Crash of a Piper PA-60 Aerostar (Ted Smith 600) near Kalamazoo: 1 killed

Date & Time: Oct 23, 1987 at 0332 LT
Registration:
N554AC
Flight Type:
Survivors:
No
Schedule:
Milwaukee – Cleveland
MSN:
60-0029-060
YOM:
1969
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
3290
Captain / Total hours on type:
101.00
Aircraft flight hours:
14254
Circumstances:
The aircraft was at cruise altitude (9,000 feet) for approximately 20 minutes when the pilot reported the loss of right engine power. Chicago ARTCC reported the closest airport was Kalamazoo, 28 miles west. The aircraft began to descend and at 0330:53 Chicago ARTCC reported N554AC was approximately 6 miles from Kalamazoo Airport. The pilot reported 'my right engine cowling is gone...I don't know if I'm going to make it.' Witnesses observed the aircraft at 'tree top level' and impact in a heavily wooded area near interstate 94, 5 miles from the airport. Investigation revealed improper weld repairs to the right engine case and separation of the number 2 cylinder from the case due to fatigue cracking in the through bolts and studs. The top section of the engine cowling separated due to the force of the cylinder separation. The pilot, sole on board, was killed.
Probable cause:
Occurrence #1: loss of engine power (total) - mech failure/malf
Phase of operation: cruise - normal
Findings
1. 1 engine - failure, total
2. Engine assembly, crankcase - cracked
3. (c) maintenance, major repair - improper - other maintenance personnel
4. (c) engine assembly, other - fatigue
5. (c) engine assembly, cylinder - separation
6. (c) cooling system, cowling - separation
----------
Occurrence #2: forced landing
Phase of operation: descent - emergency
Findings
7. (f) light condition - bright night
8. (f) unsuitable terrain or takeoff/landing/taxi area - selected - pilot in command
----------
Occurrence #3: in flight collision with object
Phase of operation: descent - uncontrolled
Findings
9. (f) object - tree(s)
Final Report:

Crash of a Beechcraft G18S in Copperhill: 1 killed

Date & Time: Feb 22, 1986 at 0627 LT
Type of aircraft:
Operator:
Registration:
N74FA
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Kenosha - Milwaukee - Atlanta
MSN:
BA-504
YOM:
1960
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
7500
Captain / Total hours on type:
2500.00
Aircraft flight hours:
14640
Circumstances:
The pilot was alerted at 0100 for 0200 flight from Kenosha to Milwaukee, WI to pick up cargo for a flight to Atlanta, GA. At 0310, the aircraft departed Milwaukee in VFR. En route, the pilot obtained weather and an IFR clearance. Some of his radio transmissions were not standard. At 0433, he complied with ATC request for frequency change, but his radio transmissions were not clear. Approximately 5 minutes later, ATC asked the pilot to change frequency again, but 5 calls were made before he replied. His last transmission was at 0445:48; he didn't respond to further ATC calls. The aircraft continued cruising at 11,000 feet until 0621, then it descended without clearance. Radar contact was lost at 0627 cst (0727 est). Shortly thereafter, it impacted trees on a mountain, then crashed to the ground and burned. A witness believed the engines were throttled back before impact. Also, the witness reported low clouds and fog, but said the mountain was visible and was not obscured. The pilot had a 1,58‰ alcohol level in blood, no sleep for 21.5 hours, history of alcohol abuse, 7 prior dwi convictions (and ndr rec). Also, he falsified FAA medical applications. FAA was advised in 1984, but took no action.
Probable cause:
Occurrence #1: loss of control - in flight
Phase of operation: cruise - normal
Findings
1. (c) preflight planning/preparation - inadequate - pilot in command
2. (c) impairment (alcohol) - pilot in command
3. (f) fatigue - pilot in command
4. (f) fatigue (flight schedule) - company/operator management
5. (f) insuff standards/requirements, operation/operator - company/operator mgmt
6. (f) inadequate surveillance of operation - faa (organization)
7. (c) judgment - poor - pilot in command
8. (f) company-induced pressure - company/operator management
9. (f) procedures/directives - not followed - pilot in command
10. (c) descent - uncontrolled - pilot in command
11. (f) fatigue (lack of sleep) - pilot in command
----------
Occurrence #2: in flight collision with object
Phase of operation: descent - uncontrolled
Findings
12. Terrain condition - mountainous/hilly
13. Object - tree(s)
----------
Occurrence #3: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report:

