Crash of a Boeing KC-135A-BN Stratotanker near Luke AFB: 4 killed

Date & Time: Mar 13, 1982 at 1050 LT
Type of aircraft:
Operator:
Registration:
57-1489
Flight Type:
Survivors:
No
Schedule:
Phoenix - Luke AFB
MSN:
17560/169
YOM:
1958
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
3604
Captain / Total hours on type:
370.00
Aircraft flight hours:
10650
Circumstances:
The KC-135A aircraft departed Phoenix-Sky Harbor International Airport at 0755 MST for a scheduled 3-hour and 30-minute flight. After completing the navigation leg, the aircraft descended into the Phoenix area for transition at Luke AFB. After completing one TACAN approach at Luke AFB, the KC-135A aircraft was vectored to Phoenix-Sky Harbor International Airport for an ILS touch-and-go landing. The aircraft was then vectored back to the final approach course for a TACAN runway 03 left approach at Luke AFB. The KC-135A aircraft was cleared for the approach to Luke AFB, and after the final approach fix radio call, a midair collision occurred with a Grumman American Yankee civilian aircraft. The empennage of the KC-135A separated, rendering the aircraft incapable of flight and it was destroyed upon ground impact. The Grumman American Yankee aircraft was destroyed during the midair collision. The four crew members in the KC-135A and the two civilians in the Grumman American Yankee were fatalities.
Crew:
LT Col James N. Floor,
Lt Col Ted L. Beam,
Maj Truman R. Young Jr.,
T/Sgt Donald J. Plough.
Probable cause:
The USAF KC-135 was on an IFR flight plan and executing a TACAN 03L approach to Luke AFB. The AA-1 had departed Sky Harbour Airport and had been released by phoenix TRSA. The AA-1 was heading westerly in airspace designated as a special traffic area and was required to have been at or below 2,000 ft msl. A pilot of another aircraft who was trailing the AA-1 stated that a low broken cloud cover was encountered and he had to descend to about 2,000 ft to remain 500 ft below the bases. He stated the pilot of the AA-1 did not descend but appeared to be skimming along in and out of the bases of the clouds. He noticed the KC-135 descending through the cloud deck followed immediately by the collision. The collision occurred about 5 mi south of Luke AFB at an altitude of 2,500 ft msl. The logbook of the AA-1 pilot indicated this was his first trip to the phoenix area. Luke AFB was depicted on the north side of the sectional chart only. VOR airway #16 was split along an e-w line with the northern and southern halves being depicted on each side of the chart.

Occurrence #1: midair collision
Phase of operation: cruise - normal
Findings
1. En route charts - inadequate
2. (c) vfr procedures - improper - pilot in command AA-1
3. (f) lack of familiarity with geographic area - pilot in command AA-1
Final Report:

Crash of a Cessna T207A Skywagon in Grand Canyon

Date & Time: Aug 18, 1981 at 1143 LT
Operator:
Registration:
N6441H
Flight Phase:
Survivors:
Yes
Schedule:
Grand Canyon - Grand Canyon
MSN:
207-0527
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2690
Captain / Total hours on type:
814.00
Circumstances:
The single engine airplane departed Grand Canyon-National Park Airport on a local touristic flight with six passengers and one pilot on board. Few minutes after takeoff, the engine failed. The pilot attempted an emergency landing when the airplane crash landed in a field near Tusayan. The aircraft was destroyed and all seven occupants were seriously injured.
Probable cause:
Engine malfunction during traffic pattern-circling due to mismanagement of fuel. The following contributing factors were reported:
- Fuel starvation,
- Selector valves obstructed,
- Rough/uneven terrain,
- Forced landing off airport on land,
- 15-20 gallons of fuel in right tank,
- 2 gallons of fuel in left tank,
- No fuel flow from selector in right tank position.
Final Report:

Crash of a Cessna T207A Skywagon in Grand Canyon: 1 killed

Date & Time: May 24, 1981 at 1733 LT
Operator:
Registration:
N6324H
Flight Phase:
Survivors:
Yes
Schedule:
Grand Canyon - Grand Canyon
MSN:
207-0483
YOM:
1978
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
2980
Captain / Total hours on type:
257.00
Circumstances:
While completing an on-demand local touristic flight, the engine failed during normal cruise. The pilot reduced his altitude and attempted an emergency landing when the airplane crash landed in rough terrain. A passenger was killed while six other occupants escaped with minor or no injuries.
Probable cause:
Powerplant failure for undetermined reasons. The following contributing factors were reported:
- High density altitude, approximately 5,400 feet
- Rough/uneven terrain,
- Forced landing off airport on land.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in Prescott

Date & Time: Feb 10, 1981 at 0810 LT
Registration:
N27661
Flight Phase:
Survivors:
Yes
Schedule:
Sedona - Prescott - Los Angeles
MSN:
31-7852093
YOM:
1978
Crew on board:
2
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3078
Captain / Total hours on type:
860.00
Circumstances:
After takeoff from Prescott-Ernest A. Love, while in initial climb, the twin engine airplane stalled and crashed. All 10 occupants were injured and the aircraft was destroyed.
Probable cause:
Stall during initial climb due to inadequate maintenance and inspection. The following contributing factors were reported:
- Flight control surfaces: elevator assembly, attachments,
- Improperly secured,
- Inadequate preflight preparation,
- Improperly loaded aircraft,
- 658 lbs over max limit,
- CofG 1.28 inch behind aft limit,
- Nosed up, unable to lower the nose with elevator down.
Final Report:

Crash of a Cessna 404 Titan II in Grand Canyon: 8 killed

Date & Time: Jul 21, 1980 at 1702 LT
Type of aircraft:
Operator:
Registration:
N2683S
Flight Phase:
Survivors:
No
Schedule:
Grand Canyon - Phoenix
MSN:
404-0606
YOM:
1979
Flight number:
YR306
Crew on board:
1
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
8
Captain / Total flying hours:
2474
Captain / Total hours on type:
323.00
Aircraft flight hours:
718
Circumstances:
At 1702, Scenic Airlines flight 306, a Cessna 404, VFR commuter flight to Phoenix, crashed approximately three miles south of runway 21 after takeoff from the Grand Canyon National Park Airport. The aircraft cut a swath through a densely wooded area on a magnetic heading of 165° and came to rest upright about 230 feet from the initial point of impact with trees. Impact forces and an intense fire destroyed the aircraft. The pilot and six of the seven passengers were killed in the accident. One passenger survived the accident but died five days later as a result of thermal injuries.
Probable cause:
The probable cause of the accident was a substantial loss of power from the left engine at a critical point in the takeoff an the failure of the pilot to establish a minimum drag configuration which degraded the marginal single-engine climb performance of the aircraft. The loss of power resulted from the seizure of the turbocharger following a progressive failure of the turbine wheel blades initiated by foreign object ingestion which had occurred previous to this flight and was not detected during maintenance on the engine 4 days before the accident.
Final Report:

Crash of a McDonnell Douglas MD-81 in Yuma

Date & Time: Jun 19, 1980 at 1849 LT
Type of aircraft:
Operator:
Registration:
N1002G
Flight Type:
Survivors:
Yes
Schedule:
Yuma-Yuma
MSN:
48001
YOM:
1979
Location:
Crew on board:
3
Crew fatalities:
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8200
Captain / Total hours on type:
150.00
Copilot / Total flying hours:
3199
Copilot / Total hours on type:
223
Aircraft flight hours:
6
Circumstances:
The airplane skidded off the right side of runway 21R while attempting a simulated hydraulic-systems-inoperative landing at the Yuma International Airport, Yuma, Arizona. The aircraft came to rest about 6,700 feet beyond the landing threshold of the runway. Although the aircraft was damaged substantially the three flightcrew members were not injured. There were no passengers. The weather was clear and the runway was dry. The aircraft was on an FAA certification test flight to demonstrate compliance with a special condition to 14 CFR Part 25. The purpose of the flight was to show that the aircraft could be controlled adequately and landed safely with a complete failure of its hydraulic systems. The aircraft landed about 1,735 feet beyond the threshold of runway 21R, and the pilot deployed the thrust reverses and applied reverse thrust before the nosewheel touched down. The aircraft began to yaw, continued to yaw after the nosewheel touched down, it then ground looped to the right, and slid off the right side of the runway. All three crew members were slightly injured and the aircraft was damaged beyond repair.
Probable cause:
Inadequate procedures established for certification test flight, and the pilot's mismanagement of thrust following the initial loss of directional control.
Final Report:

Crash of a Cessna 421B Golden Eagle II in Tucson: 2 killed

Date & Time: Mar 14, 1980 at 1645 LT
Operator:
Registration:
N59RZ
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Tucson - Tucson
MSN:
421B-0249
YOM:
1972
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
9590
Circumstances:
The twin engine airplane departed Tucson-Ryan Airport on a local post maintenance flight, carrying one pilot and one mechanic. During initial climb, the airplane went out of control and crashed in flames in a field. Both occupants were killed.
Probable cause:
Airframe failure during climb due to inadequate maintenance and inspection. The following contributing factors were reported:
- Airframe - flight control surfaces: elevator assembly, attachments, missing, flutter,
- Overload failure,
- Bolts missing from elevators,
- Elevator push-pull tube rivets failed,
- Overload elevator/stabilizers twisted.
Final Report:

Crash of a Martin 404 in Grand Canyon

Date & Time: Nov 16, 1979 at 1452 LT
Type of aircraft:
Operator:
Registration:
N40438
Flight Phase:
Survivors:
Yes
Schedule:
Grand Canyon - Las Vegas
MSN:
14173
YOM:
1952
Flight number:
KS2504
Crew on board:
3
Crew fatalities:
Pax on board:
41
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
13000
Captain / Total hours on type:
1500.00
Copilot / Total flying hours:
9600
Copilot / Total hours on type:
100
Aircraft flight hours:
30451
Circumstances:
On November 16, 1979, Nevada Airlines, Inc., Flight 2504, a Martin 404 (N40438), was a chartered flight from Las Vegas, Nevada, to Grand Canyon National Park Airport, Tusayan, Arizona, and return. About 0935 / Flight 2504 departed Las Vegas to carry a French tour group to the Grand Canyon for a sightseeing tour. There were 41 passengers and a crew of 3 aboard for the roundtrip. The crew and passengers reported that the trip from Las Vegas to Tusayan was routine. After a scenic flight over the Grand Canyon, a landing was made at Tusayan after about 1 hr 10 min of flight time. No fuel, oil, or antidetonate (ADI) fluid was taken on, and no baggage was placed aboard at Tusayan. Takeoff for the return flight was started at 1450 from runway 3. The copilot was to make the takeoff from the right seat. The weather was clear, visibility unlimited, and winds were from 040° at 15 kns. The crew stated that all pretakeoff checklist items were completed and that the takeoff roll was normal. The captain said that he checked the engine instruments at V speed, takeoff safety speed, as the aircraft was rotated for takeoff and "everything was normal." He said he raised the landing gear and, almost immediately thereafter, sensed a loss of power from the left engine. He said he took control of the aircraft from the copilot and noticed that the left engine autofeather light was illuminated and the feather button depressed. About 1451:20, the tower local controller stated, '...do you want to come back?" The captain-said he told the copilot to advise the tower that the flight had lost an engine and was returning to the airport. At 1451:50, the copilot told the tower, '... we're (sic) lost an engine and we want to come back around." The local controller cleared the aircraft as requested. There was no reply from Flight 2504. The captain stated that he noticed a 200-fpm rate of climb when the aircraft reached the departure end of the runway. He said that after passing the runway the aircraft encountered a downdraft and turbulence which overcame the single engine climb performance of the aircraft. He said that, as the engine failure emergency checklist was being accomplished, he made a slight left turn to avoid a radio tower along the flightpath. The copilot stated that the aircraft passed to the left of and below the top of the tower; the top of the tower is 6,739 feet, about 100 feet above the ground. Even though she was aware of an engine problem, the flight attendant stated that she was not aware that an engine had failed. She said she was not warned by the cockpit crew about the impending crash. The passengers recalled hearing no unusual noises during the takeoff; however, several of them saw the left propeller stop shortly after the aircraft left the ground. Several passengers stated that, once the aircraft was airborne and after the left engine had failed, they experienced a "rocking" movement of the aircraft. One passenger, a pilot who was seated at the front of the cabin, said he was aware that the left propeller had been feathered and that, immediately thereafter, the aircraft began to descend. None of the passengers interviewed, were aware that the aircraft was going to crash until they heard the noise of a tree strike. They said there was no warning given by the crew. Several witnesses on the ground stated that they saw the aircraft flying low with the left propeller stationary. Some reported that the landing gear was up. No witnesses reported smoke, fire, or any other problems with the aircraft before impact. The airport tower personnel stated that they saw the left propeller stop when the aircraft was abeam of their position in the tower and slightly below the top of the tower. The tower is located about 6,000 ft from the beginning of Flight 2504's takeoff roll. Tower personnel stated that the aircraft never climbed over 100 ft above the ground level. They said the aircraft banked slightly to the left and descended into the trees. They activated the crash notification circuit when they realized an accident was inevitable. The captain stated that he "was making it except for the downdrafts," and he noticed that the airspeed had decreased to 105 knots; V2 was about 101,5 knots. He said that when he saw that the temperature of the right engine cylinder head was rising rapidly toward the maximum limit, he reduced the manifold pressure about 2 inHg to avoid engine failure. However, he said the inability of the aircraft to climb and the proximity of the terrain required that he return the right engine to full power and select a forced-landing area. The captain stated that, since terrain surrounding the airport was heavily wooded, he headed for the clear area north of the field. He said that when he realized that he would not clear two tall trees before reaching the clear area, he lowered the nose slightly and "flew through the trees." The cockpit struck one of the trees, shattering the captain's windshield. The captain said the aircraft lost about 20 kns of airspeed when it struck the trees and the aircraft began to roll to the left; minimum control speed with the left engine inoperative was about 91 kns. He further reduced the power on the right engine, rolled the wings level, and rotated the aircraft so that it would strike the ground in a nose-high altitude. Both pilots said they hit the ground three times, with each impact becoming progressively more severe. The aircraft came to rest about 850 ft beyond the point where the first trees were struck. The crashpath was oriented on a heading of 355°, and the fuselage came to rest on a heading of 070°. A fire broke out on the right side of the aircraft as it slid to a stop. The fire originated near the cockpit, which had twisted to the left about 120°. Three crew members and seven passengers were seriously injured while 34 other occupants escaped with minor injuries. The aircraft was written off.
Probable cause:
The unwanted autofeather of the left propeller just after take-off and an encounter with turbulence and downdrafts, a combination which exceeded the aircraft's single-engine climb capability which had been degraded by the high density altitude and a turn to avoid an obstacle in the flight path. Also, the available climb margin was reduced by the rising terrain along the flight path. The cause(s) for the unwanted autofeather of the left propeller could not be determined.
Final Report:

Crash of a Fairchild C-119L Flying Boxcar near Casa Grande: 4 killed

Date & Time: Jul 8, 1979 at 2100 LT
Operator:
Registration:
N1040E
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Chandler - Chandler
MSN:
11270
YOM:
1953
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
The crew departed Chandler-Stellar Airpark on a local flight. En route, one of the engine failed. The pilot attempted an emergency landing when the airplane crashed in flames in an open field. The aircraft was destroyed and all four occupants were killed.
Probable cause:
Controlled collision with ground after pilot attempted an emergency landing due to engine problems. The following contributing factors were reported:
- Engine structure: master and connecting rods,
- Engine structure: piston, piston rings,
- Material failure,
- Intentional wheels-up landing,
- Complete failure of one engine,
- Forced landing off airport on land.
Final Report:

Crash of a Cessna 401B in Phoenix

Date & Time: Jun 5, 1979 at 1708 LT
Type of aircraft:
Operator:
Registration:
N77MG
Survivors:
Yes
Schedule:
Long Beach - Phoenix
MSN:
401B-0006
YOM:
1969
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
519
Captain / Total hours on type:
140.00
Circumstances:
While descending to Phoenix Airport, both engines failed simultaneously. The pilot reduced his altitude and attempted an emergency landing few miles from the airfield. The aircraft came to rest on its belly and was damaged beyond repair. The pilot escaped unhurt.
Probable cause:
Controlled collision with ground following a mismanagement of fuel. The following contributing factors were reported:
- Fuel starvation,
- Failed to follow approved procedures,
- Improper emergency procedures,
- Wet, soft ground,
- Complete failure of both engines,
- Forced landing off airport on land,
- Pilot did not recall changing fuel selector after power loss,
- Tip tanks separated and burned,
- Left auxiliary tank empty,
- Right auxiliary tank demolished.
Final Report: