Crash of a Cessna 340A in Ponoka

Date & Time: Nov 13, 2018 at 1815 LT
Type of aircraft:
Operator:
Registration:
C-GMLS
Flight Type:
Survivors:
Yes
MSN:
340A-0771
YOM:
1979
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On approach to Ponoka-Labrie Field, the pilot encountered technical problems with the autopilot and decided to make a go-around. While in the circuit pattern, the autopilot failed to disconnect properly so the pilot attempted an emergency landing in a field. The airplane belly landed then contacted trees. Upon impact, the tail was torn off and the aircraft came to rest. The pilot was seriously injured.

Crash of a Gulfstream 690C Jetprop 840 off Myrtle Beach

Date & Time: Nov 12, 2018 at 1415 LT
Operator:
Registration:
N840JC
Flight Type:
Survivors:
Yes
Schedule:
Greater Cumberland - Myrtle Beach
MSN:
690-11676
YOM:
1981
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
22335
Aircraft flight hours:
8441
Circumstances:
The airplane sustained substantial damage when it collided with terrain during an approach to landing at the Myrtle Beach International Airport (MYR), Myrtle Beach, South Carolina. The commercial pilot was seriously injured. The airplane was privately owned and operated under the provisions of Title 14 Code of Federal Regulations Part 91 as a personal flight. Instrument meteorological conditions prevailed, and an instrument flight rules flight plan was filed for the flight that departed Greater Cumberland Regional Airport (CBE), Cumberland, Maryland. According to the pilot, he was following radar vectors for the downwind leg of the traffic pattern to runway 36 at MYR. He turned for final approach and was inside the outer marker, when he encountered heavy turbulence. As he continued the approach, he described what he believed to be a microburst and the airplane started to descend rapidly. The pilot added full power in an attempt to climb, but the airplane continued to descend until it collided with the Atlantic Ocean 1 mile from the approach end of runway 36. A review of pictures of the wreckage provided by a Federal Aviation Administration inspector revealed the cockpit section of the airplane was broken away from the fuselage during the impact sequence. At 1456, the weather recorded at MYR, included broken clouds at 6,000 ft, few clouds at 3,500 ft and wind from 010° at 8 knots. The temperature was 14°C, and the dew point was 9°C. The altimeter setting was 30.27 inches of mercury. The airplane was retained for further examination.
Probable cause:
An encounter with low-level windshear and turbulence during the landing approach, which resulted in a loss of airplane control.
Final Report:

Crash of a Lockheed C-130E Hercules at Chaklala-Nur Khan AFB

Date & Time: Nov 9, 2018 at 1438 LT
Type of aircraft:
Operator:
Registration:
4180
Flight Type:
Survivors:
Yes
Schedule:
Chaklala - Chaklala
MSN:
4180
YOM:
1966
Country:
Region:
Crew on board:
9
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was completing a training mission at Chaklala-Nur Khan AFB in Islamabad. Upon touchdown, a tyre burst. Control was lost and the airplane veered off runway to the right and collided with a concrete wall before coming to rest, burstin into flames. All nine occupants escaped uninjured while the aircraft was destroyed by a post crash fire. It is believed that the landing was hard.

Crash of a Boeing 757-23N in Georgetown: 1 killed

Date & Time: Nov 9, 2018 at 0253 LT
Type of aircraft:
Operator:
Registration:
N524AT
Survivors:
Yes
Schedule:
Georgetown – Toronto
MSN:
30233/895
YOM:
1999
Flight number:
OJ256
Country:
Crew on board:
8
Crew fatalities:
Pax on board:
120
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The airplane departed Georgetown-Cheddi Jagan Airport at 0209LT on an international schedule flight to Toronto-Lester Bowles Pearson Airport, carrying 120 passengers (118 adults and two children) and 8 crew members. At 0222LT, while climbing to 21,000 feet, the crew encountered technical problems with the hydraulic systems and was cleared to return. The captain made a 180 turn and followed a circuit and a holding pattern to burn fuel until he started the final approach to runway 06. After touchdown, the crew started the braking procedure but the airplane was apparently unable to stop within the remaining distance. Approaching the end of the runway, the aircraft veered to the right, lost its right main gear and came to rest in a sandy area with the right engine torn off and the right wing severely damaged. All 128 occupants evacuated, among them six were injured. One week later, on November 16, a 86 year old woman died from her injuries (fractured skull).

Crash of a Boeing 747-412F in Halifax

Date & Time: Nov 7, 2018 at 0506 LT
Type of aircraft:
Operator:
Registration:
N908AR
Flight Type:
Survivors:
Yes
Schedule:
Chicago – Halifax
MSN:
28026/1105
YOM:
1997
Flight number:
KYE4854
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
21134
Captain / Total hours on type:
166.00
Copilot / Total flying hours:
7404
Copilot / Total hours on type:
1239
Aircraft flight hours:
92471
Aircraft flight cycles:
16948
Circumstances:
The Sky Lease Cargo Boeing 747-412F aircraft (U.S. registration N908AR, serial number 28026) was conducting flight 4854 (KYE4854) from Chicago/O’Hare International Airport, Illinois, U.S., to Halifax/Stanfield International Airport, Nova Scotia, with 3 crew members, 1 passenger, and no cargo on board. The crew conducted the Runway 14 instrument landing system approach. When the aircraft was 1 minute and 21 seconds from the threshold, the crew realized that there was a tailwind; however, they did not recalculate the performance data to confirm that the landing distance available was still acceptable, likely because of the limited amount of time available before landing. The unexpected tailwind resulted in a greater landing distance required, but this distance did not exceed the length of the runway. The aircraft touched down firmly at approximately 0506 Atlantic Standard Time, during the hours of darkness. After the firm touchdown, for undetermined reasons, the engine No. 1 thrust lever was moved forward of the idle position, causing the speed brakes to retract and the autobrake system to disengage, increasing the distance required to bring the aircraft to a stop. In addition, the right crab angle (4.5°) on initial touchdown, combined with the crosswind component and asymmetric reverser selection, caused the aircraft to deviate to the right of the runway centreline. During the landing roll, the pilot monitoring’s attention was focused on the lateral drift and, as a result, the required callouts regarding the position of the deceleration devices were not made. Although manual brake application began 8 seconds after touchdown, maximum braking effort did not occur until 15 seconds later, when the aircraft was 800 feet from the end of the runway. At this position, it was not possible for the aircraft to stop on the runway and, 5 seconds later, the aircraft departed the end of the runway at a speed of 77 knots and came to a stop 270 m (885 feet) past the end. The aircraft struck the approach light stanchions and the localizer antenna array. The No. 2 engine detached from its pylon during the impact sequence and came to rest under the left horizontal stabilizer, causing a fire in the tail section following the impact. The emergency locator transmitter activated. Aircraft rescue and firefighting personnel responded. All 3 crew members received minor injuries and were taken to the hospital. The passenger was not injured. During the overrun, the aircraft crossed a significant drop of 2.8 m (9 feet) approximately 166 m (544 feet) past the end of the runway and was damaged beyond repair.
Probable cause:
Findings as to causes and contributing factors:
These are conditions, acts or safety deficiencies that were found to have caused or contributed to this occurrence.
1. The ineffective presentation style and sequence of the NOTAMs available to the crew and flight dispatch led them to interpret that Runway 23 was not available for landing at Halifax/Stanfield International Airport.
2. The crew was unaware that the aircraft did not meet the pre-departure landing weight requirements using flaps 25 for Runway 14.
3. Due to the timing of the flight during the nighttime circadian trough and because the crew had had insufficient restorative sleep in the previous 24 hours, the crew was experiencing sleep-related fatigue that degraded their performance and cognitive functioning during the approach and landing.