Crash of a Beechcraft C-45H Expeditor in Milwaukee

Date & Time: Mar 18, 1977 at 0015 LT
Type of aircraft:
Operator:
Registration:
N9929Z
Flight Type:
Survivors:
Yes
Schedule:
Kenosha - Milwaukee
MSN:
AF-868
YOM:
1954
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5454
Captain / Total hours on type:
1575.00
Circumstances:
On approach to Milwaukee-General Billy Mitchell Airport by night and marginal weather conditions, the pilot failed to realize his altitude was insufficient when the twin engine airplane struck approach lights. It lost height, struck a fence and came to rest near the runway threshold. The pilot, sole on board, was injured and the aircraft was damaged beyond repair.
Probable cause:
Undershoot and collision with approach lights on final approach due to improper IFR operation. The following contributing factors were reported:
- Incorrect altimeter setting,
- Misjudged distance and altitude,
- Low ceiling,
- Rain,
- Fog,
- Altitude found at setting that would cause aircraft to be 180 feet lower than indicated.
Final Report:

Crash of a Boeing KC-97L Stratotanker in Milwaukee: 4 killed

Date & Time: Jan 29, 1969
Type of aircraft:
Operator:
Registration:
52-0904
Flight Type:
Survivors:
Yes
Schedule:
Key West – Milwaukee
MSN:
16598
YOM:
1952
Crew on board:
11
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
The approach to Milwaukee-General Billy Mitchell Airport was initiated in poor weather conditions with clouds down to 200 feet and an horizontal visibility limited to half a mile. On final, the four engine aircraft was too low, struck the ground and crashed in flames half a mile short of runway threshold. The aircraft was destroyed by a post crash fire and seven occupants were injured while four others were killed.

Crash of a Convair CV-580 in Chicago: 28 killed

Date & Time: Dec 27, 1968 at 2022 LT
Type of aircraft:
Operator:
Registration:
N2045
Survivors:
Yes
Schedule:
Minneapolis – Wausau – Green Bay – Manitowoc – Milwaukee – Chicago
MSN:
369
YOM:
1968
Flight number:
NC458
Crew on board:
4
Crew fatalities:
Pax on board:
41
Pax fatalities:
Other fatalities:
Total fatalities:
28
Captain / Total flying hours:
10972
Captain / Total hours on type:
123.00
Copilot / Total flying hours:
2421
Copilot / Total hours on type:
526
Aircraft flight hours:
27180
Circumstances:
On final approach by night to Chicago-O'Hare Airport, at an altitude of 200 feet, the captain decided to make a go-around when the airplane lors height, struck the ground then crashed inverted onto a hangar. Three crew members, 24 passengers and one people on the ground were killed while 18 other were injured.
Probable cause:
Spatial disorientation of the captain precipitated by atmospheric refraction of either the approach lights or landing lights at a critical point in the approach wherein the crew was transitioning between flying by reference to flight instruments and by visual reference to the ground.
Final Report:

Crash of a Lockheed B-34A Ventura in Milwaukee: 4 killed

Date & Time: Dec 17, 1954 at 1708 LT
Type of aircraft:
Operator:
Registration:
N44M
Flight Phase:
Survivors:
No
Schedule:
Milwaukee – Winnipeg
MSN:
4820
YOM:
1942
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
4500
Copilot / Total flying hours:
1298
Aircraft flight hours:
822
Circumstances:
The aircraft took off from runway 01 of General Mitchell Fields Milwaukee, Wisconsin, at approximately 1708 for an IFR (Instrument Flight Rules) flight to Winnipeg, Canada. Aboard were Pilot Joseph Laird, copilot Paul Laird, and two passengers, Frederick Miller Sr., President of the Miller Brewing Company, and his son, Fred Miller Jr. As N44M was passing over the northern boundary of the airport, after an apparently normal takeoff, the Mitchell Field Tower Controller received the message, "an engine on fire" and "making an emergency landing." The controller acknowledged this message and the pilot reported something about an engine sputtering. The aircraft which had started a turn to the left at this times was cleared to return to the airport and use air runway. The pilot then reported an engine feathered. As the controller turned up all runway lights to the highest intensity, personnel in the tower observed a mushrooming mass of flame just north of the field. The aircraft had crashed in a nose-down right-wing-low attitude in an open field approximately 3,200 feet north of the airport and west of a projected line of runway 01. Fire of large magnitude occurred after ground impact and continued for several hours before it was completely extinguished. All four occupants were killed.
Probable cause:
The Board determines that the probable cause of this accident was the failure of the left engine, together with a reduction of power in the right engine following takeoff, which prevented normal single-engine performance. This condition together with the fact that the aircraft was overloaded for single-engine performance resulted in loss of control. The following findings were reported:
- A structural failure and total power loss in the left engine occurred shortly after the aircraft became airborne,
- A power lessening of the right engine prevented normal single-engine performance,
- The terrain and obstructions did not permit a straight-ahead emergency landing,
- The left turn and loss of power produced loss of airspeed and control that resulted in an uncontrolled crash.
Final Report: