Crash of a Cessna 402B in Madison

Date & Time: Dec 16, 2008 at 2252 LT
Type of aircraft:
Operator:
Registration:
N4504B
Flight Type:
Survivors:
Yes
Schedule:
Appleton - Milwaukee
MSN:
402B-1370
YOM:
1978
Flight number:
FRG1531
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2069
Captain / Total hours on type:
274.00
Aircraft flight hours:
12805
Circumstances:
The on-demand cargo flight departed for the destination airport and was delayed en route due to repetitive destination airport closures. The closures were the result of snow-contaminated runways. The pilot then diverted to an alternate airport due to concerns about remaining fuel reserves. The airplane experienced a loss of engine power during an instrument approach at the alternate airport and impacted the ground about 200 yards short of the landing runway. A postaccident inspection of the airplane revealed no usable fuel on board.
Probable cause:
The pilot’s improper fuel management, which resulted in a loss of engine power during an instrument landing due to fuel exhaustion.
Final Report:

Crash of a Dassault Falcon 100 in Lawrence

Date & Time: Dec 9, 2001 at 1645 LT
Type of aircraft:
Operator:
Registration:
N202DN
Flight Type:
Survivors:
Yes
Schedule:
Madison - Lawrence
MSN:
202
YOM:
1984
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
10500
Captain / Total hours on type:
1200.00
Copilot / Total flying hours:
1229
Copilot / Total hours on type:
22
Aircraft flight hours:
5421
Circumstances:
The pilot said that the copilot was flying a visual approach to runway 15 at the Lawrence Municipal Airport, Lawrence, Kansas. The pilot said, "With gear down and full flaps at approximately 15 to 20 feet above the runway and 115 KTS, the nose abruptly dropped and there was no elevator effectiveness with the yoke pulled back to the mechanical stop." The pilot said, "After landing, I noticed that the stabilizer trim indicated full nose down in the cockpit and, upon exterior inspection, the stab was in that position." The copilot said, "I made my turn to base and proceeded to make my turn to final. No problems with the controllability were noted at this time. The turn to final was made and the airplane was lined up with the runway on final approach with normal glide path. My altitude was dropping normally and my airspeed was approximately 140 knots." The copilot said, "When it got time to pull the power back to idle for landing our airspeed was approximately 110 knots and power was reduced. At that point in time the nose of the aircraft seemed to pitch over towards the runway and increase speed. I pulled back on the yoke to raise the nose and at that same instance the pilot recognized the pitch over and pulled back on the yoke at the same time. The yoke did not seem to pull all of the way to its full extent of travel and felt to mechanically stop at about 3/4 the way travel. Even with both pilot's pulling on the yoke it seemed unresponsive and failed to raise the nose back to a proper landing attitude. The aircraft hit the runway very hard and came to a stop on the runway." A preliminary inspection of the airplane showed the stabilizer positioned at 4 degrees nose down. An examination of the airplane's systems revealed no anomalies.
Probable cause:
The copilot's failure to maintain aircraft control during the landing. Factors relating to this accident were the copilot's improper in-flight decision not to execute a go-around, the copilot not performing a go-around, the inadequate crew coordination prior to landing between the pilot and copilot, and the improperly set stabilizer trim.
Final Report:

Crash of a Socata TBM-700 in Spearfish: 4 killed

Date & Time: Aug 4, 1998 at 1345 LT
Type of aircraft:
Registration:
N69BS
Flight Type:
Survivors:
No
Schedule:
Lawrence – Madison – Spearfish
MSN:
10
YOM:
1991
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
3150
Aircraft flight hours:
1695
Circumstances:
Witnesses observed the flight enter downwind for runway 30, after it had completed a published approach to runway 12, with a circle to land on runway 30. The witnesses, one of which was a commercial pilot said that there were jagged ceilings at the time about 400 to 500 feet above the ground. He and two other men with him saw the airplane below the clouds. As the airplane proceeded downwind, it momentarily entered a cloud. As the airplane came out of the cloud, it turned left in about a 30 degree turn. The angle of bank increased to about 70 to 80 degrees, the tail of the airplane came up, and the airplane impacted the ground nose first. Several pilots at the airport heard someone from N69BS make a radio transmission on the UNICOM frequency. What was heard by several people was that N69BS had broken out at 2200 feet. They then heard, 'N69BS turning base,' immediately followed by 'lookout' and 'oh ....' All of the eye witnesses agreed that at no time did they see or hear any problems with the engine. They all said that the sounds coming from the engine never changed. The published approach in use at the time of the accident was the GPS (global positioning system) runway 12. The pilot made his initial approach to runway 12, broke off the approach to the right, entered a right downwind for a landing on runway 30. The published circling minimums for the approach were MDA (minimum descent altitude) 4,800 feet, HAT (height above terrain) 869 feet. Using an approach speed of 90 knots, the minimum visibility was 1 mile. Using an approach speed of 120 knots, the minimum visibility was 1 1/4 miles. The field elevation was 3,931 feet. The profile for the GPS runway 12 approach showed that after the IAF (Jesee way point), the course was 204 degrees, at 7,000 feet, to the Dezzi way point, from Dezzi the course was 114 degrees, descend to 5,600, to Sophi way point, after Sophi descend to 4,800 feet to the missed approach point at the Ruste way point. The distance from Dezzi to Ruste was 10 miles.
Probable cause:
The pilot's failure to maintain control of the airplane while turning to base leg. Contributing factors were low ceilings, clouds, and the pilot's failure to adhere to both the published approach procedures and the published minimum descent altitude.
Final Report:

Crash of a Learjet 31 in Aberdeen

Date & Time: Sep 2, 1997 at 1020 LT
Type of aircraft:
Operator:
Registration:
N71JC
Flight Type:
Survivors:
Yes
Schedule:
Madison - Aberdeen
MSN:
31-008
YOM:
1989
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
19947
Captain / Total hours on type:
1860.00
Aircraft flight hours:
1845
Circumstances:
According to the pilot, the airplane was high and fast on final approach, because of restricted visibility in haze, and he executed a go-around. The pilot and copilot do not recall retracting the landing gear. During the second approach, the pilot stated he did not extended the gear because he was 'sure in his mind that the gear was already down'. The airplane landed with the gear retracted. The airplane slid approximately 3,000 feet. Following the landing, the airplane caught fire under the right wing root, and the fire could not be extinguished with hand held fire extinguishers. Both pilots safely evacuated the airplane.
Probable cause:
The flightcrew's failure to extend the landing gear.
Final Report:

Crash of a Beechcraft C-45 Expeditor in Blountville

Date & Time: Feb 2, 1996 at 1830 LT
Type of aircraft:
Operator:
Registration:
N204AA
Flight Type:
Survivors:
Yes
Schedule:
Madison - Charlotte
MSN:
AF-79
YOM:
1954
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5400
Captain / Total hours on type:
350.00
Aircraft flight hours:
16972
Circumstances:
The pilot reported that as he overflew the Tri-City airport, Tennessee at 9,000 feet, the right engine power slowly decreased. The airplane was in the clouds with an outside air temperature of about zero degrees Celsius. Right engine manifold heat was applied for a few seconds, with no noticeable difference in engine performance. The right magnetos were also checked with no obvious malfunctions noted. A descent for landing was initiated to the Tri-City airport and manifold heat was applied and removed several times, with no appreciable effect. On short final approach, when the landing gear was extended, the right main gear did not indicate down. There was insufficient time to perform the emergency gear extension procedure. A go-around was initiated, during which the pilot discovered that the left manifold heat control was now stuck in the 'ON' position. The pilot stated that with less than full power available on the left engine, and the right propeller unfeathered, the airplane could be climbed to about 200 feet. He flew the airplane until terrain clearance was no longer possible, then landed in a field, gear up. The airplane slid into trees and was substantially damaged.
Probable cause:
The pilot's improper use of carburetor heat which resulted in a continuing loss of engine power, and the right landing gear's failure to extend during a single engine approach. A factor was the
insufficient time available to extend the landing gear via the emergency extension procedure.
Final Report:

Crash of a Piper PA-31T Cheyenne II-XL in Des Moines: 1 killed

Date & Time: Nov 29, 1990 at 1016 LT
Type of aircraft:
Registration:
N1879W
Survivors:
No
Schedule:
Madison - Des Moines
MSN:
31-8166065
YOM:
1981
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
7754
Captain / Total hours on type:
4093.00
Circumstances:
On final approach, after being cleared to land, the pilot informed the controller that he might have to shut down an engine. He declined to declare an emergency or request assistance. On short final, the aircraft was observed to roll to the left and descent into the terrain. Subsequent examination revealed evidence that the left engine was not developing power, although the left propeller was not feathered. There was evidence that the right engine was producing high power during impact. No mechanical deficiency of the left engine or propeller was found. The pilot, sole on board, was killed.
Probable cause:
The pilot's improper emergency procedures by not feathering the left engine after it lost power and/or was shut down, and his failure to keep the aircraft at or above the minimum control airspeed (VMC), which resulted in a loss of aircraft control. A factor related to the accident was: an undetermined problem concerning the left engine that caused it to lose power or prompted the pilot to shut it down.
Final Report:

Crash of a Lockheed 18-56 LodeStar in Madison

Date & Time: Jan 11, 1983 at 1450 LT
Type of aircraft:
Registration:
N520R
Flight Phase:
Survivors:
Yes
Schedule:
Madison - Miami
MSN:
2183
YOM:
1941
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
15245
Captain / Total hours on type:
28.00
Aircraft flight hours:
10823
Circumstances:
The pilot reported that after he taxied to the rwy, the n°1 oil temperature was not up to the minimum temperature. He set the parking and advanced the n°1 throttle to 1,500 rpm until the engine warmed up. When both oil temperatures were within limits, he advanced both throttles to 30 inches manifold pressure and 2,250 rpm for a pretakeoff check. At that time, he used the normal (toe) brakes, since the parking brake would not hold the aircraft above approximately 1,700 rpm. He then applied full power and released the brakes for takeoff. As he started to roll with a slight left crosswind, the aircraft began drifting left. He corrected with right rudder, some right brake and right aileron. The aircraft then began drifting right and the pilot suspected a wind-shift from that direction. He applied left rudder and right aileron, but the plane veered right, went off the runway and headed for a ditch. Unable to stop, the pilot tried to clear the ditch. As the aircraft became airborne, the left wing dropped and hit the ground, and the aircraft yawed and crashed. The parking brake was found partially engaged. Tire marks were evident on the runway. All four occupants escaped uninjured.
Probable cause:
Occurrence #1: loss of control - on ground/water
Phase of operation: takeoff - roll/run
Findings
1. (c) parking brakes - inadvertent use - pilot in command
2. (f) lack of total experience in type of aircraft - pilot in command
3. (f) weather condition - crosswind
4. (f) directional control - not maintained - pilot in command
5. (f) ground loop/swerve - uncontrolled - pilot in command
----------
Occurrence #2: in flight collision with terrain/water
Phase of operation: takeoff
Findings
6. (f) terrain condition - ditch
7. (f) lift-off - initiated - pilot in command
8. (f) stall/mush
Final Report:

Crash of a Cessna 402B in Park Falls

Date & Time: Oct 4, 1981 at 1942 LT
Type of aircraft:
Operator:
Registration:
N4613N
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Park Falls - Madison
MSN:
402B-1368
YOM:
1978
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5928
Captain / Total hours on type:
125.00
Circumstances:
After takeoff from Park Falls Municipal Airport, the twin engine airplane encountered difficulties to gain height. It struck power cables then stalled and crashed in a field, bursting into flames. All five occupants were seriously injured and the aircraft was destroyed.
Probable cause:
Powerplant failure for undetermined reasons. The following contributing factors were reported:
- Collision with wires/poles during initial climb,
- The pilot failed to abort takeoff,
- High obstructions,
- Pilot stated engines not producing full thrust,
- Max gross weight 6,300 lbs, gross weight at takeoff 6,238 lbs.
Final Report:

Crash of a Cessna 207 Skywagon in East Troy: 2 killed

Date & Time: Aug 17, 1976 at 2345 LT
Registration:
N91061
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Madison - Wheeling
MSN:
207-0048
YOM:
1969
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
650
Captain / Total hours on type:
50.00
Circumstances:
While cruising by night on a flight from Madison to Wheeling, the single engine airplane went out of control, entered a dive and crashed in East Troy. Both occupants were killed. The pilot was intoxicated at the time of the accident.
Probable cause:
Uncontrolled descent following pilot's physical impairment. The following contributing factors were reported:
- Alcoholic impairment of efficiency and judgment,
- Blood alcohol level 1,45‰.
Final Report:

Crash of a Beechcraft E18 in Madison: 2 killed

Date & Time: Sep 11, 1974 at 0010 LT
Type of aircraft:
Registration:
N1258
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Madison - Lexington
MSN:
BA-435
YOM:
1959
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
3366
Captain / Total hours on type:
2000.00
Circumstances:
After a night takeoff at Madison Airport, the twin engine airplane encountered difficulties to gain height when it struck tree tops and crashed in a wooded area. The aircraft was destroyed and both pilots were killed.
Probable cause:
Collision with trees after the crew misjudged altitude and clearance. The following contributing factors were reported:
- High obstructions,
- Hi trees 50 feet AGL on runway heading, 2,300 feet from runway end,
- Landing gear in transit.
Final Report: