Crash of a Rockwell Shrike Commander 500S off Horn Island: 1 killed

Date & Time: Feb 24, 2011 at 0800 LT
Operator:
Registration:
VH-WZU
Flight Type:
Survivors:
No
Schedule:
Cairns - Horn Island
MSN:
3060
YOM:
1970
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
4154
Captain / Total hours on type:
209.00
Aircraft flight hours:
17545
Circumstances:
At 0445 Eastern Standard Time on 24 February 2011, the pilot of an Aero Commander 500S, registered VH-WZU, commenced a freight charter flight from Cairns to Horn Island, Queensland under the instrument flight rules. The aircraft arrived in the Horn Island area at about 0720 and the pilot advised air traffic control that he intended holding east of the island due to low cloud and rain. At about 0750 he advised pilots in the area that he was north of Horn Island and was intending to commence a visual approach. When the aircraft did not arrive a search was commenced but the pilot and aircraft were not found. On about 10 October 2011, the wreckage was located on the seabed about 26 km north-north-west of Horn Island.
Probable cause:
The ATSB found that the aircraft had not broken up in flight and that it impacted the water at a relatively low speed and a near wings-level attitude, consistent with it being under control at impact. It is likely that the pilot encountered rain and reduced visibility when manoeuvring to commence a visual approach. However, there was insufficient evidence available to determine why the aircraft impacted the water.
Several aspects of the flight increased risk. The pilot had less than 4 hours sleep during the night before the flight and the operator did not have any procedures or guidance in place to minimize the fatigue risk associated with early starts. In addition, the pilot, who was also the operator’s chief pilot, had either not met the recency requirements or did not have an endorsement to conduct the types of instrument approaches available at Horn Island and several other locations frequently used by the operator.
Final Report:

Crash of a Rockwell Shrike Commander 500S in Rankin Inlet

Date & Time: Jul 18, 2010 at 1330 LT
Operator:
Registration:
N5800H
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Portland - Rankin Inlet - Iqaluit - Bern
MSN:
500-3082
YOM:
1970
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
23100
Captain / Total hours on type:
40.00
Copilot / Total flying hours:
5400
Copilot / Total hours on type:
13
Circumstances:
The Aero Commander 500S had recently been purchased. The new owner of the aircraft retained the services of 2 experienced pilots to deliver the aircraft from Portland, Oregon, United States, to Bern, Switzerland. After having flown several positioning legs, the aircraft arrived at Rankin Inlet for refuelling. The aircraft was refuelled from two 45-gallon drums and was to continue on to Iqaluit, Nunavut. The pilot-in-command occupied the right seat and the pilot flying the aircraft occupied the left seat. The aircraft was at its maximum takeoff weight of 7000 pounds. Prior to take off, the crew conducted a run-up and all indications seemed normal. During the takeoff roll, the engines did not produce full power and the crew elected to reject the takeoff. After returning to the ramp, a second run-up was completed and once again all indications seemed normal. Shortly after second rotation, cylinder head temperatures increased and both Lycoming TIO-540-E1B5 engines began to lose power. The pilots attempted to return to the airport, but were unable to maintain altitude. The landing gear was extended and a forced landing was made on a flat section of land, approximately 1500 feet to the southwest of the runway 13 threshold. There were no injuries and the aircraft sustained substantial damage.
Probable cause:
Findings as to Causes and Contributing Factors:
1. At the fuel compound, the 45-gallon drum containing slops was located near the stock of sealed 45-gallon drums of 100LL AVGAS, contributing to the fuel handler selecting the drum of slops in error.
2. The 45-gallon drum of slops had similar markings to the stock of sealed 45-gallon drums of 100LL AVGAS, preventing ready identification of the contaminated drum.
3. The fuel handler did not notice that the large bung plug was not sealed on the second 45-gallon drum and, as a result, delivered the drum of slops to the aircraft.
4. The pilots did not notice that the large bung plug was not sealed on the second 45-gallon drum and, as a result, fuelled the aircraft with contaminated fuel.
5. The pilots were inexperienced with refuelling from 45-gallon drums and did not take steps to ascertain the proper fuel grade in the second 45-gallon drum. As a result, slops, rather than 100LL AVGAS, was pumped into the aircraft’s fuel system.
6. The fuel system design was such that the fuel from both wing fuel cells combined in the centre fuel cell and, as a result, contaminated fuel was fed to both engines.
7. The contaminated fuel resulted in engine power loss in both engines and the aircraft was unable to maintain altitude after takeoff.
Finding as to Risk:
1. The impact force angles were substantially different from that of the ELT’s G-switch orientation. As a result, the ELT did not activate during the impact. This could have delayed search and rescue (SAR) notification.
Final Report:

Crash of a Rockwell Shrike Commander 500S in Daytona Beach: 1 killed

Date & Time: May 25, 2009 at 0846 LT
Registration:
N73U
Flight Type:
Survivors:
Yes
Schedule:
Daytona Beach - New Smyrna Beach
MSN:
500-3162
YOM:
1963
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1470
Captain / Total hours on type:
574.00
Aircraft flight hours:
3360
Circumstances:
The pilot departed in the twin-engine airplane with an unknown quantity of fuel and a fuel quantity indicating system that was known to be inaccurate. Immediately after takeoff, approximately 1/2 mile beyond the departure end of the runway, witnesses reported the engine noise from the accident airplane as "surging" as the airplane passed overhead, and one witness described a "radical" turn back to the airport. Two witnesses stated that only one engine was running, and added that it was "revving," and would then stop before revving up again. During the descent to the airport, radar data showed the airplane at 93 knots 700 feet and 1 mile from the runway, and at 90 knots at 500 feet and 1/2 mile from the runway, but the airplane crashed prior to the approach end of the runway. Post accident examination of the wreckage revealed no evidence of a pre accident mechanical malfunction. The fuel system had a capacity of 226 gallons, was serviced through a single port on top of the left wing, and the tanks were interconnected to a center fuel sump that fed both engines. The fuel cells were opened through access panels and each was intact and contained only trace amounts of fuel. The airplane was leveled, the drain petcock was opened at the center fuel cell sump, and 1 quart of fuel was drained.
Probable cause:
A total loss of engine power due to fuel exhaustion as a result of the pilot’s inadequate preflight inspection.
Final Report:

Crash of a Rockwell Shrike Commander 500S in Planeta Rica: 2 killed

Date & Time: Dec 3, 2008 at 1825 LT
Registration:
HK-1697
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Medellín – Montería
MSN:
500-3198
YOM:
1974
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
12153
Captain / Total hours on type:
2000.00
Copilot / Total hours on type:
18
Aircraft flight hours:
6179
Circumstances:
The twin engine aircraft departed Medellín-Enrique Olaya Herrera Airport at 1745LT on a cargo flight to Montería, carrying two pilots and a load of bovine embryos. The flight to Montería was completed at FL130 then the crew was cleared to start the descent to Montería-Los Garzones Airport. At an altitude of 7,500 feet on descent, the aircraft went out of control and crashed in an open field located in Verada Arroyo, near Planeta Rica. The aircraft disintegrated on impact and both pilots were killed.
Probable cause:
Loss of control in altitude for undetermined reasons.
Final Report:

Crash of a Rockwell Shrike Commander 500S near Tonganoxie: 2 killed

Date & Time: Jun 24, 2008 at 1020 LT
Operator:
Registration:
N411JT
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Kansas City - Lawrence
MSN:
500-3097
YOM:
1971
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
10500
Captain / Total hours on type:
7550.00
Aircraft flight hours:
12427
Circumstances:
The airline's chief pilot was giving a newly-hired pilot a required competency/proficiency check. Memory data from the airplane's global positioning system showed the airplane made
steep 360-degree turns to the left and right before continuing towards a practice area at gradually decreasing airspeed and altitude. A low cloud ceiling prevailed. Witnesses said they
heard both engines "sputter, then quit," and saw the airplane clear a grove of trees, stall, and strike the ground. The landing gear was down and the flaps were in the approach setting. Both propellers were in the low pitch/high rpm setting, and bore little rotational signatures. Both engine fuel supply lines contained only residual fuel. Those familiar with the chief pilot's flying practices stated that he always followed a certain routine when giving a check ride. The routine consisted of the following: After performing steep 360-degree turns, he would ask the trainee to configure the airplane for landing and demonstrate minimum control maneuvers. Prior to executing steep turns, he would turn the boost pumps on. At the completion of the maneuver, the pumps would be turned off. The investigation revealed that there are unguarded fuel shutoff switches next to the boost pumps, and the circumstances of the accident are consistent with the these fuel shutoff switches being inadvertently placed in the off position, instead of the fuel boost pumps.
Probable cause:
The pilot-in-training inadvertently shutting off both engine fuel control valves causing a loss of power in both engines, and the pilot's failure to maintain control of the airplane resulting in a stall. Contributing to the accident was the chief pilot's inadequate supervision of the pilot-in-training.
Final Report:

Crash of a Rockwell Shrike Commander 500S off Alice Town

Date & Time: Jun 9, 2008 at 1401 LT
Operator:
Registration:
N501AP
Flight Type:
Survivors:
Yes
Schedule:
Nassau – Fort Lauderdale
MSN:
500-3224
YOM:
1974
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On June 9, 2008, about 1401 eastern daylight time, an Aero Commander 500S, N501AP, registered to and operated by Gramar 500, Inc., experienced a loss of engine power in both engines and was ditched in the Atlantic Ocean about 1/2 mile south of North Bimini, Bahamas. Visual meteorological conditions prevailed in the area and a visual flight rules flight plan was filed for the 14 Code of Federal Regulations (CFR) Part 91 personal flight from Nassau International Airport (MYNN), Nassau, Bahamas, to Ft. Lauderdale Executive Airport (FXE), Ft. Lauderdale, Florida. The airplane was destroyed due to salt water immersion, and the airline transport rated pilot, the sole occupant, was not injured. The pilot stated that when the flight was past Bimini, the right engine started running rough and losing power. He turned southeast to enter a left base for runway 09 at South Bimini Airport, and the left engine also began to run rough and lost power. The pilot ditched the aircraft, evacuated into a life raft, and was rescued by a pleasure boater. The pilot also stated that 25 gallons of fuel were added while at MYNN, for a total fuel supply of 90 gallons. Both engines were test run 8 days after the accident using a test propeller. Both engines ran to near maximum RPM. One magneto from each engine was replaced prior to the test run.

Crash of a Rockwell Shrike Commander 500S in Clonbinane: 2 killed

Date & Time: Jul 31, 2007 at 2000 LT
Operator:
Registration:
VH-YJB
Flight Phase:
Survivors:
No
Site:
Schedule:
Melbourne – Shepparton
MSN:
500-3299
YOM:
1977
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
2342
Captain / Total hours on type:
970.00
Aircraft flight hours:
4558
Circumstances:
At 1946 Eastern Standard Time on 31 July 2007, a Rockwell International Aero Commander 500S, registered VH-YJB (YJB), departed Essendon Airport, Vic. on a business flight to Shepparton that was conducted at night under the instrument flight rules (IFR). On board were the pilot and one passenger. At 1958, while in the cruise at 7,000 ft above mean sea level (AMSL) in Class C controlled airspace, radar and radio contact with the aircraft was lost simultaneously by air traffic control when it was about 25 NM (46 km) north-north-east of Essendon. The air traffic controller declared a distress phase after a number of unsuccessful attempts to contact the pilot. At 2003, the Operations Director at Melbourne Centre declared the aircraft as probably lost and advised AusSAR. A search was commenced using a helicopter and an aeroplane in addition to ground search parties. No emergency locator transmitter signal was reported. At 2147, aircraft wreckage was located by a searching aircraft in timbered ranges near Clonbinane, approximately 50 km north of Melbourne. At about 2200, a ground search party confirmed that the wreckage was that of YJB and that there were no survivors. The flight was arranged to take the company owner, who was also a licensed aircraft maintenance engineer (LAME), to Shepparton to replace an unserviceable starter motor in another of the operator‟s aircraft. The pilot, who had landed at Essendon at 1915 from a previous flight in another of the operator‟s aircraft, was tasked to fly the owner to Shepparton. The pilot transferred to YJB, which had previously been prepared for flight by another company pilot. At 1938, while taxiing for takeoff, the pilot advised the aerodrome controller of the intention to conduct the IFR flight, adding, „…and request a big favour for a submission of a flight plan, with an urgent departure Essendon [to] Shepparton [and] return‟. The aerodrome controller did not have the facilities for processing flight notifications and sought the assistance of a controller in the Melbourne air traffic control centre. There were no eyewitnesses to the accident. Residents living in the vicinity of the accident site were inside their homes and reported difficulty hearing anything above the noise made by the wind and the foliage being blown about. One of the residents reported hearing a brief, loud engine noise. Another resident thought the noise was that of a noisy vehicle on the road. The noise was described as being constant, „…not spluttering or misfiring‟ and lasted for only a few seconds. Some of those residents near the accident site reported hearing and feeling an impact only moments after the engine noise ceased. The aircraft was seriously damaged by excessive in-flight aerodynamic forces and impact with the terrain. The vegetation in the immediate vicinity of the main aircraft wreckage was slightly damaged as the aircraft descended, nearly vertically, through the trees. The pilot and passenger were fatally injured.
Probable cause:
Structural failure and damage:
From the detailed examination and study of the aircraft wreckage undertaken by ATSB investigation staff, it was evident that all principal structural failures had occurred under gross overstress conditions i.e. stresses significantly in excess of the physical strength of the respective structures. The examination found no evidence of pre-existing cracking, damage or material degradation that could have appreciably reduced the strength of the failed sections, nor was there any indication that the original manufacture, maintenance or repair processes carried out on the aircraft were in any way contributory to the failures sustained.

Breakup sequence:
From the localised deformation associated with the spar failures, it was evident that the aircraft had sustained a large negative (downward) loading on the wing structure. That downward load resulted in the localised bending failure of the wing around the station 145 position (145” outboard of the aircraft centreline). The symmetry of both wing failures and the absence of axial twisting within the fuselage section suggested that the load encountered was sudden and well in excess of the ultimate strength of the wing structure. Based upon the witness marks on both wing under-surfaces and the crushing and paint transfer along the leading edges of the horizontal stabilisers, it was concluded that after separating from the inboard structure, both wings had moved aft in an axial twisting and rotating fashion; simultaneously impacting the leading edges of both horizontal tailplanes. Forces imparted into the empennage structure from that impact subsequently produced the rearward separation of the complete empennage from the fuselage. The loss of the left engine nacelle fairing was likely brought about through an impact with a section of wing leading edge as it rotated under and to the rear. The damage sustained by all of the aircraft‟s control surfaces was consistent with failure and separation from their respective primary structure under overstress conditions associated with the breakup of the aircraft. There was no evidence of cyclic or oscillatory movement of the surfaces before separation that might have suggested the contribution of an aerodynamic flutter effects.

Findings
The following statements are a summary of the verified findings made during the progress of the aircraft wreckage structural examination and analysis:
- All principal failures within the aircraft wings, tailplanes and empennage had occurred as a result of exposure to gross overstress conditions.
- The damage sustained by the aircraft wreckage was consistent with the aircraft having sustained multiple in-flight structural failures.
- The damage sustained by the aircraft wreckage was consistent with the structural failure sequence being initiated by the symmetric, downward bending failure of both wing sections, outboard of the engine nacelles.
- Breakup and separation of the empennage was consistent with having been initiated by impact of the separated outboard wings with the leading edges of the horizontal stabilisers.
- There was no evidence of material or manufacturing abnormalities within the aircraft structure that could be implicated in the failures and breakup sustained.
- There was no evidence of service-related degradation mechanisms (such as corrosion, fatigue cracking or environmental cracking) having affected the aircraft structure in the areas of failure.
Final Report:

Crash of a Rockwell Shrike Commander 500S in São Sebastião do Passé: 4 killed

Date & Time: Mar 14, 2007 at 1355 LT
Operator:
Registration:
PP-SEC
Flight Phase:
Survivors:
No
Schedule:
Petrolina – Salvador
MSN:
500-3094
YOM:
1971
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
6858
Captain / Total hours on type:
2368.00
Aircraft flight hours:
15843
Circumstances:
The twin engine aircraft departed Petrolina Airport at 1221LT on a flight to Salvador, carrying 2 passengers, 2 pilots and a load of bags containing bank documents. At 1332LT, while in cruising altitude, the crew contacted ATC and reported an engine failure. The captain elected to make an emergency landing and reduced his altitude when the aircraft entered a right turn and crashed in a field located in São Sebastião do Passé, about 50 km northwest of Salvador Airport. The aircraft was destroyed upon impact and all four occupants were killed.
Probable cause:
Engine failure in flight following a fuel exhaustion. It was determined that the crew failed to prepare the flight properly and did not calculate the fuel consumption correctly. Investigations determined that the crew calculated a fuel consumption of 100 liters per hour while the true consumption was 120 liters per hour. The following contributing factors were identified:
- Overconfidence on part of the crew,
- Poor organisational culture that affected flight safety,
- Poor flight planning,
- The crew failed to feather the propeller following the engine failure, causing drag and contributing to the loss of control at low height.
Final Report:

Crash of a Rockwell Shrike Commander 500S off Kingstown: 2 killed

Date & Time: Nov 19, 2006 at 1853 LT
Operator:
Registration:
J8-VAX
Survivors:
No
Schedule:
Canouan - Kingstown
MSN:
500-1869-45
YOM:
1969
Flight number:
SVD360
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The twin engine aircraft departed Canouan Island Airport at 1842LT on a short flight to Kingstown, Saint Vincent & Grenadines, carrying one passenger and one pilot. Shortly after takeoff, the pilot was instructed to report once passing over Bequia Island. Few minutes later, after passing Bequia Island, the pilot contacted ATC and reported he was at the altitude of 1,100 feet with an ETA in Kingstown in four minutes. At 1853LT, the aircraft crashed in unknown circumstances in the sea. The next morning, few debris were found floating on water and no trace of both occupants was ever found. The passenger was the Director of American Eagle for the Canouan Island. All SAR operations were abandoned few days later and the wreckage was not found.
Probable cause:
Due to the absence of evidences, the cause of the accident could not be determined.

Crash of a Rockwell Shrike Commander 500S in Natal

Date & Time: May 5, 2006 at 0710 LT
Operator:
Registration:
PT-IGL
Flight Type:
Survivors:
Yes
Schedule:
Recife - Natal
MSN:
500-3129
YOM:
1972
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3000
Captain / Total hours on type:
500.00
Circumstances:
The twin engine aircraft departed Recife-Guararapes Airport at 0609LT on a flight to Natal, carrying one passenger, one pilot and a load consisting of bags containing bank documents. On approach to Natal-Augusto Severo Airport runway 16L, the left engine failed. Shortly later, at a height of about 600 feet, the right engine failed as well. Aware that he will not be able to reach the airport, the pilot attempted an emergency landing in an open field. On touchdown, the undercarriage collapsed and the aircraft slid for about 200 metres before coming to rest in a muddy field. Both occupants escaped with minor injuries and the aircraft was damaged beyond repair.
Probable cause:
Double engine failure on approach caused by a fuel exhaustion. The following findings were identified:
- Poor flight preparation on part of the pilot,
- Miscalculation of fuel consumption for the flying distance (about an hour),
- The day prior to the accident, tanks were filled with a quantity of 130 liters of fuel, barely 13 liters more than the quantity theoretically necessary for the flight in the conditions existing at the time of the accident,
- No technical anomalies were found on the airplane and its equipment,
- Poor organizational culture within the operator regarding fuel policy,
- Qualitative deficiency in the instruction given to the pilot who had not acquired the basic knowledge for fuel management,
- Failure to observe the actual quantity of fuel in the tanks prior to departure,
- Shortcomings in the operator's organizational processes,
- Inadequate supervision of flight planning activities by the operator who failed to identify any flaws in the fuel management procedures by the pilots.
Final Report: