Crash of a Beechcraft 65 Queen Air in Leonardtown

Date & Time: Jun 2, 1991 at 1130 LT
Type of aircraft:
Operator:
Registration:
N655KJ
Flight Phase:
Survivors:
Yes
Schedule:
Leonardtown - Leonardtown
MSN:
LC-129
YOM:
1962
Crew on board:
1
Crew fatalities:
Pax on board:
11
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2350
Captain / Total hours on type:
150.00
Aircraft flight hours:
6000
Circumstances:
The pilot reported that shortly after takeoff on a parachute jumping flight the left engine lost power, but a second later power was restored. Soon afterwards a total power loss occurred. According to the pilot, the propeller stopped rotating and did not windmill. He did not feather the left propeller. He made a shallow left turn toward an open field, while trying to return to the airport. He was unable to maintain adequate airspeed or altitude, and in order to maintain aircraft control, he reduced power on the right engine. He made a forced landing in a wheat field. The airplane came to a stop and all occupants escaped the airplane before it caught fire. The examination of the airplane did not disclose evidence of mechanical malfunction.
Probable cause:
The loss of power in one engine for undetermined reasons.
Final Report:

Crash of a Casa 212 Aviocar 200 off Patuxent River NAS: 5 killed

Date & Time: Dec 1, 1989 at 0930 LT
Type of aircraft:
Operator:
Registration:
N296CA
Flight Type:
Survivors:
No
Schedule:
Fort Belvoir - Patuxent River
MSN:
296
YOM:
1983
Crew on board:
5
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
5
Circumstances:
Following an uneventful flight from Davison AAF (Fort Belvoir), the aircraft was approaching Patuxent River NAS when, at a height of about 800 feet, the aircraft entered an uncontrolled descent and crashed in the Chesapeake Bay. The wreckage sank by a depth of 45 feet and was found less than 100 yards offshore. All five crew members were killed. The aircraft was operated by the US Army Intelligence and Security Command (INSCOM) and carried both civil N296CA and military 88-0321 registrations.
Probable cause:
It was determined that the crew mistakenly selected beta range on the propellers on final approach at an altitude of 800 feet, causing the aircraft to enter an uncontrolled descent.

Crash of a Beechcraft E18S in Baltimore: 2 killed

Date & Time: Jul 19, 1989 at 0717 LT
Type of aircraft:
Registration:
N138JR
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Baltimore - Winchester
MSN:
BA-41
YOM:
1955
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
11715
Captain / Total hours on type:
6000.00
Aircraft flight hours:
12290
Circumstances:
Shortly after departing from runway 15L at the Baltimore-Washington Intl Airport, the pilot transmitted that he had an emergency consisting of a fire under his side panel. He reported he was going to circle and land. According to witnesses, flames and smoke were in the cockpit area. The aircraft started a gradual descent during a left turn. Subsequently, it crashed into a house. An examination of the wreckage did not reveal the origin of the fire; however, a CB radio was found with evidence that it may have been wired to the aircraft electrical system. The owners stated that the CB was not installed in the aircraft prior to the pilot's use of the plane on that flight. The pilot, sole on board, was killed.
Probable cause:
A fire that erupted in the cockpit of the aircraft (under a side panel). Related factors were: smoke and fumes in the cockpit which reduced the pilot's visual perception and ability to see.
Final Report:

Crash of a Beechcraft 65-A80 Queen Air in Baltimore: 1 killed

Date & Time: Nov 8, 1986 at 1200 LT
Type of aircraft:
Operator:
Registration:
N304D
Survivors:
Yes
Schedule:
Baltimore - Islip
MSN:
LD-226
YOM:
1965
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
2294
Captain / Total hours on type:
24.00
Aircraft flight hours:
7479
Circumstances:
During climb after takeoff, left engine seized. Pilot said he attempted left engine restart; propeller would not rotate or feather. No emergency declared. Pilot stated engine shutdown procedure was used, scientific bus switches were shut off, right generator was recycled and appeared to operate normally. Pilots got immediate vector to return to Martin Airport, but radar contact was lost for about 5 minutes. Electrical problems were encountered and pilots had problems maintaining headings, thus were delayed in diverting to alternate. With left prop unfeathered, they could not maintain altitude. Due to bad weather at Martin, they diverted to Baltimore. Radar and radio contacts were lost and they could not reach Baltimore. During forced landing, aircraft hit tree and crashed short of intended landing area. Teardown of left engine revealed #4 and #5 connecting rods had failed at crankshaft; they were discolored from heat and scored; other rod bearings had indications of oil starvation. Metallic debris from failed engine found in oil system. Several oil feed holes to rod bearings were obstructed with metallic debris. Fire damaged most of the electrical system. Aircraft (modified for environmental testing) not flight tested for drag inducing modifications; written flight crew instructions not avail for modifications. A pilot was killed and three other occupants were injured.
Probable cause:
occurrence #1: loss of engine power (partial) - mech failure/malf
phase of operation: climb - to cruise
findings
1. (c) fluid, oil - starvation
2. (c) engine assembly, connecting rod - failure, total
3. propeller feathering - not possible
4. precautionary landing - initiated
----------
occurrence #2: airframe/component/system failure/malfunction
phase of operation: descent - emergency
findings
5. (c) electrical system - undetermined
6. (f) electrical system, battery - low level
7. flight/nav instruments, heading indicator - false indication
----------
occurrence #3: forced landing
phase of operation: descent - emergency
findings
8. (f) procedures/directives - not followed - pilot in command
9. (f) in-flight planning/decision - improper - pilot in command
10. (f) inadequate training (emergency procedure(s)) - company/operator management
11. (f) insufficient standards/requirements,airman - company/operator mgmt
12. attempted
13. (f) weather condition - low ceiling
14. (f) weather condition - fog
----------
occurrence #4: in flight collision with object
phase of operation: landing - flare/touchdown
findings
15. (f) object - tree(s)
----------
occurrence #5: in flight collision with terrain/water
phase of operation: descent - uncontrolled
Final Report:

Crash of a Piper PA-61 Aerostar (Ted Smith 601P) in Cockeysville: 2 killed

Date & Time: Apr 28, 1984 at 1507 LT
Registration:
N6079R
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Lancaster – Gainesville
MSN:
61P-0735-8063359
YOM:
1980
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
2500
Captain / Total hours on type:
105.00
Circumstances:
On the day of departure the pilot had received a 30 minutes familiarization flight upon completion of the superstar conversion. Emphasis was directed to engine gages, fuel flow and counter, and power settings. The flight was flown at 5,500 feet. The pilot then obtained a weather briefing and filed a flight plan. About 15 minutes after departure, while climbing thru FL170, the pilot radioed that he had lost both engines. The aircraft was subsequently observed descending uncontrolled out of the overcast. At about 1,000 feet agl the right aileron separated. The fuel boost pumps were found in the 'off' position. The AFM states that the boost pumps should be on during climb above 10,000 feet. The pilot had been enrolled in an Aerostar transition school the previous month during which a 2-hr combined demonstration/flight evaluation flight was conducted. The instructor pilot recommended further multi-engine training. Both occupants were killed.
Probable cause:
Occurrence #1: loss of engine power (total) - nonmechanical
Phase of operation: climb - to cruise
Findings
1. (c) flight manuals - not followed - pilot in command
2. (c) fluid, fuel - starvation
3. (c) fuel boost pump selector position - improper - pilot in command
4. (f) lack of total experience in type of aircraft - pilot in command
----------
Occurrence #2: loss of control - in flight
Phase of operation: climb - to cruise
Findings
5. (f) aircraft performance, two or more engines - inoperative
6. (c) aircraft handling - uncontrolled - pilot in command
7. (c) spatial disorientation - pilot in command
8. (f) inadequate recurrent training - pilot in command
----------
Occurrence #3: airframe/component/system failure/malfunction
Phase of operation: descent - uncontrolled
Findings
9. (c) flight control, aileron - overload
10. (c) design stress limits of aircraft - exceeded - pilot in command
11. Flight control, aileron - separation
----------
Occurrence #4: in flight collision with terrain/water
Phase of operation: descent - uncontrolled
Final Report:

Crash of a Piper PA-31-310 Navajo in Cumberland: 3 killed

Date & Time: Mar 5, 1984 at 1107 LT
Type of aircraft:
Operator:
Registration:
N6629L
Survivors:
No
Schedule:
Baltimore - Cumberland
MSN:
31-565
YOM:
1969
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
2143
Captain / Total hours on type:
547.00
Aircraft flight hours:
7361
Circumstances:
Approximately 16 minutes prior to the accident the pilot was cleared for the localizer DME approach. The aircraft collided with the mountainous terrain on a heading of about 220° at approx 8.5 dme on a bearing of 051° from the airport. As indicated on the loc/dme runway 23 approach plate, the minimum altitude between the outer marker, 6.6 dme, and 10 dme was 3,000 feet. Elevation at the accident site was 2,000 feet; airport elevation was 776 feet. Post crash fire consumed most of the wreckage but the cabin heater was not in the fire area. The pilot's reported carboxy hemoglobin (co) was 20%. Autopsy revealed multiple extreme impact injuries. Products of combustion were found on fresh air side of cabin heater/heat exchanger. Source of combustion products were not determined. All three occupants were killed.
Probable cause:
Occurrence #1: in flight collision with terrain/water
Phase of operation: approach - iaf to faf/outer marker (IFR)
Findings
1. Terrain condition - high terrain
2. (f) weather condition - clouds
3. (f) weather condition - fog
4. (f) air cond/heating/pressurization - leak
5. (c) ifr procedure - not followed - pilot in command
6. (c) proper altitude - not maintained - pilot in command
7. (f) physical impairment (carbon monoxide) - pilot in command
----------
Occurrence #2: fire
Phase of operation: other
Final Report:

Crash of a Boeing EC-135N in Walkersville: 21 killed

Date & Time: May 6, 1981 at 1050 LT
Type of aircraft:
Operator:
Registration:
61-0328
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Wright-Patterson - Wright Patterson
MSN:
18235/C13
YOM:
1961
Flight number:
AGAR23
Crew on board:
17
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
21
Aircraft flight hours:
13471
Circumstances:
On 6 May 1981, EC-135N, Serial Number 61-0328, call sign AGAR 23, departed Wright Patterson AFB, Ohio, at 1005 Eastern Daylight Savings Time (EDT) on a routine training mission. On board the aircraft were 17 crewmembers and four authorized passengers. The flight proceeded uneventfully as planned for approximately 45 minutes. Then in a few brief moments, a sequence of very rapid events resulted in a crash with the loss of all onboard. At 1049:48 EDT, The Federal Aviation Administration (FAA) lost radar contact with AGAR 23. The aircraft was cruising at Flight Level 290, at .78 Mach while performing a navigational training leg. The aircraft commander, Capt Emilio, occupied the right pilot seat and a passenger, Mrs. Emilio, occupied the left pilot seat. Also in the crew compartment were the 2 navigators, Lt Col Frederick and Capt Fonke, and 2 passengers, Mrs. Fonke and SSgt Brundige. For undetermined reasons, the aircraft pitch trim moved to the full nose-down position. The aircraft then a rapidly pitched over, most likely upon release of the autopilot, and induced sufficient negative "G" forces to cause the generators to trip off line, resulting in the loss of all AC electrical power. The pitch trim could not then be moved electrically. This condition, while unusual, can be controlled if prompt corrective action is taken; however, if corrective action is delayed approximately 8 seconds, the aircraft pitch angle will be greater than 30 degrees nose-down in the airspeed in excess of 350 knots indicated airspeed. Under these conditions, the aircraft cannot be controlled until the pitch trim is moved toward neutral. While it is evident that recovery was delayed, the reason for the delay is unknown. The aircraft became uncontrollable and entered a steep descent. During the rapid descent, an explosion occurred at approximately 1300 feet above ground level followed immediately by catastrophic failure, and complete break-up of the aircraft. The wreckage was found north of Walkersville and all 21 occupants were killed.
Probable cause:
At 1049:48 EDT, FAA lost radar contact with the aircraft. The aircraft was cruising at flight level 290 at .78 Mach and was performing a navigational training leg. Navigational legs are normally flown on autopilot, and FAA altitude readouts showed the aircraft was within 100 feet of assigned altitude, characteristic of autopilot flight. The aircraft commander, Capt Joseph Emilio, occupied the right pilot seat and a passenger, Mrs. Peggy Emilio, occupied the left pilot seat. Also in the crew compartment were the 2 navigators, Lt Col Benjamin B. Frederick and Capt Donald V. Fonke, and 2 passengers, Mrs. Linda Fonke and SSgt Joseph T. Brundige. This phase of flight, the navigational leg, was the least demanding on the pilot and was the logical time for the passengers to come forward to view the cockpit area. There is no evidence that the presence of the passengers in the crew compartment contributed to, or caused, the accident. For undetermined reasons, the aircraft pitch trim moved to the full nose-down position. The autopilot can overcome the trim until near full nose-down. The aircraft then rapidly pitched over, most likely upon release of the autopilot, and induced sufficient negative "G" forces to cause the generators to trip off line and loss of all AC electrical power. The pitch trim could not then be moved electrically. This condition, while unusual, can be easily controlled if prompt corrective action is taken; however if corrective action is delayed approximately 8 seconds, the aircraft pitch angle will be greater than 30° nose-down in the airspeed in excess of 350 KIAS. Under these conditions, the aircraft cannot be controlled until the pitch trim is moved toward neutral. While it is clear that recovery was delayed, the reason for the delay is unknown. The aircraft became uncontrollable and entered a steep descent. The aircraft emerged from the clouds at 2,000 feet above ground level (AGL) and was intact. Airspeed was in excess of 400 KTAS and die to angle was 20 to 30 degrees. Engine power was above 2.0 engine pressure ratio (EPR). At approximately 1,500 feet mean sea level (MSL) an explosion occurred inside the pressurized compartment of the fuselage and weakened the aircraft structure to the extent that catastrophic failure of the aircraft followed immediately. Cause of this explosion is undetermined; however, the aircraft was in an unrecoverable condition at the time of the explosion and a crash was already inevitable.

Crash of a Rockwell Grand Commander 690 in Goldsboro

Date & Time: Jan 15, 1980 at 0118 LT
Operator:
Registration:
N182
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Hartford - Charlotte
MSN:
690-11048
YOM:
1972
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
9708
Captain / Total hours on type:
948.00
Circumstances:
While in normal cruise on a cargo flight from Hartford to Charlotte by night, the pilot informed ATC about technical problems. The aircraft lost 2,000 feet then entered an uncontrolled descent and eventually crashed in a field. The pilot was seriously injured.
Probable cause:
Uncontrolled descent and subsequent crash due to engine structure issues. The following contributing factors were reported:
- Engine tearaway,
- Engine structure: mount and vibration isolators,
- Material failure,
- Separation in flight,
- Pilot reported pitchup with autopilot off,
- Recovered with light g load,
- Right engine inbound mount pulled out.
Final Report:

Crash of a Piper PA-31T Cheyenne I in Baltimore: 3 killed

Date & Time: Feb 23, 1979 at 1958 LT
Type of aircraft:
Operator:
Registration:
N6123A
Flight Type:
Survivors:
Yes
Schedule:
Lynchburg - Baltimore
MSN:
31-7804008
YOM:
1978
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
6522
Captain / Total hours on type:
136.00
Circumstances:
While on approach to Baltimore-Martin State Airport, the crew encountered poor weather conditions. The visibility was reduced to 1/4 of a mile due to low ceiling and fog. On final, the twin engine airplane struck power cables. The captain increased engine power and initiated a go-around before diverting to Baltimore-Washington-Thurgood Marshall International Airport. On approach, while trailing about 1,500 feet of wire, the airplane went out of control and crashed in flames few hundred yards from the runway threshold. A passenger was seriously injured while three other occupants were killed.
Probable cause:
Collision with wires on final approach and subsequent uncontrolled collision with ground due to improper IFR operation. The following contributing factors were reported:
- Foreign material affecting normal operations,
- Low ceiling,
- Fog,
- Visibility about 1/4 mile or less.
Final Report:

Crash of a Rockwell Aero Commander 500B in Salisbury: 5 killed

Date & Time: Mar 31, 1978 at 1116 LT
Operator:
Registration:
N313UT
Flight Phase:
Survivors:
No
Schedule:
Salisbury - Knoxville
MSN:
500-1183-93
YOM:
1962
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
5600
Captain / Total hours on type:
2412.00
Circumstances:
After takeoff from Salisbury-Wicomico County Regional Airport, while climbing, the pilot reported a double engine failure and attempted to return for an emergency landing. On final, while turning back to airport with the left throttle at idle, the airplane stalled and crashed half a mile short of runway. The aircraft was destroyed and all five occupants were killed.
Probable cause:
Double engine failure during initial climb and subsequent stall and crash due to improperly serviced aircraft by ground crew. The following contributing factors were reported:
- Fuel contamination - exclusive of water in fuel,
- Improper fuel grade,
- Operational supervisory personnel: inadequate supervision/training of ramp crews,
- Failure of both engines,
- Improper emergency procedures,
- Failed to follow approved procedures,
- High obstructions,
- Kerosene mixed with 100LL.
Final Report: