Crash of a Boeing KC-135R Stratotanker near Chaldovar: 3 killed

Date & Time: May 3, 2013 at 1448 LT
Type of aircraft:
Operator:
Registration:
63-8877
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Bishkek - Bishkek
MSN:
18725/708
YOM:
1964
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
On 3 May 2013, at approximately 1448 hours local time (L), a KC-135R, tail number 63-8877, assigned to the 22d Expeditionary Air Refueling Squadron, 376th Air Expeditionary Wing, Transit Center at Manas, Kyrgyz Republic, crashed in the foothills of mountains located 6 miles south of Chaldovar, Kyrgyz Republic. The mishap crew (MC), which consisted of the mishap pilot (MP), mishap co-pilot (MCP), and mishap boom operator (MBO), perished during the accident. The mishap aircraft (MA) exploded inflight, impacted the terrain at three main locations, and burned. The MA was completely destroyed with total loss to government property estimated at $66.3 million. Upon impact, approximately 228 cubic meters of soil were contaminated with jet fuel, and three distinct craters containing a burn pattern were created. The MA’s mission was to refuel coalition aircraft in Afghanistan and then return to the Transit Center at Manas. Immediately after takeoff, the MA experienced an unexpected rapid heading change from the direction of flight known as a crab. During climb, nearly continuous rudder hunting caused the MA’s nose to hunt slowly left and right about one degree in both directions. The MP commented on the lateral control challenges and possible series yaw damper (SYD) malfunction but continued the mission without turning off either the SYD or rudder power. Approximately nine minutes into the flight, the MA began a series of increasing yaw and roll oscillations known as a dutch roll, which was undiagnosed by the MC. The MCP attempted to decrease these oscillations using manual aileron controls, as well as two brief attempts with the autopilot. The manual corrective inputs kept the oscillations from growing. The autopilot use further exacerbated the situation, and the oscillations intensified. After the second autopilot use, the MP assumed control of the MA and used left rudder to start a left turn. A subsequent series of alternating small rudder inputs, caused by the MA’s dutch roll-induced acceleration forces varying the MP’s foot pressure on the rudder pedals, sharply increased the dutch roll oscillations. Within 30 seconds, the MP made a right rudder input to roll out of the turn, exacerbating the dutch roll condition. The cumulative effects of the malfunctioning SYD, coupled with autopilot use and rudder movements during the unrecognized dutch roll, generated dutch roll forces that exceeded the MA’s design structural limits. The tail section failed and separated from the aircraft, causing the MA to pitch down sharply, enter into a high-speed dive, explode inflight and subsequently impact the ground at approximately 1448L.
Crew:
Cpt Victoria Ann Pinckney,
Cpt Mark Tyler Voss,
T/Sgt Herman Mackey III.
Probable cause:
The board president found, by clear and convincing evidence, the cause of the mishap was the MA’s tail section separating due to structural overstress as a result of the MC’s failure to turn off either the SYD (Series Yaw Damper) or the rudder power and oscillating dutch roll-induced acceleration forces translating through the MP’s feet as the MP used rudder during the unrecognized dutch roll condition. Additionally, the board president found, by a preponderance of evidence, that the dutch roll was instigated by the MA’s malfunctioning Flight Control Augmentation System that caused directional instability or rudder hunting which substantially contributed to this mishap. Other substantially contributing factors include insufficient organizational training programs, crew composition, and cumbersome procedural guidance.
Final Report:

Ground accident of a Boeing KC-135R Stratotanker in Bishkek

Date & Time: Sep 26, 2006 at 2010 LT
Type of aircraft:
Operator:
Registration:
63-8886
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Bishkek - Bishkek
MSN:
18734
YOM:
1964
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On Sept. 26, at approximately 8:03 p.m. local time, a KC-135R landed at Manas International Airport following a combat mission over Afghanistan. After landing, the KC-135R was parked at the intersection of the active runway and a taxiway while the crew awaited clarification on instructions from the air traffic control tower. The KC-135R was struck by a host nation TU-154 that was taking off. The TU-154's right wing struck the fairing of the KC-135R's No. 1 engine. The force of the impact nearly severed the No. 1 engine from KC-135R and destroyed a portion of the aircraft's left wing. The TU-154 lost approximately six feet of its right wingtip, but was able to get airborne and return to the airport for an emergency landing with no additional damage to the aircraft. The three aircrew members on board the KC-135R, as well as the nine aircrew members and 52 passengers aboard the TU-154, survived the accident. None of the aircrew or passengers on board the TU-154 sustained any injuries. One KC-135 crew member sustained minor abrasions while evacuating the aircraft.
Probable cause:
The collision between the TU-154 and KC-135R aircraft was clearly an accident and not the result of any intentional conduct. The Accident Investigation Board, convened by AMC, determined that the accident was caused by the Kyrgyzaeronavigation air traffic controller who cleared a civilian airliner for takeoff without verifying that the KC-135R was clear of the runway. In addition to the air traffic controller, the AIB found evidence of several contributing factors involving the KC-135R aircrew, conflicting published airport notices, and a tower liaison employed by the U.S. Government to facilitate communication between the tower and U.S. aircrews. Although the AIB found the air traffic controller primarily at fault, the U.S. KC-135R crew and tower liaison shared responsibility for ensuring the KC-135R cleared the runway to a safe location following landing. The accident might have been avoided had any of them exercised better awareness of their situation.
In conclusion, the AIB determined the principal cause of the mishap was the Kyrgyzaeronavigation controller clearing the TU-154 for takeoff without verifying that KC-135R was clear of the runway, there was evidence the following factors also contributed to the mishap:
- The Kyrgyz air traffic controller's instruction to vacate at taxiway Golf after dark conflicted with a published Notice to Airmen (NOTAM) that limited that taxiway's use to daylight hours. The contractor safety liaison (LNO) employed by the U.S. Air Force to facilitate communication between its aircrews and Kyrgyz controllers did not clarify the apparent discrepancy.
- After questioning the Kyrgyz controller's instruction to vacate the runway at taxiway Golf, the LNO instructed the KC-135R crew to hold short of Alpha. The mishap KC-135R crew misperceived the LNO's instructions and responded "holding short of Golf." The LNO failed to catch the read-back error.
- The Kyrgyz controller failed to maintain awareness of the KC-135R's location.
- The LNO failed to maintain situational awareness and intervene when the controller's actions endangered the KC-135R and aircrew.
The KC-135R is assigned to the 92nd Air Refueling Wing, Fairchild Air Force Base, Wash. While deployed at Manas AB, the KC-135R and its aircrew were assigned to U.S. Central Command's 376th Air Expeditionary Wing, flying missions supporting coalition aircraft over Afghanistan.
Final Report: