Zone

Crash of a Rockwell Shrike Commander 500U near Copperhill

Date & Time: Feb 12, 2002 at 1530 LT
Operator:
Registration:
N441WW
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Andrews - Lafayette
MSN:
500-1641-4
YOM:
1966
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
11805
Captain / Total hours on type:
3100.00
Aircraft flight hours:
7703
Circumstances:
A witness heard the airplane's engines make "sputtering" engine noises that cut out and quit prior to its impact with the wooded terrain. A sheriff's deputy who responded to the scene heard the pilot state the airplane ran out of fuel. The propeller blades of both engines displayed minor damage, and both propeller spinners were found intact and in place. No evidence of fuel odor nor fuel leakage was observed at the accident site. During examination, both engines were supplied fuel and a source of electricity. Each engine operated smoothly during testing at rpm ranging from idle to 1900.
Probable cause:
The pilot's inadequate preflight planning, which resulted in a total loss of engine power due to fuel exhaustion and a subsequent collision with trees during emergency landing on unsuitable terrain.
Final Report:

Crash of a Beechcraft G18S in Copperhill: 1 killed

Date & Time: Feb 22, 1986 at 0627 LT
Type of aircraft:
Operator:
Registration:
N74FA
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Kenosha - Milwaukee - Atlanta
MSN:
BA-504
YOM:
1960
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
7500
Captain / Total hours on type:
2500.00
Aircraft flight hours:
14640
Circumstances:
The pilot was alerted at 0100 for 0200 flight from Kenosha to Milwaukee, WI to pick up cargo for a flight to Atlanta, GA. At 0310, the aircraft departed Milwaukee in VFR. En route, the pilot obtained weather and an IFR clearance. Some of his radio transmissions were not standard. At 0433, he complied with ATC request for frequency change, but his radio transmissions were not clear. Approximately 5 minutes later, ATC asked the pilot to change frequency again, but 5 calls were made before he replied. His last transmission was at 0445:48; he didn't respond to further ATC calls. The aircraft continued cruising at 11,000 feet until 0621, then it descended without clearance. Radar contact was lost at 0627 cst (0727 est). Shortly thereafter, it impacted trees on a mountain, then crashed to the ground and burned. A witness believed the engines were throttled back before impact. Also, the witness reported low clouds and fog, but said the mountain was visible and was not obscured. The pilot had a 1,58‰ alcohol level in blood, no sleep for 21.5 hours, history of alcohol abuse, 7 prior dwi convictions (and ndr rec). Also, he falsified FAA medical applications. FAA was advised in 1984, but took no action.
Probable cause:
Occurrence #1: loss of control - in flight
Phase of operation: cruise - normal
Findings
1. (c) preflight planning/preparation - inadequate - pilot in command
2. (c) impairment (alcohol) - pilot in command
3. (f) fatigue - pilot in command
4. (f) fatigue (flight schedule) - company/operator management
5. (f) insuff standards/requirements, operation/operator - company/operator mgmt
6. (f) inadequate surveillance of operation - faa (organization)
7. (c) judgment - poor - pilot in command
8. (f) company-induced pressure - company/operator management
9. (f) procedures/directives - not followed - pilot in command
10. (c) descent - uncontrolled - pilot in command
11. (f) fatigue (lack of sleep) - pilot in command
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Occurrence #2: in flight collision with object
Phase of operation: descent - uncontrolled
Findings
12. Terrain condition - mountainous/hilly
13. Object - tree(s)
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Occurrence #3: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report: