Crash of an Airbus A330-243 in Jeddah

Date & Time: May 21, 2018 at 2150 LT
Type of aircraft:
Operator:
Registration:
TC-OCH
Survivors:
Yes
Schedule:
Madinah - Dhaka
MSN:
437
YOM:
2001
Flight number:
SV3818
Country:
Region:
Crew on board:
10
Crew fatalities:
Pax on board:
142
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The aircraft departed Madinah-Mohammad Bin Abdulazziz Airport at 1724LT on a schedule service to Dhaka with 142 passengers and 10 crew members on board. At 1746LT, while cruising at FL370, the crew informed ATC about a malfunction of the green hydraulic system followed by a 'green hydraulic system reservoir low level' warning. The crew decided to return to Madinah but this was not possible due to deteriorating weather conditions, so it was decided to divert to Jeddah-King Abdulazziz Airport. Several attempts to lower the nose gear were unsuccessful and only both main landing gear seemed to be down. After a circuit to burn fuel, the crew was cleared to descent and expected to make a low pass over runway 16C but neither the control tower nor ground staff were able to confirm the nose gear extension. Eventually, the crew was cleared to land on runway 34R with the nose gear retracted. The aircraft landed 700 metres past the runway threshold and the nose landed 1,350 metres further, causing both engine nacelles to hit the runway surface. The airplane slid for few hundred metres and came to rest 700 metres from the runway end. All 152 occupants evacuated safely and the aircraft was damaged beyond repair.

Crash of a Boeing 747-281BSF in Abuja

Date & Time: Dec 4, 2013 at 2119 LT
Type of aircraft:
Operator:
Registration:
EK-74798
Flight Type:
Survivors:
Yes
Schedule:
Jeddah - Abuja
MSN:
23698/667
YOM:
1986
Flight number:
SV6814
Country:
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
23000
Captain / Total hours on type:
13000.00
Copilot / Total flying hours:
5731
Copilot / Total hours on type:
1296
Aircraft flight hours:
94330
Aircraft flight cycles:
15255
Circumstances:
Following an uneventful cargo flight from Jeddah, the crew completed the approach and landing procedures on runway 04 at Abuja-Nnamdi Azikiwe Airport. During the landing roll, the aircraft overran the displaced threshold then veered to the right and veered off runway. While contacting a grassy area, the aircraft collided with several parked excavator equipment and trucks. The aircraft came to a halt and was severely damaged to both wings and engines. All six occupants escaped uninjured while the aircraft was damaged beyond repair.
Probable cause:
The accident resulted as the crew was not updated on the information available on the reduced runway length.
The following contributing factors were identified:
1. Lack of briefing by Saudia dispatcher during pre-flight.
2. Runway status was missing from Abuja ATIS information.
3. Ineffective communication between crew and ATC on short finals.
4. The runway markings and lighting not depicting the displaced threshold.
5. The entire runway lighting was ON beyond the displaced threshold.
Final Report:

Crash of an Airbus A300B4-605R in Jeddah

Date & Time: May 1, 2012 at 1449 LT
Type of aircraft:
Operator:
Registration:
TC-OAG
Flight Type:
Survivors:
Yes
Schedule:
Madinah - Jeddah
MSN:
747
YOM:
1994
Flight number:
SV2865
Country:
Region:
Crew on board:
10
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
9200
Copilot / Total flying hours:
15957
Aircraft flight hours:
54832
Aircraft flight cycles:
18308
Circumstances:
On 1 May 2012, aircraft TC-OAG, an Airbus A300-605R was performing a commercial flight for Saudi Arabian Airlines (SVA) as SVA2865. SVA 2865 departed from Prince Mohammed Bin Abdulaziz International Airport (PMAI) Madinah at 08h50 en-route to the King Abdulaziz International Airport (KAIA) Jeddah, Kingdom of Saudi Arabia. SVA 2865 was on a positioning flight with 10 crew members and no passengers. No discrepancies were noted on this aircraft prior to departure from Madinah. The visibility at Jeddah was good with a few clouds present. During the initial ILS approach to runway 16 Right (16R), while at 8 nautical miles (nm) and 2600 feet (ft), the landing gear handle was lowered. Both main landing gear extended and locked down and, the nose gear doors opened but the nose landing gear did not lower. The Captain who was then the Pilot Monitoring (PM) took over the controls and carried out a missed approach. The First Officer (FO) became the Pilot Monitoring (PM). SVA 2865 was then given an area to the northeast of Jeddah to carry out attempts at lowering the nose gear. The flight crew attempted to manually free fall the nose landing gear at least ten (10) times. The nose landing gear would not lower into the locked position, but the nose gear doors remained open during all those attempts. As a precautionary measure, SVA 2865 performed a fly-by of runway 16R at 500 ft. The air traffic controller confirmed that the nose landing gear (NLG) was not down. SVA 2865 was vectored over the Red Sea to lower the fuel load, thus reducing the landing weight. During this period, the Fire & Rescue Services (FRS) at Jeddah foamed a portion of runway 16 Left (16L) between taxiway Kilo 5 (K5) and K2. The majority of the FRS vehicles were standing by at the junction of taxiways K4 and K3. SVA 2865 was vectored for an instrument approach for Runway 16L. The Auto Pilot and the Auto Throttle Systems were OFF. The surface winds were from 220° at 12 knots (kt), gusting to 19 kt and the temperature was + 37 Celsius (°C). The flight crew used the "Landing with Nose Landing Gear Abnormal" checklist ensuring the aircraft was properly prepared and configured for the approach, the before landing, the flare and the touchdown sequences, including when the aircraft stopped and the necessary procedures to secure the aircraft before evacuation. The aircraft landed on its main landing gear 4000 ft past the threshold of runway 16L. The nose of the aircraft was slowly lowered to the runway with the nose landing gear doors touching the runway within the foamed area 4500 ft from the end of runway 16L. The front of the fuselage then touched the runway within the last portion of foam, 3500 ft from the end of runway 16L. The nose area of the aircraft slid on the runway, where sparks were present until the aircraft came to a full stop 1500 ft prior to the end of runway 16L. As soon as the aircraft passed by the position of the FRS vehicles, the FRS vehicles gave chase to the aircraft and reached it within 30 seconds after it came to a full stop. Although there was no post-crash fire, the FRS personnel applied water and foam to the nose area of the aircraft. All of the crew members were evacuated from the aircraft by ladder provided by the FRS. The crew was taken to the airport clinic as a precautionary measure. All were released the same day. The accident occurred at 14h49 on runway 16L at the KAIA - Jeddah, Kingdom of Saudi Arabia.
Probable cause:
Cause related findings:
- The NLG up-lock contained a spring, Part Number GA71102 that was broken as a result of fatigue initiated at the third coil of the spring.
- The spring had been broken for a prolonged period of time, as noted by the spring linear wear marks on the outside area of the spring coils.
- Damage observed on the NLG up-lock resulted from hard contact with the broken spring during normal NLG operation.
- The fracture process of the spring was initiated at the third coil level. At least 6000 cycles of fatigue (number of striations) have been estimated by fatigue striation measurements. The crack on the spring started on the internal surface of the spring which was not shot peened.
- The normal and free fall extensions of the NLG failed due to a mechanical blockage created by the broken spring jammed against the cam.
Final Report:

Ground fire of a Boeing 777-266ER in Cairo

Date & Time: Jul 29, 2011 at 0911 LT
Type of aircraft:
Operator:
Registration:
SU-GBP
Flight Phase:
Survivors:
Yes
Schedule:
Cairo - Jeddah
MSN:
28423/71
YOM:
1997
Flight number:
MS667
Country:
Region:
Crew on board:
10
Crew fatalities:
Pax on board:
307
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
16982
Captain / Total hours on type:
5314.00
Copilot / Total flying hours:
2247
Copilot / Total hours on type:
198
Aircraft flight hours:
48281
Aircraft flight cycles:
11448
Circumstances:
On July 29, 2011, the said Boeing 777-200, Egyptian registration SU-GBP, operated by EgyptAir, arrived from Madina, Saudi Arabia (Flight No 678) and stopped at Gate F7, terminal 3, Cairo international airport almost at 0500 UTC time. Necessary maintenance actions (After Landing Check ALC, Transit Check) have been performed by EgyptAir engineers and technicians, to prepare the aircraft for the following scheduled flight (Cairo/Jeddah, scheduled at 0730 UTC, same day 29 July 2011, flight number 667). The cockpit crew (Captain and F/O) for the event flight (Cairo/Jeddah), started the cockpit preparation including checking the cockpit crew oxygen system as per normal procedures. The F/O reported that the oxygen pressure was within normal range (730 psi). At almost 0711 UTC, and while waiting for the last passengers to board the aircraft, the F/O officer reported that a pop, hissing sound originating from the right side of his seat was heard, associated with fire and smoke coming from the right side console area below F/O window #3 (right hand lower portion of the cockpit area) [The aircraft was still preparing for departure at Gate F7, Terminal 3 at Cairo Airport at the time the crew detected the fire]. The Captain requested the F/O to leave the cockpit immediately and notify for cockpit fire. The captain used the cockpit fire extinguisher bottle located behind his seat in attempt to fight and extinguish the fire. The attempt was unsuccessful, the fire continued in the cockpit. The F/O left the cockpit, he asked the cabin crew to deplane all the passengers and crew from the aircraft, based on captain’s order. He moved to the stairs and then underneath the aircraft in attempt to find anyone with a radio unit but he could not. He returned to the service road in front of the aircraft and stopped one car and asked the person in the car to notify the fire department that the aircraft is burning on the stand F7 using his radio unit. The cabin crew deplaned the passengers using the two doors 1L and 2L. The passenger bridge was still connected to the entry doors that were used for deplaning. The first fire brigade arrived to the aircraft after three minutes. The fire was extinguished. Extinguishing actions and cooling of the aircraft were terminated at 0845 UTC (1045 Cairo local time). The aircraft experienced major damage resulting from the fire and smoke. Passengers deplaned safely, some (passengers, employees) suffered mild asphyxia caused by smoke inhalation. Passengers and crew were as follows: Passengers 307, Cockpit Crew 2, Cabin Crew 8.
Probable cause:
Probable causes for the accident can be reached through:
- Accurate and thorough reviewing of the factual information and the analysis sections
- Excluding the irrelevant probable causes included in the analysis section
Examination of the aircraft revealed that the fire originated near the first officer's oxygen mask supply tubing, which is located underneath the side console below the no. 3 right hand flight deck window. Oxygen from the flight crew oxygen system is suspected to have contributed to the fire's intensity and speed.
The cause of the fire could not be conclusively determined. It is not yet known whether the oxygen system breach occurred first, providing a flammable environment or whether the oxygen system breach occurred as a result of the fire.
Accident could be related to the following probable causes:
1. Electrical fault or short circuit resulted in electrical heating of flexible hoses in the flight crew oxygen system. (Electrical Short Circuits; contact between aircraft wiring and oxygen system components may be possible if multiple wire clamps are missing or fractured or if wires are incorrectly installed).
2. Exposure to Electrical Current
Final Report:

Ground accident of a Boeing 747-306M in Cairo

Date & Time: Jul 17, 2010 at 0730 LT
Type of aircraft:
Operator:
Registration:
HS-VAC
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Cairo - Jeddah
MSN:
23056/587
YOM:
1983
Flight number:
SV9302
Country:
Region:
Crew on board:
22
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was completing a positioning flight from Cairo to Jeddah. During the takeoff roll, the engine n°4 experienced an uncontained failure. The takeoff procedure was rejected and the aircraft came to a halt and later transferred to a hangar. All 22 crew members escaped uninjured while the aircraft was considered as damaged beyond repair.
Probable cause:
Failure of the n°4 engine during takeoff following the failure of the high pressure compressor.

Crash of a McDonnell Douglas MD-90-30 in Riyadh

Date & Time: May 8, 2009 at 1558 LT
Type of aircraft:
Operator:
Registration:
HZ-APW
Flight Type:
Survivors:
Yes
Schedule:
Jeddah - Riyadh
MSN:
53513/2257
YOM:
1999
Flight number:
SVA9061
Country:
Region:
Crew on board:
7
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
A Saudi Arabian Airlines MD-90 was substantially damaged during a runway excursion accident Riyadh (RUH). The seven crew members escaped unhurt. The airplane operated on a repositioning flight from Jeddah. During the flight, the captain discussed the use of manual spoilers during landing with the first officer. He further stated that; as he "had only around 400 hours in the aircraft" as a captain, he wanted to "see the effect' of landing with manual spoilers. He further explained that the flight provided an opportunity to "do it manually" (use manual spoilers) as it was a repositioning flight and, the weather and dry runway conditions were ideal. As such, he discussed the procedure with the first officer and elected to land with the auto ground spoiler system unarmed. The flight was uneventful. During the approach to Riyadh the Landing Checklist was completed, which included the arming of the auto ground spoiler system for landing. After the Landing Checklist was completed, the captain disarmed the auto ground spoiler system with the intention of applying manual ground spoilers after landing. The auto braking system was also not armed prior to landing. The final approach and touchdown to runway 15 Left at Riyadh were uneventful. The touchdown airspeed was 135 knots calibrated air speed (CAS). On touchdown, the captain manually extended the spoiler/speed brake lever, but did not latch it in the fully extended (EXT) position (fully aft and latched upwards). The captain then removed his right hand from the speed brake lever in order to deploy the thrust reversers. The first officer noted the movement of the spoiler/speed brake lever and called "Spoilers Deployed". Since the spoiler/speed brake lever was not fully pulled aft and latched upwards, the lever automatically returned to the forward retracted (RET) position. This movement of the spoiler/speed brake lever was not noticed by the captain and the first officer. In response, the ground spoilers re-stowed before being fully deployed and, a speed brake/flap configuration (SPD BRK/FLP CONFIG) Level 1 Amber Alert occurred. This alert occurred as the aircraft was not yet fully weight on wheels (WOW) and the aircraft still sensed a flight condition with speed brakes deployed and flaps extended beyond six degrees. Six seconds after touchdown on the right main landing gear, the nose gear touched down and the aircraft transferred to a ground condition (WOW on nose gear and main wheel spin up). The SPD BRK/FLP CONFIG alert extinguished when the nose gear oleo actuated ground shift on landing. After touchdown, the aircraft banked to the right and began to drift right of the runway centerline. In response, he applied left rudder, deployed the thrust reversers and applied left aileron. But this did not have any noticeable effect. The captain saw the approaching G4 taxiway exit and in an attempt to keep the aircraft from leaving the runway surface beyond the G4 taxiway exit, he decided to direct the aircraft towards the taxiway. He then applied a right rudder input which caused the aircraft to commence a rapid sweeping turn to the right towards the G4 taxiway exit. The aircraft left the runway at high speed, traversed the full width of the G4 taxiway, and exited the surface at its southern edge. The aircraft then entered a sand section and travelled the distance infield between the edge of the G4 taxiway and the adjacent section of taxiway GOLF. The left main landing gear collapsed during this time. The aircraft came to rest on taxiway GOLF. There was no post impact fire.
Probable cause:
Cause Related Findings
1. The Captain decided to land with manual ground spoilers when the auto ground spoiler system was fully operational.
2. The initiative by the Captain to conduct this improvised exercise contravened the Standard Operating Procedures (SOPs) and the Flight Operations Policy Manual (FOPM).
3. The auto ground spoiler system was disarmed prior to landing.
4. The spoiler/speed brake lever was partially applied manually after landing.
5. The spoiler/speed brake lever was released before it was fully extended and latched.
6. The spoiler/speed brake lever automatically retracted as per design.
7. The ground spoilers never fully deployed.
8. The loss of lift and aircraft deceleration were greatly reduced by the lack of ground spoiler deployment.
9. Brakes were not used in an attempt to control or slowdown the aircraft.
10. The Captain applied a large right rudder input with the intention of directing the aircraft onto the G4 taxiway exit.
11. The aircraft exited the runway at high speed and was travelling too fast to successfully negotiate the right turn onto the G4 taxiway.

Crash of an Airbus A300B4-203 in Jeddah

Date & Time: Mar 1, 2004 at 0140 LT
Type of aircraft:
Operator:
Registration:
AP-BBA
Flight Phase:
Survivors:
Yes
Schedule:
Jeddah - Quetta
MSN:
114
YOM:
1980
Flight number:
PK2002
Country:
Region:
Crew on board:
12
Crew fatalities:
Pax on board:
261
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
During the takeoff roll on runway 34 at Jeddah-King Abdulaziz Airport, ATC informed the crew about a fire on the left main gear. The captain rejected takeoff and was able to stop the aircraft within the remaining distance. All 273 occupants evacuated safely but the aircraft was considered as damaged beyond repair.
Probable cause:
It was determined that both tyres on the left main gear burst during the takeoff roll. Debris punctured a fuel tank in the left wing and other parts were ingested by the left engine.

Ground accident of a Boeing 747-368 in Kuala Lumpur

Date & Time: Aug 23, 2001 at 2208 LT
Type of aircraft:
Operator:
Registration:
HZ-AIO
Flight Phase:
Survivors:
Yes
Schedule:
Kuala Lumpur - Jeddah
MSN:
23266
YOM:
1985
Flight number:
SV3830
Country:
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Following technical problems with the engines, the aircraft was transferred to a hangar at Kuala Lumpur for maintenance. In the evening, a team of six technicians was dispatched to convoy the aircraft to the main terminal where 319 passengers should embark on a flight to Jeddah. While on a taxiway, the engineers attempted to turn to another taxiway when control was lost. The aircraft veered off taxiway and came to rest, nose first, in a drainage ditch. All six occupants were injured and the aircraft was damaged beyond repair. At the time of the accident, only the engine n°2 and 3 only were running and it is believed that the auxiliary hydraulic pump switches were in the OFF position. Thus, the nosewheel steering system was inoperative as well as the brakes.

Crash of a Boeing 707-3B4C in Monrovia

Date & Time: Mar 23, 2001 at 0430 LT
Type of aircraft:
Operator:
Registration:
SU-BMV
Survivors:
Yes
Schedule:
Jeddah – Monrovia
MSN:
20260
YOM:
1969
Country:
Region:
Crew on board:
7
Crew fatalities:
Pax on board:
175
Pax fatalities:
Other fatalities:
Total fatalities:
0
Aircraft flight hours:
55500
Aircraft flight cycles:
27300
Circumstances:
On a night approach to Monrovia-Roberts Airport, at an altitude of about 600 feet, the crew encountered local patches of fog and visual contact with the runway was momentarily lost by the pilot-in-command. Nevertheless, he decided to continue the approach when the aircraft landed hard on runway 04. The aircraft bounced twice then lost its both right engines. Out of control, it veered off runway and came to rest about 200 metres further. All 182 occupants evacuated safely while the aircraft was damaged beyond repair.

Crash of a Boeing 737-4Q8 in Ceyhan: 6 killed

Date & Time: Apr 7, 1999 at 0045 LT
Type of aircraft:
Operator:
Registration:
TC-JEP
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Adana - Jeddah
MSN:
25378
YOM:
1995
Flight number:
TK5904
Country:
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
6
Aircraft flight hours:
11600
Aircraft flight cycles:
6360
Circumstances:
The aircraft departed Adana Airport runway 05 at 0036LT on a positioning flight to Jeddah, Saudi Arabia, to pick up Turkish pilgrims. Nine minutes after takeoff, while climbing to an altitude of 4,000 metres in poor weather conditions, the aircraft nosed down, entered a dive and crashed in a near vertical attitude in an open field located near Ceyhan, about 30 km east of Adana Airport. The aircraft disintegrated on impact, causing a large crater. Debris were found at a depth of 10 metres. The accident was not survivable.
Probable cause:
The following findings were identified:
- The severe weather conditions probably contributed to the cause of the accident,
- The Pitot static anti-ice system was probably not activated during preparations for flight because the crew failed to follow the pre takeoff checklist,
- The crew failed to recognize the cause of an erratic airspeed indication,
- The crew failed to use other cockpit indications for control and recovery of the airplane,
- The presence of cabin crew in the cockpit probably distracted the attention of the cockpit crew.