Crash of a Cessna 208B Super Cargomaster in Rhinelander

Date & Time: Mar 5, 2020 at 0815 LT
Type of aircraft:
Operator:
Registration:
N706FX
Flight Type:
Survivors:
Yes
Schedule:
Milwaukee – Rhinelander
MSN:
208B-0426
YOM:
1995
Flight number:
FDX8312
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7245
Captain / Total hours on type:
3684.00
Aircraft flight hours:
11458
Circumstances:
The pilot reported that, upon reaching the decision altitude on a GPS instrument approach, he saw the runway end identifier lights and continued the approach. Shortly after, the lights disappeared and then reappeared. He continued the approach and landing thinking the airplane was lined up with the runway by using the runway edge lights for reference. Upon touching down about 225 ft left of the runway, the airplane dug into snow and flipped over, which resulted in substantial damage to the wings and tail. The pilot reported that there were no preaccident mechanical malfunctions or failures with the airplane that would have precluded normal operation.
Probable cause:
The pilot's improper decision to continue an instrument approach to landing following a loss of visual reference with the runway, which resulted in the airplane touching down left of the runway in snow and flipping over.
Final Report:

Crash of a Cessna 402B in Madison

Date & Time: Dec 16, 2008 at 2252 LT
Type of aircraft:
Operator:
Registration:
N4504B
Flight Type:
Survivors:
Yes
Schedule:
Appleton - Milwaukee
MSN:
402B-1370
YOM:
1978
Flight number:
FRG1531
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2069
Captain / Total hours on type:
274.00
Aircraft flight hours:
12805
Circumstances:
The on-demand cargo flight departed for the destination airport and was delayed en route due to repetitive destination airport closures. The closures were the result of snow-contaminated runways. The pilot then diverted to an alternate airport due to concerns about remaining fuel reserves. The airplane experienced a loss of engine power during an instrument approach at the alternate airport and impacted the ground about 200 yards short of the landing runway. A postaccident inspection of the airplane revealed no usable fuel on board.
Probable cause:
The pilot’s improper fuel management, which resulted in a loss of engine power during an instrument landing due to fuel exhaustion.
Final Report:

Crash of a Cessna 550 Citation II off Milwaukee: 6 killed

Date & Time: Jun 4, 2007 at 1600 LT
Type of aircraft:
Operator:
Registration:
N550BP
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Milwaukee - Detroit
MSN:
550-0246
YOM:
1981
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
14000
Aircraft flight hours:
4402
Circumstances:
On June 4, 2007, about 1600 central daylight time, a Cessna Citation 550, N550BP, impacted Lake Michigan shortly after departure from General Mitchell International Airport, Milwaukee, Wisconsin (MKE). The two pilots and four passengers were killed, and the airplane was destroyed. The airplane was being operated by Marlin Air under the provisions of 14 Code of Federal Regulations Part 135 and departed MKE about 1557 with an intended destination of Willow Run Airport, near Ypsilanti, Michigan. At the time of the accident flight, marginal visual meteorological conditions prevailed at the surface, and instrument meteorological conditions prevailed aloft; the flight operated on an instrument flight rules flight plan.
Probable cause:
The pilots’ mismanagement of an abnormal flight control situation through improper actions, including failing to control airspeed and to prioritize control of the airplane, and lack of crew coordination. Contributing to the accident were Marlin Air’s operational safety deficiencies, including the inadequate checkrides administered by Marlin Air’s chief pilot/check airman, and the Federal Aviation Administration’s failure to detect and correct those deficiencies, which placed a pilot who inadequately emphasized safety in the position of company chief pilot and designated check airman and placed an ill-prepared pilot in the first officer’s seat.
Final Report:

Ground accident of a Beechcraft 99A Airliner in Milwaukee

Date & Time: Jan 24, 2007 at 2000 LT
Type of aircraft:
Operator:
Registration:
N699CZ
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Stevens Point – Milwaukee
MSN:
U-133
YOM:
1969
Flight number:
FRG1509
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
13400
Captain / Total hours on type:
2400.00
Aircraft flight hours:
35447
Circumstances:
A Beech 99 and a Cessna 402 were substantially damaged in a ground collision that occurred during night taxi operations at General Mitchell International Airport (MKE), Milwaukee, Wisconsin. Both pilots followed each of the controller's instructions to proceed to the same cargo ramp using intersecting taxiways after having landed. Neither controller had advised either pilot that other aircraft would be approaching the same taxiway intersection. Neither pilot reported seeing the other airplane approaching the taxiway intersection. The Cessna 402 landed on runway 25R and was instructed to taxi to the cargo ramp via Golf, Bravo, and Alpha taxiways. The Beech 99 landed on runway 25L. The taxi instructions given to the Beech 99 pilot were to turn right at taxiway A2 (high-speed taxiway), monitor ground on frequency 121.8, and taxi to the cargo ramp. The local controller reported he scanned taxiway A, the runway, and saw the Beech 99 clear of the runway. As the Beech 99 prepared to turn off taxiway A2 onto taxiway A, the Cessna 402 approached the taxiway A and taxiway A2 intersection. The Beech 99's right propeller impacted the Cessna 402's left wing tip fuel tank. The impact of the two airplanes resulted in a fire. Both of the pilots involved in the ground collision evacuated their respective airplanes. The FAA Order 7110.65, "Air Traffic Control," states that the absence of holding instructions authorizes an aircraft to cross all taxiways and runways that intersect the taxi route. FAA Order 7110.65, "Air Traffic Control," states that it is the procedure for controllers to instruct aircraft where to turn off the runway after landing and advise the aircraft to hold short of a runway or taxiway if required for traffic. Neither aircraft was issued hold short instructions. The Airport Surface Detection Equipment Model X (ASDEX), provided images of each airplane's movement leading up to the time of the ground collision. The ASDE-X replay showed the Beech 99 taxiing at 20 knots on taxiway A2 approaching the taxiway A intersection. The Cessna 402 was shown taxiing at 20 knots just short of the taxiway A and taxiway A2 intersection. Both pilots reported that they did not see the other airplane approaching the same intersection while taxiing. Title 14 Code of Federal Regulations Part 91 states that vigilance shall be maintained by each person operating an aircraft so as to "see and avoid" other aircraft.
Probable cause:
The failure of both pilots to adequately scan for and avoid other aircraft traffic during taxi operations, and the failure of Air Traffic Control to issue a traffic advisory to both of the pilots. A contributing factor to the accident was the night time light conditions.
Final Report:

Crash of a Short 360-300 in Watertown

Date & Time: Feb 5, 2006 at 1654 LT
Type of aircraft:
Operator:
Registration:
N372AC
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Milwaukee - Milwaukee
MSN:
3720
YOM:
1987
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1524
Captain / Total hours on type:
630.00
Copilot / Total flying hours:
519
Copilot / Total hours on type:
122
Aircraft flight hours:
21996
Circumstances:
Prior to departure, both flight crews decided that they would join-up while in flight to take video and still pictures of each airplane. Both aircraft were Shorts Brothers SD-360-300 turboprop airplanes. While flying in formation, N3735W announced over the radio that they would turn right, toward N372AC, and descend. During the turn, N3735W's left wing impacted the left wing and engine of N372AC. After the collision, N372AC rolled to the left and pitched down significantly before the flight crew regained control of the airplane. After the collision, N372AC was losing hydraulic fluid and eventually had a complete hydraulic system failure. The airplane made an emergency landing at a nearby airport with its flaps retracted and its landing gear partially extended. The airplane overran the end of the runway, coming to rest about 100 feet from the departure threshold. White paint transfer markings and scrapes were observed on the left wing deice boot, the outboard side of the left engine cowling was crushed inboard, the left wing-strut leading edge was torn open and bent, and the lower fuselage skin, immediately forward of the landing gear wheel wells and stub wing, was torn from left to right, consistent with a propeller strike. N3735W impacted terrain and the airplane was destroyed during a subsequent ground fire. The flight crew and passenger were killed. The outboard three-quarters of the left wing was separated from the main wreckage and was not fire damaged. The upper wing surface had linear scrapes diagonally across the wing skin. The left aileron from N3735W was found on the runway where N372AC had landed.
Probable cause:
The other airplane's flight crew failure to maintain clearance while maneuvering during formation flight. Contributing to the accident was the decision of both flight crews to fly in formation.
Final Report:

Crash of a Short 360-300 in Watertown: 3 killed

Date & Time: Feb 5, 2006 at 1654 LT
Type of aircraft:
Operator:
Registration:
N3735W
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Milwaukee - Milwaukee
MSN:
3735
YOM:
1988
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
1643
Captain / Total hours on type:
1181.00
Copilot / Total flying hours:
7015
Copilot / Total hours on type:
4984
Aircraft flight hours:
10077
Circumstances:
Prior to departure, both flight crews decided that they would join-up while in flight to take video and still pictures of each airplane. Both aircraft were Shorts Brothers SD-360-300 turboprop airplanes. While flying in formation, N3735W announced over the radio that they would turn right, toward N372AC, and descend. During the turn, N3735W's left wing impacted the left wing and engine of N372AC. After the collision, N372AC rolled to the left and pitched down significantly before the flight crew regained control of the airplane. After the collision, N372AC was losing hydraulic fluid and eventually had a complete hydraulic system failure. The airplane made an emergency landing at a nearby airport with its flaps retracted and its landing gear partially extended. The airplane overran the end of the runway, coming to rest about 100 feet from the departure threshold. White paint transfer markings and scrapes were observed on the left wing deice boot, the outboard side of the left engine cowling was crushed inboard, the left wing-strut leading edge was torn open and bent, and the lower fuselage skin, immediately forward of the landing gear wheel wells and stub wing, was torn from left to right, consistent with a propeller strike. N3735W impacted terrain and the airplane was destroyed during a subsequent ground fire. The flight crew and passenger were killed. The outboard three-quarters of the left wing was separated from the main wreckage and was not fire damaged. The upper wing surface had linear scrapes diagonally across the wing skin. The left aileron from N3735W was found on the runway where N372AC had landed.
Probable cause:
The flight crew failed to maintain clearance from another aircraft as they turned to break formation flight while maneuvering. Contributing to the accident was the decision of both flight crews to fly in formation.
Final Report:

Crash of a Beechcraft 99 Airliner in Wausau

Date & Time: Dec 16, 2003 at 0730 LT
Type of aircraft:
Operator:
Registration:
N399CZ
Flight Type:
Survivors:
Yes
Schedule:
Milwaukee – Wausau
MSN:
U-52
YOM:
1969
Flight number:
FRG1544
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
9000
Captain / Total hours on type:
55.00
Aircraft flight hours:
35914
Circumstances:
The airplane sustained substantial damage during a hard landing. The pilot stated, "On approach to rwy 8 at [Central Wisconsin Airport] I got high [and] right of course. When I broke out of clouds around 1000 [feet above ground level] I saw the runway, realizing I was high I pulled the power back [and] increased my rate of descent. I started to arrest my rate of descent [and] add power to keep my speed up. The engines didn't spool up in time resulting in a hard [landing]. I noticed the right wing was a little low taxing in so I thought maybe I blew a tire on landing. Not until I shut down [and] got out did I realize I hit the prop about an inch back [and] the engine nacelle dropped down several inches in front." The weather was: Wind 330 degrees at 8 knots; visibility 4 statute miles; present weather light snow; sky condition overcast 300 feet; temperature 1 degree C; dew point -1 degree C; altimeter 29.41 inches of mercury. The pilot reported that the flight did not have any mechanical malfunctions.
Probable cause:
The pilot's failure to maintain the proper descent rate and his inadequate flare.
Final Report:

Crash of a Swearingen SA226TC Metro II in Fort Wayne: 1 killed

Date & Time: Nov 9, 2000 at 0123 LT
Type of aircraft:
Operator:
Registration:
N731AC
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Fort Wayne – Milwaukee
MSN:
TC-255
YOM:
1978
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
2870
Captain / Total hours on type:
75.00
Aircraft flight hours:
20885
Circumstances:
The airplane was destroyed on impact with trees and terrain after takeoff. A post-impact fire ensued. A courier stated that he put 14 cases and 5 bags into the airplane and that "everything took place as it normally does." A witness stated, "I heard a very low flying aircraft come directly over my house. ... It sounded very revved up like a chainsaw cutting through a tree at high speed." The accident airplane's radar returns, as depicted on a chart, exhibited a horseshoe shaped flight path. That chart showed that the airplane made a left climbing turn to a maximum altitude of 2,479 feet. That chart showed the airplane in a descending left turn after that maximum recorded altitude was attained. The operator reported the pilot had flown about 75 hours in the same make and model airplane and had flown about 190 hours in the last 90 days. The weather was: Wind 090 degrees at 7 knots; visibility 1 statute mile; present weather light rain, mist; sky condition overcast 200 feet; temperature 9 degrees C; dew point 9 degrees C. No pre-impact engine anomalies were found. NTSB's Materials Laboratory Division examined the annunciator panel and recovered light assemblies and stated, "Item '29' was a light assembly with an identification cover indicating that it was the '[Right-hand] AC BUS' light. Examination of the filaments in the two installed bulbs revealed that one had been stretched, deformed and fractured and the other had been stretched and deformed." The airplane manufacturer stated that the airplane's left-hand and right-hand attitude gyros are powered by the 115-volt alternating current essential bus. Two inverters are installed and one inverter is used at a time as selected by the inverter select switch. The inverter select switch is located on the right hand switch panel. The airplane was not equipped with a backup attitude gyro and was not required to be equipped with one. The airplane was certified with a minimum flight crew of one pilot. Subsequent to the accident, the operator transitioned "from the single pilot operation of our Fairchild Metroliner to the inclusion of a First Officer."
Probable cause:
The indicated failure of the right hand AC bus during takeoff with low ceiling. The factors were the low ceiling, night, and the excessive workload the pilot experienced on takeoff with an electrical failure without a second in command.
Final Report:

Ground fire of an IAI-1124A Westwind II in Milwaukee

Date & Time: Dec 26, 1999 at 0715 LT
Type of aircraft:
Registration:
N422BC
Flight Phase:
Survivors:
Yes
Schedule:
Milwaukee - Waukesha
MSN:
302
YOM:
1980
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
14363
Captain / Total hours on type:
2024.00
Aircraft flight hours:
7975
Circumstances:
During the activation of the crew oxygen system a fire erupted which consumed the entire pressure vessel. Representatives from the National Aeronautics and Space Administration's (NASA) Johnson Space Center (JSC), White Sands Testing Facility (WSTF), Las Cruces, New Mexico, examined the retained oxygen system components. Examination of these components revealed that the fire's initiation location was the first stage pressure reducer located in the oxygen regulator assembly.
Probable cause:
The failure of the first stage pressure reducer in the oxygen regulator assembly.
Final Report:

Crash of a Lockheed C-130H Hercules in Tegucigalpa: 3 killed

Date & Time: Apr 1, 1997
Type of aircraft:
Operator:
Registration:
88-4408
Flight Type:
Survivors:
Yes
Schedule:
Milwaukee – Tegucigalpa – Howard AFB
MSN:
5161
YOM:
1989
Country:
Crew on board:
10
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
The aircraft departed Milwaukee-General Billy Mitchell Airport on a flight to Howard AFB, Panama City, with an intermediate stop in Tegucigalpa, carrying 10 crew members and a load consisting of foods and electronics. At Tegucigalpa-Toncontin Airport, the aircraft landed 2,000 feet past the runway threshold in a 50° flaps down configuration. Unable to stop within the remaining distance, it overran and crashed on a road and a bridge, bursting into flames. Three crew members were killed and seven others were injured.