4. Using unfactored (actual) landing distance charts may have given the crew the impression that landing on Runway 14 would have had a considerable runway safety margin, influencing their decision to continue the landing in the presence of a tailwind.
5. When planning the approach, the crew calculated a faster approach speed of reference speed + 10 knots instead of the recommended reference speed + 5 knots, because they misinterpreted that a wind additive was required for the existing conditions.
6. New information regarding a change of active runway was not communicated by air traffic control directly to the crew, although it was contained within the automatic terminal information service broadcast; as a result, the crew continued to believe that the approach and landing to Runway 14 was the only option available.
7. For the approach, the crew selected the typical flap setting of flaps 25 rather than flaps 30, because they believed they had a sufficient safety margin. This setting increased the landing distance required by 494 feet.
8. The crew were operating in a cognitive context of fatigue and biases that encouraged anchoring to and confirming information that aligned with continuing the initial plan, increasing the likelihood that they would continue the approach.
9. The crew recognized the presence of a tailwind on approach 1 minute and 21 seconds from the threshold; likely due to this limited amount of time, the crew did not recalculate the performance data to confirm that the runway safety margin was still acceptable.
10. An elevated level of stress and workload on short final approach likely exacerbated the performance-impairing effects of fatigue to limit the crew’s ability to determine the effect of the tailwind, influencing their decision to continue the approach.
11. The higher aircraft approach speed, the presence of a tailwind component, and the slight deviation above the glideslope increased the landing distance required to a distance greater than the runway length available.
12. After the firm touchdown, for undetermined reasons, the engine No. 1 thrust lever was moved forward of the idle position, causing the speed brakes to retract and the autobrake system to disengage, increasing the distance required to bring the aircraft to a stop.
13. The right crab angle (4.5°) on initial touchdown, combined with the crosswind component and asymmetric reverser selection, caused the aircraft to deviate to the right of the runway centreline.
14. During the landing roll, the pilot monitoring’s attention was focused on the lateral drift and, as a result, the required callouts regarding the position of the deceleration devices were not made.
15. The pilot flying focused on controlling the lateral deviation and, without the benefit of the landing rollout callouts, did not recognize that all of the deceleration devices were not fully deployed and that the autobrake was disengaged.
16. Although manual brake application began 8 seconds after touchdown, maximum braking effort did not occur until 15 seconds later, when the aircraft was 800 feet from the end of the runway. At this position, it was not possible for the aircraft to stop on the runway and, 5 seconds later, the aircraft departed the end of the runway at a speed of 77 knots and came to a stop 270 m (885 feet) past the end of the runway.
17. During the overrun, the aircraft crossed a significant drop of 2.8 m (9 feet) approximately 166 m (544 feet) past the end of the runway and was damaged beyond repair. While this uneven terrain was beyond the 150 m (492 feet) runway end safety area proposed by Transport Canada, it was within the recommended International Civil Aviation Organization runway end safety area of 300 m (984 feet).

Findings as to risk:
These are conditions, unsafe acts or safety deficiencies that were found not to be a factor in this occurrence but could have adverse consequences in future occurrences.
1. If the pilot monitoring does not call out approach conditions or approach speed increases, the pilot flying might not make corrections, increasing the risk of a runway overrun.

Other findings:
These items could enhance safety, resolve an issue of controversy, or provide a data point for future safety studies.
1. The investigation concluded that there was no reverted rubber hydroplaning and almost certainly no dynamic hydroplaning during this occurrence.
2. Although viscous hydroplaning can be expected on all wet runways, the investigation found that when maximum braking effort was applied, the aircraft braking was consistent with the expected braking on Runway 14 under the existing wet runway conditions.
Final Report:

Crash of a Sukhoi Superjet 100-95B in Yakutsk

Date & Time: Oct 10, 2018 at 0321 LT
Type of aircraft:
Operator:
Registration:
RA-89011
Survivors:
Yes
Schedule:
Ulan-Ude - Yakutsk
MSN:
95019
YOM:
2012
Flight number:
SYL414
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
87
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
13125
Captain / Total hours on type:
1080.00
Copilot / Total flying hours:
3200
Copilot / Total hours on type:
1300
Aircraft flight hours:
8115
Aircraft flight cycles:
3320
Circumstances:
Following an uneventful flight from Ulan-Ude, the crew initiated the approach to Yakutsk-Platon Oyunsky Intl Airport Runway 23L. Due to work in progress, the runway 05R threshold was displaced by 1,150 metres, reducing the landing distance to 2,248 metres for the runway 23L on which the touchdown zone lighting system was unserviceable. On approach, the crew was informed by ATC that the friction coefficient was 0,45. The crew completed the landing on runway 23L with a slight tailwind component of 4 knots and started the braking procedure. Unable to stop within the remaining distance, the aircraft overran, entered the construction area and collided with the junction of a concrete section under reconstruction, causing both main landing gear to collapse (the left main gear was torn off). The aircraft slid for another 250 metres before coming to rest. All 92 occupants evacuated safely and the aircraft was damaged beyond repair.
Probable cause:
The cause of the aviation accident with the RRJ 95B RA-89011 aircraft when landing at night with one deactivated thrust reverser was the transfer to the crew of incorrect information about the value of the friction coefficient, which led to the landing on an icy runway, the average normative friction coefficient which was less than 0.3, which did not allow landing in accordance with current regulations. This led to a significant increase in landing distance, rolling the aircraft out of the runway and collision with the junction of the reconstructed section of the runway with a height of about 0.4 m, which led to the destruction of the main landing gear supports and damage to the engines with fuel leakage without causing a fire.
The contributing factors were the following:
- Absence of a connecting ramp (which was not envisaged by the reconstruction project) between the current and the part of the runway being reconstructed;
- inefficiency of the SMS of Yakutsk Airport JSC in terms of identification and control of risks associated with the possibility of ice formation at the runway, and insufficient control over the implementation of the SMS by aviation authorities;
- erroneous determination of the Xc value at the last measurement;
- inefficiency of ice removal procedure during runway cleaning due to lack of chemical reagents for ice removal and/or thermal machines at the airfield;
- lack of information from the RRJ-95LR-100 RA 89038 aircraft crew about actual rolling out of the runway, which was an aviation incident and was subject to investigation;
- failure by airport and ATC officials to take appropriate action after receiving the RRJ-95LR-100 RA-89038 low friction report from the aircraft crew.
Final Report:

Crash of an Antonov AN-32 in Khartoum

Date & Time: Oct 3, 2018
Type of aircraft:
Operator:
Flight Type:
Survivors:
Yes
Country:
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The airplane was engaged in an exercise with a second Sudanese Air Force Antonov AN-32. After touchdown on runway 18, the crew started the braking procedure when the airplane was struck by the AN-32 from behind. After collision, both airplanes went out of control and came to rest on the runway edge. There were no casualties while both aircraft were destroyed. It appears that the AN-32 landed shortly after the AN-26 and was unable to stop in a timely manner.

Crash of an Antonov AN-26 in Khartoum

Date & Time: Oct 3, 2018
Type of aircraft:
Operator:
Registration:
7706
Flight Type:
Survivors:
Yes
MSN:
104 04
YOM:
1980
Country:
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The airplane was engaged in an exercise with a second Sudanese Air Force Antonov AN-32. After touchdown on runway 18, the crew started the braking procedure when the airplane was struck by the AN-32 from behind. After collision, both airplanes went out of control and came to rest on the runway edge. There were no casualties while both aircraft were destroyed. It appears that the AN-32 landed shortly after the AN-26 and was unable to stop in a timely manner.

