Crash of a Douglas C-47 in McChord AFB: 4 killed

Date & Time: Sep 18, 1969
Operator:
Flight Phase:
Flight Type:
Survivors:
Yes
Crew on board:
3
Crew fatalities:
Pax on board:
10
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
The aircraft was on a routine flight from McChord AFB to California. At liftoff, the airplane crashed in unknown circumstances. Eight occupants were injured and the aircraft was destroyed. Both pilots and two passengers were killed.
Crew:
Lt Col Robert E. Walker, pilot, †
Cpt Peter Michael Cunningham, copilot, †
T/Sgt Donald G. Love, flight engineer. †
Passengers:
1st Lt Joseph R. Baxter, †
M/Sgt William B. Johnston,
Lt Col Jack S. McKinley,
Sgt William D. Wallace,
T/Sgt Billy D. Byrd,
Sgt Charles L. Andrews,
PO2C Charles B. Nichols,
PO3C Darrell E. Calentine,
M/Sgt Granville Hicks.

Crash of a De Havilland DHC-2 Beaver in Wenatchee: 1 killed

Date & Time: Jul 23, 1969 at 1114 LT
Type of aircraft:
Operator:
Registration:
CF-MGS
Survivors:
Yes
Schedule:
Nanaimo - Friday Harbor - Wenatchee
MSN:
1427
YOM:
1960
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1475
Captain / Total hours on type:
151.00
Circumstances:
Upon landing on a swift river near Wenatchee, the float equipped aircraft crashed and partially sank. The pilot was rescued while the passenger drowned.
Probable cause:
Improper level off on part of the pilot while landing on a swift river. Inadequate preflight preparation on part of the pilot and operations dispatched the flight into an area with no docking facilities.
Final Report:

Crash of a Convair CV-880-22M-3 in Moses Lake: 3 killed

Date & Time: Jun 24, 1969 at 1603 LT
Type of aircraft:
Operator:
Registration:
JA8028
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Moses Lake - Moses Lake
MSN:
22-00-49M
YOM:
1963
Flight number:
JL090
Crew on board:
5
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
7613
Captain / Total hours on type:
25.00
Copilot / Total flying hours:
2773
Copilot / Total hours on type:
32
Aircraft flight hours:
14278
Circumstances:
Shortly after liftoff, the flight instructor reduced power on engine n°4 to check the trainee’s emergency procedures, and the aircraft began to yaw to the right. This yaw-continued to increase until, at a point approximately 6,500 feet down the runway, the right wing went down and the No. 4 engine pod made contact with the runway. In a severe sideslip to the right, the aircraft slid off the runway and thence in a northerly direction through 2,600 feet of rough terrain, breaking up and bursting into flames before it came to rest on an easterly heading. Four crew members escaped from the burning aircraft through a break in the fuselage, but of these four, only two survived. The body of one trainee was later found in the burned cockpit area. Ground impact and fire after impact almost completely destroyed the airplane.
Probable cause:
Delayed corrective action during a simulated critical-engine-out takeoff maneuver resulting in an excessive sideslip from which full recovery could not be effected.
Final Report:

Crash of a Beechcraft 99A Airliner in Pasco: 2 killed

Date & Time: Jun 20, 1969 at 1505 LT
Type of aircraft:
Operator:
Registration:
N2550A
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Pasco - Spokane
MSN:
U-106
YOM:
1969
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
4280
Captain / Total hours on type:
51.00
Circumstances:
Shortly after takeoff from Pasco-Tri-Cities Airport, while in initial climb, the airplane adopted a high angle of attack and nose high attitude. It stalled then crashed in a huge explosion near the airport, killing both pilots.
Probable cause:
Inadequate preflight preparation on part of the pilot and improper operation of flight controls on part of the copilot. It was determined that the airplane pitched up steeply after takeoff as the pitch trim was found in a full nose up position and the pilot-in-command's seat was unlock and found in a full aft position.
Final Report:

Crash of a Beechcraft C-45H Expeditor in Port Angeles: 10 killed

Date & Time: Feb 5, 1969 at 0653 LT
Type of aircraft:
Operator:
Registration:
N8181H
Flight Phase:
Survivors:
No
Schedule:
Port Angeles – Seattle
MSN:
52-10637
YOM:
1952
Flight number:
PGT601
Crew on board:
2
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
10
Captain / Total flying hours:
8358
Captain / Total hours on type:
577.00
Circumstances:
Just after liftoff from Port Angeles-Callam County Airport, the twin engine aircraft encountered difficulties to gain height then stalled and crashed in flames. The airplane was destroyed by impact forces and a post crash fire and all 10 occupants were killed.
Probable cause:
The exact cause of the accident could not be determined with certainty. However, the following findings were reported:
- Premature liftoff for unknown reason,
- Elevator trim full nose down for unknown reason,
- Weight and balance within the prescribed limits,
- It was not possible to know which pilot was at controls at the time of the accident.
Final Report:

Crash of a Lockheed P2V-7 Neptune near Whidbey Island NAS

Date & Time: Jan 3, 1969
Type of aircraft:
Operator:
Registration:
140160
Flight Phase:
Flight Type:
MSN:
726-7063
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Crashed in unknown circumstances in the region of Whidbey Island NAS. Crew fate remains unknown.

Crash of a Beechcraft UC-45B Mk.3T in Seattle

Date & Time: Dec 5, 1968 at 1410 LT
Type of aircraft:
Registration:
CF-RQL
Flight Type:
Survivors:
Yes
MSN:
5980
YOM:
1943
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4207
Captain / Total hours on type:
30.00
Circumstances:
On final approach to Seattle-Boeing Field, both engine failed. The airplane lost height, struck electrical wires and crashed in flames in a parking lot. The pilot was injured and the aircraft was destroyed as well as seven cars.
Probable cause:
The probable causes were:
- Engine failure,
- Mismanagement of fuel,
- Fuel starvation,
- Checklist not followed,
- Fuel selector on nose tank.
Final Report:

Crash of a Boeing KC-135A-BN Stratotanker on Mt Shadow: 9 killed

Date & Time: Jan 19, 1967 at 1800 LT
Type of aircraft:
Operator:
Registration:
56-3613
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Hickam - Fairchild
MSN:
17362
YOM:
1958
Crew on board:
9
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
9
Circumstances:
While descending to Fairchild AFB on a flight from Hickam Field, Hawaii, the airplane was too low and the struck the slope of Mt Shadow (4,337 feet high) located 40 miles northwest of Fairchild AFB. The airplane struck trees and disintegrated on impact, killing all nine crew members.
Probable cause:
Controlled flight into terrain.

Ground explosion of a Lockheed C-141A-LM Starlifter at McChord AFB: 3 killed

Date & Time: Sep 7, 1966
Type of aircraft:
Operator:
Registration:
65-0281
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
6133
YOM:
1965
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
On 7 September, 1966, 65-0281 was the first C-141 destroyed. It blew up while simultaneous hazardous maintenance procedures were being performed. Three maintenance members were killed in an explosion of the Right Extended Range tank. The Wing at McChord had recently converted to the StarLifter. The first aircraft had arrived on 9 August 1966. This aircraft, 65-0281, was the third C-141 to be stationed at McChord, and had arrived on base just a week before, on 29 August, 1966. The maintenance teams had minimal practical experience with the new airplane. It was having multiple maintenance difficulties. The Right Extended Range Tank feel gage was erratic, and the AC "Power On" Light was inop. Two electricians were in the cockpit working on the "Power On" Light. A Maintenance Team Chief was also in the cockpit with three trainees. In addition, he was supervising a maintenance team on another aircraft. The Assistant Team Chief had started de-fueling the Right Extended Range Tank to prepare it for troubleshooting. The other fuel tanks were full. Two additional technicians arrived to work on the fuel gage before the de-fueling was complete. One of the electrical technicians connected testing equipment to the fuel tank but failed to ground it. The other technician plugged an extension cord into the external 115V AC receptacle of the APU. The live extension cord apparently came in contact with the case of the test equipment. Electricity flowed through the case, up the cables into the tank. Due to a short in the coaxial shielding a spark was created within the nearly empty tank. The right wing exploded. The Assistant Team Chief standing under the wing, and the technician on the wing were killed almost immediately. One of the technicians in the cockpit was badly burned while exiting the right troop door into a burning pool of JP-4. He died a few days later. The others on the aircraft received only minor injuries.
Source:
http://www.c141heaven.info/dotcom/65/pic_65_0281.php

Crash of a Travel Air S6000B in Ellensburg: 1 killed

Date & Time: Mar 4, 1966 at 1510 LT
Type of aircraft:
Registration:
N9842
Flight Phase:
Flight Type:
Survivors:
No
MSN:
1036
YOM:
1929
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
254
Captain / Total hours on type:
5.00
Circumstances:
While cruising in poor weather conditions, control was lost and the airplane went into an uncontrolled descent before crashing in a field. The pilot, sole on board, was killed.
Probable cause:
It was determined that the pilot was flying under VFR mode in adverse weather conditions. Control was lost after an overload failure, causing skin and attachments failure in flight.
Final Report: