Crash of a Cessna 414A Chancellor off Mattapoisett: 1 killed

Date & Time: Nov 20, 1998 at 1220 LT
Type of aircraft:
Operator:
Registration:
N6820J
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Hyannis - New Bedford
MSN:
414A-0671
YOM:
1981
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
3458
Aircraft flight hours:
2675
Circumstances:
The airplane was level at 2,000 feet, in instrument meteorological conditions, when the pilot reported 'we've just lost our ahh artificial horizon.' About 5 minutes later, air traffic control lost radar contact, and communications with the airplane. A witness about 1 mile north of the accident site stated he heard the sound of engine noise coming from the water and he described the sound as loud and constant. The sound lasted for about 30 seconds and was followed by an 'explosive collision/impact sound.' He further stated he walked to the shore and attempted to locate the source of the sound, but 'because of the fog, I couldn't see anything at all.' The airplane was located in about 25 feet of water, and was scattered over a 150 to 200 foot area. The recovered wreckage consisted of both engines, parts of the airplane's left wing, empennage, fuselage, seats, and interior. The airplane's attitude indicator was not recovered. A faint needle impression was found on the face of the airplane's vertical speed indicator between minus 2,500 and 3,000 feet per minute. Examination of the left and right vacuum pumps did not reveal any malfunctions or failures.
Probable cause:
The pilot's failure to maintain control of the airplane after an undetermined failure of the airplane's attitude indicator. A factor in this accident was fog.
Final Report:

Crash of a Cessna 414 Chancellor in Monroe

Date & Time: Nov 17, 1998 at 1855 LT
Type of aircraft:
Operator:
Registration:
N30ML
Flight Phase:
Survivors:
Yes
Schedule:
Monroe - Dallas
MSN:
414-0005
YOM:
1969
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
313
Captain / Total hours on type:
54.00
Aircraft flight hours:
6415
Circumstances:
The airplane impacted terrain during takeoff initial climb in dark night conditions with a 100 ft ceiling and 1/4 mile visibility in fog. The instrument rated private pilot sustained serious injuries and does not recall the flight. No discrepancies were found with the aircraft, flight instruments, or engines that would have contributed to the accident. A weather briefing was obtained and an IFR flight plan was filed. The pilot had 312.8 hrs total time (54.2 hrs in this aircraft), 61 hrs night flight time (36.9 hrs in this aircraft) and 26.8 hrs actual instrument time (19.6 hrs in this aircraft). Toxicological findings were positive for benzoylecgonine (metabolite of cocaine), ethanol, and cocaethylene (substance formed when cocaine and alcohol are simultaneously ingested) in a urine sample subpoenaed by the NTSB from the hospital that treated the pilot. Benzoylecgonine can be found in urine for 3 to 5 days after cocaine use. Since blood was not available for analysis, it could not be determined how much of each substance was ingested and when they were ingested. The pilot stated that he was not under the influence of cocaine or alcohol on the day of the crash.
Probable cause:
The pilot's spatial disorientation which resulted in a loss of aircraft control. Factors were fog, low ceilings, and dark night conditions.
Final Report:

Ground collision of an Ilyushin II-62M in Anchorage

Date & Time: Nov 11, 1998 at 0133 LT
Type of aircraft:
Operator:
Registration:
RA-86564
Flight Phase:
Survivors:
Yes
Schedule:
Anchorage - San Francisco
MSN:
4934734
YOM:
1979
Crew on board:
12
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The Ilyushin II-62M was parked at gate with its 12 crew members on board, awaiting the passengers for the next leg to San Francisco. An Asiana Boeing 747-400 (HL7414) was taxiing to gate N6 for a refueling stop on the flight Seoul - New York (flight 211). While trying to make a U-turn, the Boeing's n°1 engine struck the wing of the Ilyushin. Then the left winglet struck the base of the Ilyushin's tail. The Asiana crew added more power causing the wing to cut through nearly half of the tail of the Russian aircraft. The maximum ground speed recorded by the on-board recorders was 16 knots, while according to the company flight manual it should have been "10 knots or below (5 knots if wet or slippery)".
Probable cause:
The excessive taxi speed by the pilot of the other aircraft. A factor associated with the accident was the other pilot's inadequate maneuver to avoid the parked airplane.