Crash of a Boeing 737-8BK off Weno Island: 1 killed

Date & Time: Sep 28, 2018 at 0924 LT
Type of aircraft:
Operator:
Registration:
P2-PXE
Survivors:
Yes
Schedule:
Kolonia – Chuuk – Port Moresby
MSN:
33024/1688
YOM:
2005
Flight number:
PX073
Region:
Crew on board:
12
Crew fatalities:
Pax on board:
35
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
19780
Captain / Total hours on type:
2276.00
Copilot / Total flying hours:
4618
Copilot / Total hours on type:
368
Aircraft flight hours:
37160
Aircraft flight cycles:
14788
Circumstances:
On 28 September 2018, at 23:24:19 UTC2 (09:24 local time), a Boeing 737-8BK aircraft, registered P2-PXE (PXE), operated by Air Niugini Limited, was on a scheduled passenger flight number PX073, from Pohnpei to Chuuk, in the Federated States of Micronesia (FSM) when, during its final approach, the aircraft impacted the water of the Chuuk Lagoon, about 1,500 ft (460 m) short of the runway 04 threshold. The aircraft deflected across the water several times before it settled in the water and turned clockwise through 210 deg and drifted 460 ft (140 m) south east of the runway 04 extended centreline, with the nose of the aircraft pointing about 265°. The pilot in command (PIC) was the pilot flying, and the copilot was the support/monitoring pilot. An Aircraft Maintenance Engineer occupied the cockpit jump seat. The engineer videoed the final approach on his iPhone, which predominantly showed the cockpit instruments. Local boaters rescued 28 passengers and two cabin crew from the left over-wing exits. Two cabin crew, the two pilots and the engineer were rescued by local boaters from the forward door 1L. One life raft was launched from the left aft over-wing exit by cabin crew CC5 with the assistance of a passenger. The US Navy divers rescued six passengers and four cabin crew and the Load Master from the right aft over-wing exit. All injured passengers were evacuated from the left over-wing exits. One passenger was fatally injured, and local divers located his body in the aircraft three days after the accident. The Government of the Federated States of Micronesia commenced the investigation and on 14th February 2019 delegated the whole of the investigation to the PNG Accident Investigation Commission. The investigation determined that the flight crew’s level of compliance with Air Niugini Standard Operating Procedures Manual (SOPM) was not at a standard that would promote safe aircraft operations. The PIC intended to conduct an RNAV GPS approach to runway 04 at Chuuk International Airport and briefed the copilot accordingly. The descent and approach were initially conducted in Visual Meteorological Conditions (VMC), but from 546 ft (600 ft)4 the aircraft was flown in Instrument Meteorological Conditions (IMC). The flight crew did not adhere to Air Niugini SOPM and the approach and pre-landing checklists. The RNAV (GPS) Rwy 04 Approach chart procedure was not adequately briefed. The RNAV approach specified a flight path descent angle guide of 3º. The aircraft was flown at a high rate of descent and a steep variable flight path angle averaging 4.5º during the approach, with lateral over-controlling; the approach was unstabilised. The Flight Data Recorder (FDR) recorded a total of 17 Enhanced Ground Proximity Warning System (EGPWS) alerts, specifically eight “Sink Rate” and nine “Glideslope”. The recorded information from the Cockpit Voice Recorder (CVR) showed that a total of 14 EGPWS aural alerts sounded after passing the Minimum Descent Altitude (MDA), between 307 ft (364 ft) and the impact point. A “100 ft” advisory was annunciated, in accordance with design standards, overriding one of the “Glideslope” aural alert. The other aural alerts were seven “Glideslope” and six “Sink Rate”. The investigation observed that the flight crew disregarded the alerts, and did not acknowledge the “minimums” and 100 ft alerts; a symptom of fixation and channelised attention. The crew were fixated on cues associated with the landing and control inputs due to the extension of 40° flap. Both pilots were not situationally aware and did not recognise the developing significant unsafe condition during the approach after passing the Missed Approach Point (MAP) when the aircraft entered a storm cell and heavy rain. The weather radar on the PIC’s Navigation Display showed a large red area indicating a storm cell immediately after the MAP, between the MAP and the runway. The copilot as the support/monitoring pilot was ineffective and was oblivious to the rapidly unfolding unsafe situation. He did not recognise the significant unsafe condition and therefore did not realise the need to challenge the PIC and take control of the aircraft, as required by the Air Niugini SOPM. The Air Niugini SOPM instructs a non-flying pilot to take control of the aircraft from the flying pilot, and restore a safe flight condition, when an unsafe condition continues to be uncorrected. The records showed that the copilot had been checked in the Simulator for EGPWS Alert (Terrain) however there was no evidence of simulator check sessions covering the vital actions and responses required to retrieve a perceived or real situation that might compromise the safe operation of the aircraft. Specifically sustained unstabilised approach below 1,000 ft amsl in IMC. The PIC did not conduct the missed approach at the MAP despite the criteria required for visually continuing the approach not being met, including visually acquiring the runway or the PAPI. The PIC did not conduct a go around after passing the MAP and subsequently the MDA although:
• The aircraft had entered IMC;
• the approach was unstable;
• the glideslope indicator on the Primary Flight Display (PFD) was showing a rapid glideslope deviation from a half-dot low to 2-dots high within 9 seconds after passing the MDA;
• the rate of descent high (more than 1,000 ft/min) and increasing;
• there were EGPWS Sink Rate and Glideslope aural alerts; and
• the EGPWS visual PULL UP warning message was displayed on the PFD.
The report highlights that deviations from recommended practice and SOPs are a potential hazard, particularly during the approach and landing phase of flight, and increase the risk of approach and landing accidents. It also highlights that crew coordination is less than effective if crew members do not work together as an integrated team. Support crew members have a duty and responsibility to ensure that the safety of a flight is not compromised by non-compliance with SOPs, standard phraseology and recommended practices. The investigation found that the Civil Aviation Safety Authority of PNG (CASA PNG) policy and procedures of accepting manuals rather than approving manuals, while in accordance with the Civil Aviation Rules requirements, placed a burden of responsibility on CASA PNG as the State Regulator to ensure accuracy and that safety standards are met. In accepting the Air Niugini manuals, CASA PNG did not meet the high standard of evidence-based assessment required for safety assurance, resulting in numerous deficiencies and errors in the Air Niugini Operational, Technical, and Safety manuals as noted in this report and the associated Safety Recommendations. The report includes a number of recommendations made by the AIC, with the intention of enhancing the safety of flight (See Part 4 of this report). It is important to note that none of the safety deficiencies brought to the attention of Air Niugini caused the accident. However, in accordance with Annex 13 Standards, identified safety deficiencies and concerns must be raised with the persons or organisations best placed to take safety action. Unless safety action is taken to address the identified safety deficiencies, death or injury might result in a future accident. The AIC notes that Air Niugini Limited took prompt action to address all safety deficiencies identified by the AIC in the 12 Safety Recommendations issued to Air Niugini, in an average time of 23 days. The quickest safety action being taken by Air Niugini was in 6 days. The AIC has closed all 12 Safety Recommendations issued to Air Niugini Limited. One safety concern prompting an AIC Safety Recommendation was issued to Honeywell Aerospace and the US FAA. The safety deficiency/concern that prompted this Safety Recommendation may have been a contributing factor in this accident. The PNG AIC is in continued discussion with the US NTSB, Honeywell, Boeing and US FAA. This recommendation is the subject of ongoing research and the AIC Recommendation will remain ACTIVE pending the results of that research.
Probable cause:
The flight crew did not comply with Air Niugini Standard Operating Procedures Manual (SOPM) and the approach and pre-landing checklists. The RNAV (GPS) Rwy 04 Approach chart procedure was not adequately briefed. The aircraft’s flight path became unstable with lateral over-controlling commencing shortly after autopilot disconnect at 625 ft (677 ft). From 546 ft (600 ft) the aircraft was flown in Instrument Meteorological Conditions (IMC) and the rate of descent significantly exceeded 1,000 feet/min in Instrument Meteorological Conditions (IMC) from 420 ft (477 ft). The flight crew heard, but disregarded, 13 EGPWS aural alerts (Glideslope and Sink Rate), and flew a 4.5º average flight path (glideslope). The pilots lost situational awareness and their attention was channelised or fixated on completing the landing. The PIC did not execute the missed approach at the MAP despite: PAPI showing 3 whites just before entering IMC; the unstabilised approach; the glideslope indicator on the PFD showing a rapid glideslope deviation from half-dot low to 2-dots high within 9 seconds after passing the MDA; the excessive rate of descent; the EGPWS aural alerts: and the EGPWS visual PULL UP warning on the PFD. The copilot (support/monitoring pilot) was ineffective and was oblivious to the rapidly unfolding unsafe situation. It is likely that a continuous “WHOOP WHOOP PULL UP”70 hard aural warning, simultaneously with the visual display of PULL UP on the PFD (desirably a flashing visual display PULL UP on the PFD), could have been effective in alerting the crew of the imminent danger, prompting a pull up and execution of a missed approach, that may have prevented the accident.
Final Report:

Crash of a Dassault Falcon 50 in Greenville: 2 killed

Date & Time: Sep 27, 2018 at 1346 LT
Type of aircraft:
Registration:
N114TD
Survivors:
Yes
Schedule:
St Petersburg - Greenville
MSN:
17
YOM:
1980
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
11650
Copilot / Total flying hours:
5500
Aircraft flight hours:
14002
Circumstances:
The flight crew was operating the business jet on an on-demand air taxi flight with passengers onboard. During landing at the destination airport, the cockpit voice recorder (CVR) recorded the sound of the airplane touching down followed by the pilot's and copilot's comments that the brakes were not operating. Air traffic controllers reported, and airport surveillance video confirmed, that the airplane touched down "normally" and the airplane's thrust reverser deployed but that the airplane continued down the runway without decelerating before overrunning the runway and impacting terrain. Postaccident examination of the airplane's brake system revealed discrepancies of the antiskid system that included a broken solder joint on the left-side inboard transducer and a reversal of the wiring on the right-side outboard transducer. It is likely that these discrepancies resulted in the normal braking system's failure to function during the landing. Before the accident flight, the airplane had been in long-term storage for several years and was in the process of undergoing maintenance to bring the airplane back to a serviceable condition, which in-part required the completion of several inspections, an overhaul of the landing gear, and the resolution of over 100 other unresolved discrepancies. The accident flight and four previous flights were all made with only a portion of this required maintenance having been completed and properly documented in the airplane's maintenance logs. A pilot, who had flown the airplane on four previous flights along with the accident pilot (who was acting as second-in-command during them), identified during those flights that the airplane's normal braking system was not operating when the airplane was traveling faster than 20 knots. He remedied the situation by configuring the airplane to use the emergency, rather than normal, braking system. That pilot reported this discrepancy to the operator's director of maintenance, and it is likely that maintenance personnel from the company subsequently added an "INOP" placard near the switch on the date of the accident. The label on the placard referenced the antiskid system, and the airplane's flight manual described that with the normal brake (or antiskid) system inoperative, the brake selector switch must be positioned to use the emergency braking system. Following the accident, the switch was found positioned with the normal braking system activated, and it is likely that the accident flight crew attempted to utilize the malfunctioning normal braking system during the landing. Additionally, the flight crew failed to properly recognize the failure and configure the airplane to utilize the emergency braking system, or utilize the parking brake, as described in the airplane's flight manual, in order to stop the airplane within the available runway.
Probable cause:
The operator's decision to allow a flight in an airplane with known, unresolved maintenance discrepancies, and the flight crew's failure to properly configure the airplane in a way that would have allowed the emergency or parking brake systems to stop the airplane during landing.
Final Report: