Crash of a Lockheed 18-56 LodeStar in Coolangatta: 21 killed

Date & Time: Mar 10, 1949 at 0950 LT
Type of aircraft:
Operator:
Registration:
VH-BAG
Flight Phase:
Survivors:
No
Schedule:
Coolangatta – Brisbane
MSN:
2194
YOM:
1942
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
18
Pax fatalities:
Other fatalities:
Total fatalities:
21
Captain / Total flying hours:
2300
Copilot / Total flying hours:
1700
Circumstances:
Shortly after takeoff from Coolangatta Airport, while climbing to a height of some 250 feet, the aircraft banked right and then to the left. It went out of control and crashed in flames in a swamp. The aircraft was partially destroyed by a post impact fire and all 21 occupants were killed.
Probable cause:
The accident was caused by the aircraft being loaded so its centre of gravity was behind the rear limit. The report also stated that incorrect setting of the elevator trim tab may have been a contributory cause. The rear limit for the centre of gravity was 39% of Mean Aerodynamic Chord. The load sheet prepared for the fatal flight indicated the centre of gravity of VH-BAG was at 39.2% of Mean Aerodynamic Chord. The load sheet was based on a load chart prepared by the Department of Civil Aviation and based on information supplied by the RAAF. During the investigation, inquiries were made with the US Civil Aeronautics Administration and this revealed an error in the load chart. The main undercarriage of the Lockheed Lodestar retracted to the rear so that retraction caused the centre of gravity to move rearwards but this was not taken into account in the design of the load chart. Other errors also came to light. The passenger seats were 1 inch (25 mm) further apart than shown on the load chart, causing the centre of gravity to be further to the rear than calculated, especially when the aircraft was fully loaded. Up to 18 kilograms (40 lb) of food and beverages for the passengers were stored at the rear of the passenger cabin but were not taken into account on the load chart. Investigation of the accident concluded that after the aircraft's undercarriage retracted, the centre of gravity would have been at about 43.4% of Mean Aerodynamic Chord. With the centre of gravity 4% of MAC behind the rear limit the aircraft would have been tail-heavy and longitudinally unstable. The aircraft had been in daily civil operations in Australia since November 1946 so the investigators assumed there must have been numerous flights with the centre of gravity significantly more than 39% of Mean Aerodynamic Chord. It was necessary for the investigators to find something unique about the fatal flight of VH-BAG that would explain its sudden climb immediately after take-off and the pilot's inability to regain control and prevent the aircraft crashing. The aircraft's tail was one of the few parts of the aircraft not destroyed by fire. The position of the elevator trim tab spool appeared to be in the normal position for landing rather than a typical position for take-off. The investigators concluded that on the final takeoff it was likely that the elevator trim tab was still set for landing. This, coupled with the aircraft being tail-heavy and longitudinally unstable after undercarriage retraction, caused the aircraft to pitch nose-up so strongly that the pilot was unable to retain control or prevent the aircraft stalling. Minister for Civil Aviation Arthur Drakeford made a public announcement that the accident had occurred because the aircraft was tail-heavy and unstable as the result of incorrect loading. The Minister said the operator had not taken adequate steps to ensure safe loading of its aircraft and he hinted that stricter regulation of the loading of aircraft was being considered.

Crash of a De Havilland DH.84 Dragon in Mingende: 1 killed

Date & Time: Dec 31, 1948
Type of aircraft:
Registration:
VH-AMO
Flight Type:
Survivors:
No
Schedule:
Wewak – Mingende
MSN:
2067
YOM:
1943
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
Crashed in flames while landing in Mingende. The aircraft was destroyed by a post crash fire and the pilot John Glover was killed. He was the father of the Catholic Mission of the Holy Ghost and was performing a cargo flight from Wewak to Mingende, delivering goods for the New Year's day.

Crash of a Douglas DC-3-232 in Mangalore

Date & Time: Dec 29, 1948
Type of aircraft:
Operator:
Registration:
VH-UZJ
Flight Type:
Survivors:
Yes
Schedule:
Launceston - Melbourne
MSN:
2002
YOM:
1937
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew (two pilots and one stewardess) was positioning from Launceston to Melbourne. On approach to Essendon, poor weather conditions forced ATC to close the airport to all trafic and VH-UZJ was diverted to Mangalore Airport. On approach, the aircraft was too low, crashed in a field and broke in two. All three crew members were injured and the aircraft was written off.
Probable cause:
Poor judgement on part of the pilot who continued the approach at an unsafe altitude.

Crash of an Airspeed AS.10 Oxford I in Mt Ruahine: 3 killed

Date & Time: Nov 30, 1948
Type of aircraft:
Operator:
Registration:
NZ1227
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Napier - Ohakea
MSN:
2609
YOM:
1940
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
While cruising in the region of Hawletts Hut, the twin engine aircraft went out of control and crashed in a dense wooded area located in the Ruahine Mountain Range. All three crew members were killed. It is believed that the aircraft suffered a structural failure in flight.

Crash of a Boeing B-29A-60-BN Superfortress off Fais Island

Date & Time: Nov 12, 1948
Type of aircraft:
Operator:
Registration:
44-62076
Flight Phase:
Survivors:
Yes
MSN:
11553
Region:
Crew on board:
10
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
While conducting a reconnaissance mission for a missing B-29 & its crew from the 23rd Reconnaissance Squadron since November 7, 1948, the aircraft suffered multiple failures of its navigation & radio systems and eventually run out of fuel. The captain ditched the aircraft in shallow water off Fais Island, about 250 km northeast of Yap Island. The aircraft sank and was lost while all ten crew members were later rescued by the crew of a Navy Catalina.

Crash of a Douglas DC-3-232 in Mount Macedon: 3 killed

Date & Time: Nov 8, 1948 at 0740 LT
Operator:
Registration:
VH-UZK
Flight Phase:
Survivors:
Yes
Site:
Schedule:
Melbourne – Deniliquin
MSN:
2003
YOM:
1937
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
19
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
The aircraft christened 'Kurana' left Melbourne-Essendon at 0726LT bound for Deniliquin. Fourteen minutes later, the crew encountered low visibility due to clouds. At an altitude of 3,000 feet, the crew increased power on both engines to gain height but the aircraft hit trees and crashed in flames in a wooded area. All 19 passengers and the stewardess were injured while all three crew members were killed as the cockpit was destroyed.
Probable cause:
The cause of the aircraft striking high ground whilst flying in cloud at a height of approximately 3,000 feet was that:
a) The pilot failed to follow the track specified in his flight plan and deviated about nine miles to port of the correct track. This deviation was either deliberate or due to an error in navigation.
b) The pilot failed to comply with the visual flight rules' requirements, thus violating the conditions of his flight clearance.

Crash of a Lockheed 10A Electra in Mt Ruapehu: 13 killed

Date & Time: Oct 23, 1948 at 1415 LT
Type of aircraft:
Operator:
Registration:
ZK-AGK
Flight Phase:
Survivors:
No
Site:
Schedule:
Palmerston North – Hamilton
MSN:
1128
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
10
Pax fatalities:
Other fatalities:
Total fatalities:
13
Circumstances:
En route, the crew encountered marginal weather conditions with strong winds and rain showers. In low visibility, the aircraft christened 'Kaka' hit the slope of Mt Ruapehu and disintegrated on impact, killing all 13 occupants. The aircraft was off course at the time of the accident.
Probable cause:
Failure of the crew to take the appropriate measures to follow the correct track. However, strong winds and the lack of radio navigational beacon was considered as a contributory factor.

Crash of a Consolidated PB2B-2 Catalina on Lord Howe Island: 7 killed

Date & Time: Sep 28, 1948 at 1930 LT
Type of aircraft:
Operator:
Registration:
A24-381
Flight Type:
Survivors:
Yes
Site:
Schedule:
Lord Howe Island - Lord Howe Island
MSN:
61163
Country:
Region:
Crew on board:
9
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
7
Circumstances:
Rathmines-based No 11 Squadron suffered the loss of a Catalina amphibian and seven crewmen in a night crash on Lord Howe Island on this day. The aircraft had completed the outward leg of a navigation exercise to the island and altered course for home when a serious fuel leak began filling the compartment with petrol vapor 20 minutes into the return leg. The captain decided to turn back to Lord Howe and attempt a landing on the island’s sheltered lagoon. After crossing the island west to east, the aircraft turned back before clipping the ridge line below Malabar Hill at about 1930LT. The Catalina careered down the slope before exploding in flames. Local residents who rushed to the scene extracted two seriously injured crew from the wreck. The death toll was the highest suffered by the RAAF in a peacetime accident up until that time.
Crew (11th Squadron):
F/Lt Malcolm D. Smith, †
F/Lt James McCoy, †
F/Lt William D. Keller, †
F/Lt Alex McKenzie, †
Sydney L. Piercey, pilot, †
W/O Sydney H. Bacon, †
W/O Donald E. Salis, †
F/LT Bert R. Bradley,
W/O John D. Lea.
Source:
http://airpower.airforce.gov.au/HistoryRecord/HistoryRecordDetail.aspx?rid=534

Crash of a Douglas C-47A-50-DL near Quirindi: 13 killed

Date & Time: Sep 2, 1948 at 2015 LT
Operator:
Registration:
VH-ANK
Flight Phase:
Survivors:
No
Site:
Schedule:
Brisbane – Sydney
MSN:
9999
YOM:
1943
Flight number:
ANA331
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
10
Pax fatalities:
Other fatalities:
Total fatalities:
13
Circumstances:
While cruising in low visibility due to marginal weather conditions, the aircraft hit the slope of Square Peak (4,600 feet) located in the region of Quirindi. The wreckage was found few hours later and all 13 occupants were killed. At the time of the accident, the aircraft was off course by 100 miles.
Probable cause:
Investigations were unable to determine the exact cause of the accident. However, the inquiry found that the probable cause of the crash was interference with the airplane's magnetic compass due to a nearby electrical storm and a defect in the navigational signals sent by the Government-maintained Kempsey low-frequency radio range station, an important navigational aid to flights in the area. Errors and deficiencies in the aeronautical charts used to navigate the mountainous area were also found.

Crash of a De Havilland DH.80 Puss Moth off Oamaru: 1 killed

Date & Time: Aug 25, 1948
Operator:
Registration:
ZK-AJW
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Invercargill – Christchurch
MSN:
2046
YOM:
1930
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
While cruising in foggy conditions, the single engine aircraft went out of control and crashed into the sea near the Waitaki River mouth, northeast of Oamaru. The dead body of the pilot and owner A. J. McIntosh was found on a beach a week later, on September 1st, 1948. Some debris of the aircraft were also found.