Crash of a Beechcraft G18S in Anvik: 1 killed

Date & Time: Jun 4, 1981 at 1745 LT
Type of aircraft:
Operator:
Registration:
N146PA
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Anvik - Anchorage
MSN:
BA-480
YOM:
1959
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
12700
Captain / Total hours on type:
327.00
Circumstances:
After takeoff from Anvik Airport, the twin engine airplane stalled and crashed, bursting into flames. The pilot, sole on board, was killed. He was en route to Anchorage on a company cargo flight.
Probable cause:
Stall during initial climb because the pilot failed to abort takeoff. The following contributing factors were reported:
- Inadequate preflight preparation,
- Improperly loaded aircraft,
- 188 lbs over max gross weight.
Final Report:

Crash of a Convair C-131E Samaritan in Dillingham

Date & Time: Jun 4, 1981 at 1617 LT
Type of aircraft:
Registration:
N121CA
Flight Type:
Survivors:
Yes
Schedule:
Dillingham - Anchorage
MSN:
342
YOM:
1956
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
9500
Captain / Total hours on type:
630.00
Circumstances:
After takeoff from Dillingham Airport, while on a company ferry flight to Anchorage, the right engine surged at meto power and the crew was forced to shut it down. The decision to return was taken and the crew followed a circuit pattern then started the descent. On final approach, the airplane descended into trees and crashed in a wooded area located few hundred yards short of runway 01. The aircraft was destroyed while all three occupants escaped with minor injuries.
Probable cause:
Engine malfunction during initial climb after exhaust stacks failed. The following contributing factors were reported:
- Material failure,
- Leak,
- Power indicators failure,
- Governors malfunction,
- Overheated, erratic,
- The pilot-in-command failed to follow approved procedures,
- Right engine fire warning light during takeoff,
- Engine surged at meto power,
- Exhaust stack broken,
- Bmep conduit overheated.
Final Report:

Crash of a Cessna 402 in Cliff

Date & Time: May 27, 1981 at 1300 LT
Type of aircraft:
Registration:
N2AQ
Flight Phase:
Survivors:
Yes
Schedule:
Tucson - Dodge City
MSN:
402-0210
YOM:
1968
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4083
Captain / Total hours on type:
310.00
Circumstances:
En route from Tucson to Dodge City in good weather conditions, the right engine caught fire. The pilot shut down the engine and as he was unable to maintain a safe altitude, he attempted an emergency landing. The airplane belly landed in a field near Cliff and came to rest in flames. The pilot, sole on board, escaped uninjured while the aircraft was destroyed by a post crash fire.
Probable cause:
Powerplant fire and explosion in flight due to a cylinder assembly failure. The following contributing factors were reported:
- Powerplant detonation,
- Fire in engine,
- Intentional wheels-up landing off airport on land,
- Exhaust system: external supercharger,
- Foreign object damage, warped,
- Rough/uneven terrain,
- Hole burnt near n°2 exhaust valve seat,
- Density altitude 7,900 feet.
Final Report:

Crash of a Rockwell Aero Commander 560 in Walkerton: 1 killed

Date & Time: May 24, 1981 at 1901 LT
Registration:
N272GD
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Walkerton - Walkerton
MSN:
560-226
YOM:
1955
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
2600
Circumstances:
After takeoff from Walketon, while in initial climb, the twin engine airplane stalled and crashed. The pilot, sole on board, was killed.
Probable cause:
Stall during initial climb after the pilot failed to maintain flying speed.
Final Report:

Crash of a Cessna T207A Skywagon in Grand Canyon: 1 killed

Date & Time: May 24, 1981 at 1733 LT
Operator:
Registration:
N6324H
Flight Phase:
Survivors:
Yes
Schedule:
Grand Canyon - Grand Canyon
MSN:
207-0483
YOM:
1978
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
2980
Captain / Total hours on type:
257.00
Circumstances:
While completing an on-demand local touristic flight, the engine failed during normal cruise. The pilot reduced his altitude and attempted an emergency landing when the airplane crash landed in rough terrain. A passenger was killed while six other occupants escaped with minor or no injuries.
Probable cause:
Powerplant failure for undetermined reasons. The following contributing factors were reported:
- High density altitude, approximately 5,400 feet
- Rough/uneven terrain,
- Forced landing off airport on land.
Final Report:

Crash of a Beechcraft G18S in Hyannis: 2 killed

Date & Time: May 23, 1981 at 0555 LT
Type of aircraft:
Operator:
Registration:
N75LA
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Hyannis - Nantucket
MSN:
BA-527
YOM:
1960
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
3500
Captain / Total hours on type:
171.00
Circumstances:
Shortly after takeoff from Hyannis-Barnstable Airport, while on a cargo flight to Nantucket, the twin engine airplane entered an uncontrolled descent and crashed. Both occupants were killed.
Probable cause:
Uncontrolled collision with ground during initial climb due to inadequate preflight preparation on part of the pilot-in-command. The following contributing factors were reported:
- Improperly loaded aircraft,
- Approximately 1,551 lbs over max gross weight,
- CofG 31,25 inches behind aft CG limit.
Final Report:

Crash of a Cessna 414 Chancellor in Winkler County

Date & Time: May 22, 1981 at 1700 LT
Type of aircraft:
Registration:
N4200C
Survivors:
Yes
Schedule:
San Antonio - Winkler County
MSN:
414-0516
YOM:
1974
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4441
Captain / Total hours on type:
1456.00
Circumstances:
On final approach to Winkler County Airport, the twin engine airplane stalled and crashed, bursting into flames. Both occupants escaped with minor injuries while the aircraft was damaged beyond repair.
Probable cause:
Stall on final approach after the pilot failed to maintain flying speed. The following contributing factors were reported:
- Unfavorable wind conditions,
- Downdrafts, updrafts,
- Wind gusts to 18 knots.
Final Report:

Crash of a Short SC.7 Skyvan 3 Variant 200 in Slate Creek

Date & Time: May 15, 1981 at 1215 LT
Type of aircraft:
Operator:
Registration:
N70DA
Flight Type:
Survivors:
Yes
Schedule:
Chicken - Slate Creek
MSN:
SH.1848
YOM:
1968
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3132
Captain / Total hours on type:
735.00
Circumstances:
Upon landing at Slave Creek Airport, the twin engine airplane landed hard and bounced. On impact, the undercarriage were torn off and the airplane came to rest. Both pilots were uninjured while the aircraft was written off.
Probable cause:
Hard landing, gear collapsed and subsequent crash caused by an improper level off on part of the pilot-in-command. The following contributing factors were reported:
- Improper recovery from bounced landing,
- Overload failure.
Final Report:

Crash of a Mitsubishi MU-2B-10 Marquise near Miami

Date & Time: May 13, 1981 at 1316 LT
Type of aircraft:
Operator:
Registration:
N92JR
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Miami - Miami
MSN:
006
YOM:
1967
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3260
Captain / Total hours on type:
85.00
Circumstances:
The twin engine airplane was engaged in a local post maintenance test flight at Miami and was carrying one engineer and one pilot. While flying at low height, both engines lost power. The pilot attempted an emergency belly landing in an field. While both occupants escaped uninjured, the aircraft was damaged beyond repair.
Probable cause:
Wheels-up landing due to inadequate preflight preparation. The following contributing factors were reported:
- Mismanagement of fuel,
- Miscalculated fuel consumption,
- Fuel exhaustion,
- Inadequate maintenance and inspection,
- 100 hours inspection in progress,
- Fuel quantity indicating system not calibrated.
Final Report:

Crash of a Boeing EC-135N in Walkersville: 21 killed

Date & Time: May 6, 1981 at 1050 LT
Type of aircraft:
Operator:
Registration:
61-0328
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Wright-Patterson - Wright Patterson
MSN:
18235/C13
YOM:
1961
Flight number:
AGAR23
Crew on board:
17
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
21
Aircraft flight hours:
13471
Circumstances:
On 6 May 1981, EC-135N, Serial Number 61-0328, call sign AGAR 23, departed Wright Patterson AFB, Ohio, at 1005 Eastern Daylight Savings Time (EDT) on a routine training mission. On board the aircraft were 17 crewmembers and four authorized passengers. The flight proceeded uneventfully as planned for approximately 45 minutes. Then in a few brief moments, a sequence of very rapid events resulted in a crash with the loss of all onboard. At 1049:48 EDT, The Federal Aviation Administration (FAA) lost radar contact with AGAR 23. The aircraft was cruising at Flight Level 290, at .78 Mach while performing a navigational training leg. The aircraft commander, Capt Emilio, occupied the right pilot seat and a passenger, Mrs. Emilio, occupied the left pilot seat. Also in the crew compartment were the 2 navigators, Lt Col Frederick and Capt Fonke, and 2 passengers, Mrs. Fonke and SSgt Brundige. For undetermined reasons, the aircraft pitch trim moved to the full nose-down position. The aircraft then a rapidly pitched over, most likely upon release of the autopilot, and induced sufficient negative "G" forces to cause the generators to trip off line, resulting in the loss of all AC electrical power. The pitch trim could not then be moved electrically. This condition, while unusual, can be controlled if prompt corrective action is taken; however, if corrective action is delayed approximately 8 seconds, the aircraft pitch angle will be greater than 30 degrees nose-down in the airspeed in excess of 350 knots indicated airspeed. Under these conditions, the aircraft cannot be controlled until the pitch trim is moved toward neutral. While it is evident that recovery was delayed, the reason for the delay is unknown. The aircraft became uncontrollable and entered a steep descent. During the rapid descent, an explosion occurred at approximately 1300 feet above ground level followed immediately by catastrophic failure, and complete break-up of the aircraft. The wreckage was found north of Walkersville and all 21 occupants were killed.
Probable cause:
At 1049:48 EDT, FAA lost radar contact with the aircraft. The aircraft was cruising at flight level 290 at .78 Mach and was performing a navigational training leg. Navigational legs are normally flown on autopilot, and FAA altitude readouts showed the aircraft was within 100 feet of assigned altitude, characteristic of autopilot flight. The aircraft commander, Capt Joseph Emilio, occupied the right pilot seat and a passenger, Mrs. Peggy Emilio, occupied the left pilot seat. Also in the crew compartment were the 2 navigators, Lt Col Benjamin B. Frederick and Capt Donald V. Fonke, and 2 passengers, Mrs. Linda Fonke and SSgt Joseph T. Brundige. This phase of flight, the navigational leg, was the least demanding on the pilot and was the logical time for the passengers to come forward to view the cockpit area. There is no evidence that the presence of the passengers in the crew compartment contributed to, or caused, the accident. For undetermined reasons, the aircraft pitch trim moved to the full nose-down position. The autopilot can overcome the trim until near full nose-down. The aircraft then rapidly pitched over, most likely upon release of the autopilot, and induced sufficient negative "G" forces to cause the generators to trip off line and loss of all AC electrical power. The pitch trim could not then be moved electrically. This condition, while unusual, can be easily controlled if prompt corrective action is taken; however if corrective action is delayed approximately 8 seconds, the aircraft pitch angle will be greater than 30° nose-down in the airspeed in excess of 350 KIAS. Under these conditions, the aircraft cannot be controlled until the pitch trim is moved toward neutral. While it is clear that recovery was delayed, the reason for the delay is unknown. The aircraft became uncontrollable and entered a steep descent. The aircraft emerged from the clouds at 2,000 feet above ground level (AGL) and was intact. Airspeed was in excess of 400 KTAS and die to angle was 20 to 30 degrees. Engine power was above 2.0 engine pressure ratio (EPR). At approximately 1,500 feet mean sea level (MSL) an explosion occurred inside the pressurized compartment of the fuselage and weakened the aircraft structure to the extent that catastrophic failure of the aircraft followed immediately. Cause of this explosion is undetermined; however, the aircraft was in an unrecoverable condition at the time of the explosion and a crash was already inevitable.