Crash of a Mitsubishi MU-2B-60 Marquise near Rock: 2 killed

Date & Time: Nov 4, 1998 at 2058 LT
Type of aircraft:
Operator:
Registration:
N5LN
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Augusta - Augusta
MSN:
799
YOM:
1980
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
3136
Captain / Total hours on type:
300.00
Copilot / Total flying hours:
22770
Copilot / Total hours on type:
420
Aircraft flight hours:
4712
Circumstances:
The airplane's left engine had been overhauled and required an in-flight Negative Torque Sensing (NTS) check. The procedures required that the left engine be shut down during the test flight. The test flight was conducted at night. The pilots were briefed that there was icing and moderate rime icing mixed below 15,000 feet in clouds and precipitation. The cloud bases were between 2,500 to 2,900 feet agl. After departure, the pilot reported to ATC that they were clear and on top of the clouds at about 6,500 feet msl. N5LN was assigned a 180 degree heading at an assigned altitude of 8,000 feet. Without notification to ATC, N5LN turned to a southeast heading, descended from 7,700 feet to about 5,500 feet, and decelerated from about 182 kts to about 138 kts. ATC assigned N5LN a block altitude of 6,000 to 8,000 feet and a VFR-On-Top clearance. ATC instructed N5LN to turn right to stay in the assigned airspace. N5LN turned right but continued to descend from about 5,500 feet to the last radar indication of 4,500 feet. The airplane impacted the ground in a steep attitude. The inspection of the wreckage indicated the landing gear was down, and with full right rudder trim and about six degrees nose up trim. The examination of the engines indicated both engines were rotating and operating at the time of impact. The examination of the airframe and propellers found no pre-existing anomalies that would have precluded normal operation.
Probable cause:
The pilot failed to maintain control of the aircraft and made an improper evaluation of the weather. Additional factors were flying a test flight at night with the icing conditions in the clouds.
Final Report:

Crash of a Boeing 737-2P6 in Atlanta

Date & Time: Nov 1, 1998 at 1848 LT
Type of aircraft:
Operator:
Registration:
EI-CJW
Survivors:
Yes
Schedule:
Atlanta - Dallas
MSN:
21355
YOM:
1977
Flight number:
FL867
Crew on board:
5
Crew fatalities:
Pax on board:
100
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
15000
Captain / Total hours on type:
2500.00
Copilot / Total flying hours:
4976
Copilot / Total hours on type:
167
Aircraft flight hours:
45856
Aircraft flight cycles:
49360
Circumstances:
The first officer of AirTran Airways flight 890, which preceded AirTran flight 867 in the accident airplane, identified and reported a leak from the right engine of the Boeing 737-200 during a postflight inspection at William B. Hartsfield Atlanta International Airport (ATL), Georgia. AirTran mechanics at ATL identified the source of the leak as a chafed hydraulic pressure line to the right thrust reverser. They found the part in the illustrated parts catalog (IPC), which was not designed as a troubleshooting document and does not contain sufficient detail for such use. One of the mechanics telephoned an AirTran maintenance controller in Orlando, Florida, for further instructions. The mechanics who initially identified the source of the leak had little experience working on the Boeing 737 because they had worked for ValuJet Airlines, which flew DC-9s only, until ValuJet and AirTran merged in September 1997. On the basis of the information provided by the mechanic, and without questioning his description of the line or verifying the part number that he had provided against the IPC or some other appropriate maintenance document, the maintenance controller instructed the mechanic to cap the leaking line and deactivate the right thrust reverser in accordance with AirTran's Minimum Equipment List procedures. However, instead of capping the hydraulic pressure line, the mechanics capped the right engine hydraulic pump case drain return line. The mechanics performed a leak check by starting the auxiliary power unit and turning on the electric hydraulic pumps to pressurize the airplane's hydraulic systems; no leaks were detected. Although the mechanics were not required by company procedures to test their repair by running the engines, this test would have alerted the mechanics that they had incorrectly capped the hydraulic pump case drain line, which would have overpressurized the hydraulic pump and caused the hydraulic pump case seal to rupture. However, because the mechanics did not perform this test, the overpressure and rupture occurred during the airplane's climb out, allowing depletion of system A hydraulic fluid. Depletion of system A hydraulic fluid activated the hydraulic low-pressure lights in the cockpit, which alerted the flight crew that the airplane had a hydraulic problem. The crew notified air traffic control that the airplane would be returning to ATL and subsequently declared an emergency. The flight crew's initial approach to the airport was high and fast because of the workload associated with performing AirTran's procedures for the loss of hydraulic system A and the limited amount of time available to perform the procedures. Nevertheless, the crew was able to configure and stabilize the airplane for landing. However, depletion of system A hydraulic fluid disabled the nosewheel steering, inboard flight spoilers, ground spoilers, and left and right inboard brakes. The flight crew was able to land the airplane using the left thrust reverser (the right thrust reverser was fully functional but intentionally deactivated by the mechanics), outboard brakes (powered by hydraulic system B), and rudder. The flight crew used the left thrust reverser and rudder in an attempt to control the direction of the airplane down the runway, but use of the rudder pedals in this manner had depleted the system A accumulator pressure, which would have allowed three emergency brake applications. The use of the right outboard brake without the right inboard brake at a higher-than-normal speed (Vref for 15-degree flaps is faster than Vref for normal landing flaps) and with heavy gross weight (the airplane had consumed only 4,650 pounds of the 28,500 pounds of fuel on board at takeoff) used up the remaining friction material on the right outboard brake, causing it to fail. (The left outboard brake was still functional at this point.) The lack of brake friction material on the right outboard brake caused one of the right outboard brake pistons to overtravel and unport its o-ring, allowing system B hydraulic fluid to leak out; as a result, the left outboard brake also failed. Loss of the left and right inboard and outboard brakes, loss of nosewheel steering, and use of asymmetric thrust reverse caused the flight crew to lose control of the airplane, which departed the left side of the runway and came to rest in a ditch.
Probable cause:
The National Transportation Safety Board determines the probable cause(s) of this accident to be:
(1) the capping of the incorrect hydraulic line by mechanics, which led to the failure of hydraulic system A;
(2) the mechanics' lack of experience working with the Boeing 737 hydraulic system; and
(3) the maintenance controller's failure to ascertain more information regarding the leaking hydraulic line before instructing the mechanics to cap the line and deactivate the right thrust reverser.
Contributing to the cause of the accident were:
(1) the asymmetric directional control resulting from the deactivation of the right thrust reverser;
(2) the depletion of the left and right inboard brake accumulator pressure because of the flight crew's use of the rudder pedals with only the left thrust reverser to control the direction of the airplane down the runway;
(3) the failure of the right outboard brake because the airplane was slowed without the use of the left and right inboard brakes and was traveling at a higher-than-normal speed and with heavy gross weight;
(4) the failure of the right outboard brake after one of the right outboard pistons overtraveled and unported its o-ring, allowing system B hydraulic fluid to deplete and the left outboard brake to fail; and
(5) the mechanics' improper use of the illustrated parts catalog for maintenance and troubleshooting and the maintenance controller's failure to use the appropriate documents for maintenance and troubleshooting.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in Hayden: 1 killed

Date & Time: Oct 28, 1998 at 0858 LT
Operator:
Registration:
N35533
Flight Type:
Survivors:
No
Schedule:
Colorado Springs - Hayden
MSN:
31-8052047
YOM:
1980
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1800
Captain / Total hours on type:
375.00
Aircraft flight hours:
12411
Circumstances:
The Part 135 cargo flight was approaching its destination on an IFR flight plan. The pilot had requested the ILS-DME approach to runway 10, but 2 minutes later, he changed his request to the VOR-B approach to runway 28. ARTCC cleared him for the approach to the non-towered airport. The pilot contacted the airport's Unicom, and requested that the ramp personnel be standing by with fuel and oxygen. The airplane was found 5.8 nm from the approach end of runway 28, at 7,900 feet. The approach minimums for the VOR-B was 7,900 feet, which the pilot could descend to at 8.7 nm. The VOR was located 285 degrees at 13.6 nm from the accident site, and the ILS-DME transmitter was located 285 degrees at 5.6 nm from the accident site. The airplane was equipped with a single DME display head, and it had a Nav 1/Nav 2 selector switch.
Probable cause:
The pilot not following instrument procedures and subsequently descended to minimums prematurely. Factors were the mountainous terrain and the falling snow.
Final Report:

Crash of a Learjet 45 in Wallops Flight Facility

Date & Time: Oct 27, 1998 at 1456 LT
Type of aircraft:
Operator:
Registration:
N454LJ
Flight Type:
Survivors:
Yes
Schedule:
Wallops Flight Facility - Wallops Flight Facility
MSN:
45-004
YOM:
1998
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
13073
Captain / Total hours on type:
767.00
Aircraft flight hours:
339
Circumstances:
The Learjet was participating in water ingestion tests, which required multiple landing rolls through a diked pool on the runway. On one of the landing rolls, the airplane's left main landing gear and nose landing gear tracked through the pool, while the right main landing gear tracked outside the pool. The airplane veered to the left, departed the left side of the runway, and struck a pickup truck parked adjacent to the runway. The airplane came to rest inverted and on fire. Formal hazard identification and risk management procedures were not employed and no alignment cues were in place on the runway to facilitate pool entry alignment. Further, the accident truck, other vehicles, heavy equipment, and personnel were placed hundreds of feet inside the FAA recommended runway-safe and object-free areas during the test.
Probable cause:
The failure of the pilot to obtain/maintain alignment with the water pool, which resulted in the loss of control. Factors in the accident were the inadequate preflight planning of the flight test facility and the airplane manufacturer which resulted in hazards in the test area and the subsequent collision of the airplane with a vehicle.
Final Report:

Crash of a Cessna 421C Golden Eagle III in Eagle Pass

Date & Time: Oct 18, 1998 at 0600 LT
Operator:
Registration:
N19MH
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Eagle Pass - San Antonio
MSN:
421C-1008
YOM:
1980
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2095
Captain / Total hours on type:
120.00
Aircraft flight hours:
4071
Circumstances:
During takeoff climb, the twin-engine airplane encountered a strong downdraft and impacted trees and terrain. The pilot reported that while taxiing to the runway, he scanned the sky with the monochrome weather radar, which was set at the 40-mile range. 'No weather was shown behind the runway and a cell was shown 15 miles from the runway.' The takeoff roll was 'uneventful,' and the airplane was rotated at 95 knots. Climb out was accomplished at 110 knots, the engines were at maximum power, the propellers at maximum RPM, and the manifold pressure was indicating maximum. A 10-degree turn towards the Cotulla VOR was being made when at 1,500 feet msl, a sharp descent was felt with the VSI indicating an 800 ft/min rate of descent. The wings were leveled and the airspeed was slowed to 85 knots. 'The rate of descent slowed to 400 ft/min and then finally to 300 ft/min until impact...' The airplane was destroyed by fire that erupted on impact. A review of doppler weather radar images showed thunderstorms in the vicinity of the airport.
Probable cause:
A downdraft, which exceeded the aircraft's climb performance. A factor was the thunderstorms in the vicinity of the airport.
Final Report:

Crash of a Beechcraft 99A Airliner in Missoula

Date & Time: Oct 17, 1998 at 0230 LT
Type of aircraft:
Operator:
Registration:
N299GL
Flight Type:
Survivors:
Yes
Schedule:
Billings - Missoula
MSN:
U-102
YOM:
1969
Flight number:
AIP5010
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4567
Captain / Total hours on type:
667.00
Aircraft flight hours:
39685
Circumstances:
While flying a night visual approach, the co-pilot flared too high above the runway. As the aircraft floated down the runway, the speed decreased, and the pilot-in-command took control. Because he felt the aircraft was approaching a stall, he initiated a go-around. During the attempted go-around, the pilot-in-command found it necessary to keep both hands on the control wheel due to the fact that the aircraft had been trimmed to the full nose-up position during the landing flare. Even with both hands on the control wheel, the aircraft became very difficult to control. Although the co-pilot moved the throttles to maximum power and began retraction of the flaps, the pilot-in-command's remedial action had occurred too late to successfully execute the go-around. It was later discovered that during the operator's initial training, both crew members had been taught to apply full nose-up trim after crossing the runway threshold and reducing the power to idle. This action, which the operator eliminated from the landing sequence procedure after this accident, was inconsistent with the instructions in the Beech 99 Pilots Operating Manual.
Probable cause:
The pilot-in-command's delayed remedial action in response to the co-pilot's improper landing flare, and the co-pilot's application of excessive (full nose-up) trim during the landing flare as taught in the operator's initial aircrew training program. Factors include the co-pilot's improper flare and his lack of total experience in this type of aircraft.
Final Report:

Crash of a Beechcraft 65-B80 Queen Air in Brainerd

Date & Time: Oct 17, 1998 at 0033 LT
Type of aircraft:
Operator:
Registration:
N138BA
Flight Type:
Survivors:
Yes
Schedule:
Minneapolis - Brainerd
MSN:
LD-361
YOM:
1967
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4738
Captain / Total hours on type:
1813.00
Aircraft flight hours:
8119
Circumstances:
The pilot said that during the ILS approach he reached a point where he thought he should be seeing the approach lights. He said that he checked the radio to determine if it was on the correct frequency. He said that he realized that the transmit switch was selected to the wrong radio and when he returned his attention to the instruments, he realized that he had allowed the airplane to descend low on the glide path. He said that before he could react, the airplane impacted the terrain.
Probable cause:
The pilot's failure to maintain the proper glidepath and his diversion of attention during a critical phase of flight.
Final Report: