Crash of a Convair CV-240-7 in New Delhi: 23 killed

Date & Time: May 15, 1958 at 2018 LT
Type of aircraft:
Operator:
Registration:
AP-AEH
Flight Phase:
Survivors:
Yes
Schedule:
New Delhi – Karachi
MSN:
52
YOM:
1949
Flight number:
PK205
Country:
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
32
Pax fatalities:
Other fatalities:
Total fatalities:
23
Captain / Total flying hours:
4775
Captain / Total hours on type:
324.00
Aircraft flight hours:
12668
Circumstances:
The aircraft had landed at Palam at 1902 hours following an uneventful flight from Karachi. A thorough service check was carried out, and it was refuelled and loaded for the return flight to Karachi. The total take-off weight indicated on the load sheet was 41 589 lbs. The investigation revealed an error in the empty weight of the aircraft and the actual gross take-off weight was determined to be 41 319 lbs, which is 1 181 lbs less than the maximum permissible all-up weight. At 2018 hours the aircraft commenced its take-off run and was airborne at the latter half of the runway. Soon afterwards flames were observed at the western boundary of the airfield. The crash crew chief had watched the aircraft take-off. He saw the aircraft becoming airborne and then climbing to a height estimated by him to be 50 ft. He then noticed the landing lights pointing downwards and the aircraft losing height. He feared that a crash was imminent and immediately instructed the crew to proceed in that direction. At about this time the crash siren was sounded. The crash tender reached the site of the accident in about 7 to 8 minutes by which time the fire had reached large proportions. Fatal injuries were sustained by 4 members of the crew, 17 passengers and 2 others who were in the vicinity of the crash. Nine passengers and one other were seriously injured. The aircraft was destroyed by impact and fire.
Probable cause:
The captain did not properly observe and Interpret his flight instruments and thus inadvertently permitted the aircraft to descend to the ground immediately after a night take-off during which no visual reference was possible. A contributory factor may have been the slow reactions of the captain due to his state of health.
Final Report:

Crash of a Convair CV-240-12 in Warsaw

Date & Time: Apr 11, 1958
Type of aircraft:
Operator:
Registration:
SP-LPB
Flight Type:
Survivors:
Yes
Schedule:
Warsaw - Warsaw
MSN:
155
YOM:
1949
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was conducting a local training mission at Warsaw-Okecie Airport. On final approach, the four engine aircraft went out of control, stalled and crashed in a field short of runway. All four crew members were injured and the aircraft was damaged beyond repair.
Probable cause:
A propeller blade detached on short final, causing the aircraft to be out of control.

Crash of a Convair CV-240-0 at New Haven

Date & Time: Mar 1, 1958 at 1024 LT
Type of aircraft:
Operator:
Registration:
N94213
Flight Phase:
Survivors:
Yes
Schedule:
Boston – New Haven – Bridgeport – New York
MSN:
23
YOM:
1948
Flight number:
AA535
Crew on board:
3
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7453
Captain / Total hours on type:
4660.00
Copilot / Total flying hours:
5300
Copilot / Total hours on type:
3205
Aircraft flight hours:
20857
Circumstances:
This was scheduled passenger flight 535 of March 1 from Boston, Massachusetts, to New York, New York, with stops planned at New Haven and Bridgeport, Connecticut. The crew, consisting of Captain Edward W. Johnson, First Officer Norman A. Paquette, and Stewardess Marian Sullivan, reported to company operations at Boston well ahead of scheduled departure time. Departure from Boston at 0927 was on time and was in accordance with an TFR clearance to cruise at 6,000 feet via airways to New Haven. The flight was routine and on schedule to New Haven. The aircraft was not refueled during the five-minute stop at New Haven, during which time both engines were stopped. The flight departed the terminal with five passengers and 1460 gallons of fuel. Gross weight of the aircraft was well under the maximum allowable and its center of gravity was located within prescribed limits. The wind was calm and runway 14 (4,116 feet), one of two macadam runways, was selected for takeoff. There is no air traffic control tower at New Haven. After completion of the takeoff checklist, the aircraft moved onto the runway and takeoff was initiated from a tan start without delay. This segment of the flight was being flown by First Officer Paquette who occupied the right seat. Captain Johnson, on the left, maintained directional control during the initial acceleration of the aircraft. Before the aircraft reached the intersection of runways 14 and 19, the landing gear was retracted. The aircraft then skidded clown runway 14 near its center and cane to rest 1,050 feet from the far end. Captain Johnson, Stewardess Sullivan, and three passengers left through the right emergency escape hatch over the wing. First Officer Paquette and the two remaining passengers left through the partially opened front entrance door. Fire, around the left engine and the left outboard wing area, caused considerable damage and was extinguished by the local fire department.
Probable cause:
The Board determines that the probable cause of this accident was the improper technique of the captain resulting in the unintentional retraction of the landing gear prior to V 1 speed, which was made possible by a malfunctioning left gear safety switch. A contributing factor was inadequate inspection by the carrier. The following findings were reported:
- The first officer made the takeoff with the captain performing the duties of copilot from his left seat,
- The aircraft operated normally up to 85 knots in the takeoff roll,
- The captain prematurely applied upward pressure on the landing gear selector handle,
- A defective landing gear safety switch allowed the landing gear selector handle to be unlocked during ground operation of the aircraft, and permitted the landing gear to retract,
- Fire did not develop in the left nacelle and fuel tank area until the aircraft skidded to a stop on the runway,
- The company’s inspection of the safety switch was inadequate.
Final Report:

Crash of a Convair CV-240-1 in Palm Springs

Date & Time: Feb 13, 1958 at 1345 LT
Type of aircraft:
Operator:
Registration:
N8405H
Flight Phase:
Survivors:
Yes
Schedule:
Las Vegas – Palm Springs – San Diego
MSN:
22
YOM:
1948
Flight number:
WA019
Crew on board:
3
Crew fatalities:
Pax on board:
18
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
9845
Captain / Total hours on type:
3547.00
Copilot / Total flying hours:
5240
Copilot / Total hours on type:
785
Aircraft flight hours:
22516
Circumstances:
About 1342 Flight 19 took off from runway 31. The takeoff appeared normal, and the aircraft climbed to approximately 500 feet above the ground. At this time several ground witnesses saw two or more silvery pieces separate from the aircraft. Most witnesses said the pieces seemingly separated from the area of the right wing. Almost simultaneously the aircraft was observed to nose down sharply and descend at a steep angle. As it neared the ground it leveled off considerably but continued to descend. It contacted the ground raising a large cloud of dust and then disappeared from the view of the observers behind intervening higher terrain. Seconds later large columns of smoke were seen rising from the accident site. During the ground roll the aircraft struck large boulders in its path and fire occurred which consumed the major portion of the aircraft. There were no fatalities but serious injuries resulted to 5 of the 18 passengers and minor injuries to most of the others. The crew of three received minor or slight injuries.
Probable cause:
The Board determines that the probable cause of this accident was the failure of a mechanic to secure properly the right wing leading edge section as a result of which the unit separated in flight. This improper installation was undetected because of inadequate inspection. The following findings were reported:
- During the departure from Palm Springs the right wing leading edge separated in flight,
- Separation of the component resulted in severe control difficulty and buffeting of the aircraft,
- A gear-down emergency landing was made in the boulder-strewn desert about four miles north-northwest of the airport,
- During the ground roll impacts with the boulders caused severe damage and breakup of the aircraft, and a fire in the left wing spread rapidly and destroyed the aircraft,
- N8405H received a No. 3, areas 1 and 3, heavy maintenance check about two hours of flying time before the accident,
- During the maintenance a mechanic assigned to close and secure the right leading edge forgot to install the retaining screws,
- The gap straps were properly installed,
- An inadequate inspection of the aircraft by the lead mechanic resulted in his failure to detect the omission,
- The gap straps held the leading edge in place until the Palm Springs departure when they failed from loads beyond their design strength.
Final Report:

Crash of a Convair CV-240-0 in Tulsa: 1 killed

Date & Time: Jan 6, 1957 at 0001 LT
Type of aircraft:
Operator:
Registration:
N94247
Survivors:
Yes
Schedule:
Providence – Chicago – Saint Louis – Springfield – Joplin – Tulsa
MSN:
104
YOM:
1948
Flight number:
AA327
Location:
Crew on board:
3
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
8655
Captain / Total hours on type:
4100.00
Copilot / Total flying hours:
2170
Copilot / Total hours on type:
924
Aircraft flight hours:
18062
Circumstances:
Flight 327 was scheduled between Providence, Rhode Island, and Tulsa, Oklahoma, with intermediate stops including Chicago, Illinois; and St. Louis, Springfield, and Joplin, Missouri. The flight to Chicago was routine; however, the crew, when securing the cockpit, observed that the fire-warning light for the forward cargo and electrical accessory compartments flickered. This was called to the attention of both the ground crew and the relieving crew (a routine crew change was made) and was written in the aircraft log. Because of necessary repairs to the fire-warning system the flight was delayed 1 hour, 40 minutes and it departed Chicago at 1950. The new crew consisted of Captain Wesley G. Mims, First Officer Paul H. Johnson, and Stewardess Shirley D. Walker. Flight 327 was routine to Joplin and it departed there at 2323 with seven passengers aboard. Leaving Joplin the aircraft weighed 35,940 pounds, which was well under the allowable gross takeoff weight; the load was properly distributed. The flight was cleared by ARTC (Air Route Traffic Control) to the Owasso “H” facility, 2 via airway V-88, to maintain 4,000 feet, and to contact Tulsa approach control on crossing the south course of Chanute low frequency range for further clearance. At approximately 2333, 10 minutes after takeoff from Joplin, ARTC, through the company radio, advised the flight to climb to 4,500 feet, to maintain 4,500 feet, and to report leaving 4,000. This transmission was acknowledged and flight 327 reported leaving 4,000 feet at 2334. Approximately 10 minutes later company radio at Tulsa gave the flight the Tulsa 2328 weather sequence. The company then gave the flight the local altimeter setting as 30.15 and field pressure as 460 feet above zero. This was acknowledged and flight 327 reported it was changing over to Tulsa approach control frequency. At 2347 the flight reported crossing the south leg of Chanute low frequency range and was immediately cleared by approach control direct to Owasso, to descend to and maintain 3,500 feet, and to report when over Owasso. The 2328 Tulsa weather was given the flight as: Measured ceiling 600 feet, overcast; visibility 2-1/2 miles; very light drizzle and fog; wind calm. Liter, the flight reported it was 1-1/2 minutes from Owasso and asked if any delay was expected. Approach control advised no delay was expected since the only local traffic was then making an ILS (Instrument Landing System) approach. Shortly thereafter approach control advised flight 327 that the visibility was then 1-3/4 miles, that the U.S. Weather Bureau was checking the ceiling, and asked if an Owasso approach straight in to runway 17 was to be mad or if an ILS approach was preferred. The flight advised it would make the Owasso approach and at 2357 was cleared accordingly. It was asked to report when over the Owasso facility inbound. At 2400 flight 327 reported over Owasso, inbound, and was cleared to land on runway 17L. Two minutes later a special 2355 weather observation was transmitted to the flight as: Measured 200, overcast; visibility 1-3/4; very light drizzle and fog. This transmission was not acknowledged and nothing further was heard from the flight. Repeated efforts by approach control and other facilities to contact the flight were unsuccessful.
Probable cause:
The Board determines that the probable cause of this accident was the captain's lack of alertness in allowing the first officer to continue an instrument descent to an altitude too low to permit terrain clearance. The following findings were reported:
- This flight was the first time the captain and first officer had flown together,
- The first officer flew the aircraft from Joplin and during the instrument approach,
- The aircraft and its components, including altimeters, functioned in a normal manner throughout the flight and approach,
- The last weather report received by the flight indicated weather conditions were rapidly deteriorating,
- The captain told the first officer he could descend to 700 feet, without specifying mean sea level or above the elevation of the airport,
- The captain allowed the aircraft to be flown below the company’s approved landing minimums for this type approach and to an altitude precluding terrain clearance.
Final Report:

Crash of a Convair CV-240-0 at Fort Leonard Wood AFB: 30 killed

Date & Time: Aug 4, 1955 at 1223 LT
Type of aircraft:
Operator:
Registration:
N94221
Survivors:
No
Schedule:
Tulsa – Joplin – Springfield – Saint Louis – New York
MSN:
40
YOM:
1948
Flight number:
AA476
Crew on board:
3
Crew fatalities:
Pax on board:
27
Pax fatalities:
Other fatalities:
Total fatalities:
30
Captain / Total flying hours:
15540
Captain / Total hours on type:
5000.00
Copilot / Total flying hours:
8500
Copilot / Total hours on type:
2500
Aircraft flight hours:
14865
Circumstances:
Flight 476 of August 4 was a scheduled operation between Tulsa, Oklahoma, and La Guardia Field, New York, with several intermediate stops including Joplin, Springfield, and St. Louis, Missouri. The flight departed Tulsa at 1006 (one minute behind schedule) with Captain Hugh C. Barren, First Officer William G. Gates, and Stewardess Thelma R. Ballard as crew. En route stops were made at Joplin and Springfield, and no discrepancies were reported or noted at either point. However, a traffic delay in the Joplin area resulted in the flight arriving and departing Springfield 21 minutes behind schedule. Two of the eight passengers deplaned at Springfield, 21 passengers boarded the flight there. Gross weight of the aircraft at takeoff was 38,663 pounds, 2,302 pounds under that allowable, and the center of gravity was located within prescribed limits. Flight 476 departed Springfield VFR for St. Louis, its next scheduled stop, at 1153 via Victor Airway 14 to cruise at 7,000 feet. It was off the ground at 1156. Twenty-one minutes later (1217) the crew initiated a general call asking, "Does anyone read 476?" Springfield company radio acknowledged but received no reply. Two other American Airlines flights, one cruising in the vicinity of Springfield at 7,000 feet, the other 30 miles north-northeast of St. Louis, heard a transmission from Flight 476 that No. 2 engine was on fire. This message was also heard by American's ground station at St. Louis. Three minutes later the American flight in the Springfield area intercepted the following message, "Springfield, are you reading 476? We have bad engine fire." This was the last message heard from the flight. All transmissions were on company frequency. During this interval numerous witnesses on the ground back along the flight path saw the aircraft with smoke and flame coming from the right engine. The aircraft was also tracked by a military radar installation near Springfield until it disappeared from the scope in the vicinity of Fort Leonard Wood. At approximately 1222 the operations officer on duty at Forney Field, Fort Leonard Wood, received a radio message from an Army pilot flying nearby that a two-engine aircraft with a fire in the right engine was on final approach to runway 14. The tower operator at Forney Field saw the approaching aircraft and gave it clearance to land. Before the operations officer could alert the crash crew another call from the Army pilot informed him that the airplane had crashed short of the runway. The time was 1223. Army personnel with portable fire-fighting equipment reached the wreckage on foot. There were no survivors. Heavy fire-fighting equipment and ambulances could not reach the scene until the Army engineers had bulldozed a road through the densely wooded area in which the crash occurred.
Probable cause:
The Board determines that the probable cause of this accident was installation of an unairworthy cylinder, the failure of which resulted in an uncontrollable fire and subsequent loss of a wing in flight. The following findings were reported:
- Weather was not a factor,
- N° 12 cylinder of the right engine was not airworthy and failed near its base after less than six hours of operation, causing a fire that the crew could not control,
- Visual inspection procedures being used by the carrier did not reveal the unairworthy condition of the cylinder,
- The right main tank fuel shutoff valve was open, which greatly increased the intensity and duration of the fire,
- Fire damage prevented the closing of this valve,
- Procedures recommended by the manufacturer and specified in the carrier's overhaul manual had been countermanded by verbal instructions approved by the carrier's engineering department and were not being followed by the carrier's inspectors with respect to the handling of cylinders.
Final Report:

Crash of a Convair CV-240-0 in Springfield: 13 killed

Date & Time: Mar 20, 1955 at 2236 LT
Type of aircraft:
Operator:
Registration:
N94234
Survivors:
Yes
Schedule:
Newark – Chicago – Saint Louis – Springfield – Tulsa
MSN:
66
YOM:
1948
Flight number:
AA711
Crew on board:
3
Crew fatalities:
Pax on board:
32
Pax fatalities:
Other fatalities:
Total fatalities:
13
Captain / Total flying hours:
9670
Captain / Total hours on type:
1324.00
Copilot / Total flying hours:
1922
Copilot / Total hours on type:
2
Aircraft flight hours:
13383
Circumstances:
American 711 reported en route to the company that it was over Vichy (a position along Victor Airway 14 about 100 miles from Springfield) and estimated it would reach the Springfield VOR station at 2233. Initial radio contact with Springfield Approach Control was established at 2218 and the flight gave it the same Springfield estimate. The approach controller transmitted the 2208 weather observation to the flight. Reported conditions were: Ceiling 400 feet overcast; visibility 10 miles; wind west 12; altimeter 29.68. In response to the controller’s question the flight then indicated it intended to land at Springfield. Immediately thereafter clearance was issued for a standard range approach, instructing flight 711 to report over the range station and when starting the procedure turn. Shortly thereafter the flight asked clearance to descend. There being no other traffic the controller cleared the flight for an approach and to descend whenever it wished. At 2229 the latest weather observation for the airport, completed at 2228, was transmitted to the flight. Conditions given were: Ceiling 500 feet overcast; visibility 8 miles, very light drizzle; wind west 10. The flight informed the controller it would make a circling approach to runway 31, the active runway. At 2234 the flight reported, “American 711, over the Omni at 34, proceeding to the field.” Approximately two minutes later an explosion was seen and heard north-northwest of the airport and attempts to contact the flight thereafter failed. The aircraft crashed about 0,25 miles short of runway 31 and was destroyed. Both pilots and 11 passengers were killed. A weather observation immediately following the accident was: Ceiling 500 feet overcast; visibility 5 miles, very light drizzle; wind northwest 8; altimeter 29.66.
Probable cause:
The Board determines that the probable cause of this accident was a descent to the ground while approaching the airport caused by the crew’s inattention to their flight instruments and a possible sensory illusion giving them an erroneous impression of the attitude of the aircraft. The following findings were reported:
- Weather conditions at Springfield were above the minimums for an American Airlines Convair aircraft to make a VOR instrument approach and to circle for the landing,
- The flight did not execute the CAA approved VOR instrument approach procedure but proceeded directly from the station toward the airport,
- Analysis of the existing weather conditions indicates that before the aircraft turned toward the airport visual reference with the ground was possible but not probable at the required altitude,
- While approaching the airport the aircraft was nearly on the 193-degree inbound radial required by the VOR instrument approach procedure and was flown visually below the overcast for several miles,
- The aircraft descended until it struck the ground approximately 1-1/14 miles north-northwest of the airport,
- There was no evidence found indicating malfunction or failure of the aircraft and there was no indication of an emergency aboard the aircraft.
Final Report:

Crash of a Convair CV-240-6 in Capilla del Señor

Date & Time: Oct 16, 1954 at 1520 LT
Type of aircraft:
Operator:
Registration:
LV-ADQ
Flight Phase:
Survivors:
Yes
Schedule:
Buenos Aires – Córdoba
MSN:
77
YOM:
1949
Country:
Crew on board:
5
Crew fatalities:
Pax on board:
27
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The aircraft, engaged on a scheduled flight non-stop from Ezeiza to Córdoba, took off from Ezeiza Airport at 1500LT with 27 passengers and 5 crew. The approved flight plan provided for a VFR flight at a cruising level of 1,200 meters. At 1510LT the aircraft asked Buenos Aires ATC for clearance to change its altitude to 600 meters due to a marked frontal belt having been encountered. Shortly after this, the aircraft entered a storm area with rain, hail and strong electrical discharges of increasing intensity which caused uncontrolled loss of altitude. It continued descending until it struck the ground at approximately 1520LT, injuring the pilot, two crew and four passengers.
Probable cause:
Through causes which could not be fully ascertained and in circumstances arising while the aircraft, in attempting to leave the area of a violent storm, was flying at a low altitude, the aircraft was carried into the ground. The following factors were considered as contributory:
- The persistence of the pilot-in-command in attempting in climb, without making use, at the appropriate time, of the full power available to arrest the descent caused, according to his own statement, by meteorological conditions,
- The decision by the pilot-in-command to enter a local storm the violence of which he did not foresee and which he could have circumnavigated as prescribed by the operational standards of the company,
- The fact that the pilot-in-command had no meteorological information relating to the weather conditions he encountered.
Final Report:

Crash of a Convair CV-240-4 off Folkestone: 3 killed

Date & Time: Jun 19, 1954 at 2300 LT
Type of aircraft:
Operator:
Registration:
HB-IRW
Flight Phase:
Survivors:
Yes
Schedule:
Geneva – London
MSN:
61
YOM:
1948
Location:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
While overflying The Channel by night at an altitude of 12,000 feet, the port engine stopped. The captain feathered its propeller, informed ATC about his position and obtained the permission to divert to Manston Airport. Few minutes later, the right engine failed as well. The crew decided to ditch the aircraft about 12 km off Folkestone. After one hour, four crew members and two passengers were rescued by the crew of a boat while three other passengers drowned. The aircraft later sank and was lost.
Probable cause:
Failure of both engine in flight following a fuel exhaustion. It was determined that at the time of the accident, fuel tanks were empty as the aircraft was not refueled prior to takeoff from Geneva Airport. Investigations revealed that the crew requested to refuel before takeoff but for unknown reason, this operation was not completed. Also, both pilots failed to follow the pre-departure checklist and failed to check the fuel jauges prior to departure.

Crash of a Convair CV-240-1 near Wright: 9 killed

Date & Time: Feb 26, 1954 at 1032 LT
Type of aircraft:
Operator:
Registration:
N8407H
Flight Phase:
Survivors:
No
Schedule:
Los Angeles – Las Vegas – Cedar City – Salt Lake City – Casper – Rapid City – Minneapolis
MSN:
37
YOM:
1948
Flight number:
WA034
Location:
Crew on board:
3
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
9
Captain / Total flying hours:
7500
Captain / Total hours on type:
4634.00
Copilot / Total flying hours:
6850
Copilot / Total hours on type:
2300
Aircraft flight hours:
12145
Circumstances:
Western Air Lines' Flight 314 departed Los Angeles, California, on a scheduled flight to Minneapolis, Minnesota, with intermediate stops scheduled at Las Vegas, Nevada; Cedar City and Salt Lake City, Utah; Casper, Wyoming, and Rapid City, South Dakota. The flight was routine to Salt Lake City, where a relief crew consisting of Captain M. R. Cawley, First Officer R. E. Crowther and Stewardess Mary Grace Creagan took over the flight in accordance with company crew assignment schedules. Prior to departure from Salt Lake City the aircraft was refueled to a total of 1,000 gallons, which filled all tanks, Flight 34 departed from the Salt Lake City ramp at 0721, but returned a few minutes later because of a broken nose wheel steering cable. The cable was replaced and Flight 34 was off the ground at 0850. According to company records, at takeoff the gross weight was 36,990 pounds, 2,144 pounds less than the maximum allowable weight of 39,134 pounds; the load was properly distributed so that the center of gravity of the aircraft was within approved limits. There were an passengers. The flight plan filed with Air Route Traffic Control specified Instrument Flight Rules at 15,000 feet via Green 3 and Blue 76 Airways. Eastward from Salt Lake City the Casper weather went below company minimums and Flight 34 elected to overfly this scheduled stop. After being advised of this action by the company Casper radio, Air Route Traffic Control issued a new clearance for the flight to descend to and maintain 13,000 feet to the Rapid City range station via Blue 37 and Red 2 Airways. However, an altitude change to 17,000 feet was requested by the flight and this was authorized by ARTC. At 1010 N8407H reported 17,000 over Casper, estimating the Wright intersection (122 miles west of Rapid City) at 1027. The Flight reported as being over the Wright intersection at 1025, at 17,000 feet, estimating Rapid City at 1050. The Casper company radio operator gave the flight the 0930 en route weather and the 1010 Rapid City Special #2 terminal weather. This, the last radio contact, was acknowledged by the flight at 1027. At 1041 the Rapid City radio operator attempted unsuccessfully to contact the flight to deliver a clearance for an instrument approach to Rapid City. Attempts continued until 1053 and at that time the Denver company dispatcher was advised that contact with the flight had been lost. At 1106 emergency procedures were initiated. Intermittent snows and restricted visibilities hampered intensive air search efforts. The wreckage was sighted by a Western Air Lines pilot the afternoon of February 28, and ground parties reached the scene that night. The aircraft had crashed in an isolated ranch area and all nine occupants had been killed.
Probable cause:
The Board, after intensive study of all evidence, determines that the probable cause of this accident was a sudden emergency of undetermined origin under adverse weather conditions resulting in rapid descent and impact with the ground at high speed. The following findings were reported:
- Weather was a major factor in the accident as heavy to possibly severe turbulence and heavy icing existed in the area,
- The flight was routine until approximately five minutes before the crash,
- A sudden emergency or difficulty of undetermined origin occurred that resulted in rapid descent to the ground; no emergency was declared,
- Both engines were developing power at impact,
- Due to the disintegration of the wreckage it was impossible to definitely determine if structural failure or control malfunctioning had occurred prior to impact.
Final Report: