilot's failure to maintain minimum engine control speed after a partial loss of power of the left engine for undetermined reasons. The pilot's inexperience in type of aircraft and an over maximum gross weight aircraft were contributing factors.
Final Report:

Crash of a Swearingen SA226TC Metro II in Wilmington: 2 killed

Date & Time: Apr 23, 1987 at 1935 LT
Type of aircraft:
Registration:
N505LB
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Wilmington - Lumberton
MSN:
TC-202
YOM:
1972
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
6160
Captain / Total hours on type:
1860.00
Aircraft flight hours:
7667
Circumstances:
The right engine failed during takeoff immediately after rotation 3,000 feet down the 7,002 feet runway 16. The pilot continued the flight and the landing gear remained extended. The unauthorized pilot rated passenger made transmissions to the tower. Witnesses reported that the aircraft reached approximately 150 feet then descended into trees 20° to the right of runway centerline and 3,000 feet south of the airport. The pre-1979 3rd stage stator assembly in the right engine did not have the latest manufacture welding process/inspection and failed causing the uncontained turbine failure. Instruments in the wreckage indicated that an undeterminable loss of electrical power occurred at the time of engine failure. Performance data indicated that a safe landing could have been made on the remaining runway past the point of engine failure. Both occupants were killed.
Probable cause:
Occurrence #1: loss of engine power (partial) - mech failure/malf
Phase of operation: takeoff - initial climb
Findings
1. (f) turbine assembly, nozzle retention - inadequate
2. (f) acft/equip, inadequate design - manufacturer
3. (f) turbine assembly, turbine wheel - burst
4. (f) electrical system - undetermined
----------
Occurrence #2: forced landing
Phase of operation: descent - emergency
----------
Occurrence #3: in flight collision with object
Phase of operation: descent - uncontrolled
Findings
5. (f) object - tree(s)
6. (c) in-flight planning/decision - poor - pilot in command
7. (f) pressure induced by others - pilot in command
8. (c) emergency procedure - not followed - pilot in command
9. (c) all available runway - not used - pilot in command
----------
Occurrence #4: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Findings
10. Terrain condition - ground
Final Report:

Crash of a Piper PA-31P Pressurized Navajo in Wilmington: 1 killed

Date & Time: Jul 11, 1981 at 1513 LT
Type of aircraft:
Registration:
N7318L
Flight Type:
Survivors:
No
Schedule:
Fayetteville - Wilmington
MSN:
31P-71
YOM:
1968
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
2453
Circumstances:
The pilot, sole on board, departed Fayetteville, NC, on a flight to Wilmington to demonstrate the airplane to potential customers. After being cleared for a VOR approach to runway 34, the pilot started the descent in bad weather conditions with thunderstorm activity. In severe turbulences, control was lost and the airplane stalled and crashed in a field. The aircraft was destroyed and the pilot was killed.
Probable cause:
Stall on approach after the pilot continued flight into known areas of severe turbulences. The following contributing factors were reported:
- The pilot failed to maintain flying speed,
- Low ceiling,
- Rain,
- Fog,
- Unfavorable wind conditions,
- Turbulence associated with clouds and thunderstorms,
- Thunderstorm activity,
- Visibility 3/4 of a mile or less,
- Lightning in vicinity of accident,
- Wind gusting 27 knots.
Final Report:

Crash of a Martin 404 in Wilmington

Date & Time: Aug 22, 1962 at 0748 LT
Type of aircraft:
Operator:
Registration:
N40401
Flight Type:
Survivors:
Yes
Schedule:
Wilmington - Wilmington
MSN:
14101
YOM:
1952
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4492
Captain / Total hours on type:
125.00
Aircraft flight hours:
20260
Circumstances:
The crew was completing a local training flight at Wilmington-New Hanover County Airport. After touchdown, the airplane went out of control, veered off runway and came to rest. While all three crew members were uninjured, the aircraft was damaged beyond repair.
Probable cause:
The accident was the consequence of an unwanted propeller reversal during a critical phase of landing caused by malfunction of the propeller low pitch stop lever assembly, resulting from foreign matter in the servo valve control.