Crash of a Tupolev TU-154B-2 in New Delhi

Date & Time: Jan 9, 1993 at 0408 LT
Type of aircraft:
Operator:
Registration:
85533
Survivors:
Yes
Schedule:
Hyderabad - New Delhi
MSN:
82A533
YOM:
1982
Flight number:
IC840
Country:
Region:
Crew on board:
13
Crew fatalities:
Pax on board:
152
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
10245
Circumstances:
On 9th January, 1993 TU-154 aircraft No. 85533 wet leased by Indian Airlines from Uzbekistan Airways was operating flight IC-840 from Hyderabad to Delhi. The aircraft was being flown by Uzbeki operating crew and there were 165 persons on board including the crew. The aircraft touched down slightly outside the right edge of the runway, collided with some fixed installations on the ground, got airborne once again and finally touched down on kutcha ground on the right side of the runway. At this stage the right wing and the tail of the aircraft broke away and it came to rest in an inverted position. During the process, the aircraft caught fire and was destroyed. Most occupants of the aircraft escaped unhurt. Six persons suffered either limb fracture or other serious injuries while 45 persons suffered injuries of a minor nature.
Probable cause:
The probable cause of accident has been attributed to :
- The failure of the Pilot-in-Command to divert to Ahmedabad when he was informed that the RVR on runway 28 was below the minima applicable to his flight.
- The switching on of landing lights, on the instruction of the second Captain, at a height of only about ten metres, resulting in the loss of all visual references due to the blinding effect of
light reflections from fog.
- The failure of captain to carry out a missed approach when visual reference to the runway was lost.
Final Report:

Crash of an Avro 748-234-2A in Surabaya: 16 killed

Date & Time: Jan 9, 1993
Type of aircraft:
Operator:
Registration:
PK-IHE
Survivors:
Yes
Schedule:
Banjarmasin - Surabaya
MSN:
1620
YOM:
1968
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
39
Pax fatalities:
Other fatalities:
Total fatalities:
16
Circumstances:
On short final to Surabaya-Juanda Airport, the right engine failed. The aircraft banked to the right and crashed in a swampy area located 800 metres short of runway. 16 occupants were killed while 28 others were injured.
Probable cause:
Failure of the right engine on short final for undetermined reasons. The relative low approach speed of the aircraft contributed to the stall/right bank.

Crash of a Learjet 35 in Hermosillo: 9 killed

Date & Time: Jan 8, 1993 at 0846 LT
Type of aircraft:
Registration:
XA-LAN
Survivors:
No
Site:
Schedule:
Mexico City - Hermosillo
MSN:
35-267
YOM:
1979
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
9
Captain / Total flying hours:
15339
Copilot / Total flying hours:
1780
Aircraft flight hours:
6771
Circumstances:
Following an uneventful flight from Mexico City, the crew was cleared for an approach to Hermosillo-General Ignacio Pesqueira Garcia Airport runway 23. During the descent, the crew was alerted by ATC about poor weather conditions and limited visibility. On final, at an altitude of 1,800 feet, the aircraft struck the slope of Mt El Bachoco located 10,4 km short of runway 23. The aircraft was destroyed and all nine occupants were killed.
Probable cause:
Controlled flight into terrain after the crew failed to maintain the minimum prescribed altitude of 2,800 feet on approach. The lack of visibility due to poor weather conditions was considered as a contributing factor.
Final Report:

Crash of a De Havilland DHC-8-311 in Paris: 4 killed

Date & Time: Jan 6, 1993 at 1920 LT
Operator:
Registration:
D-BEAT
Survivors:
Yes
Schedule:
Bremen - Paris
MSN:
210
YOM:
1990
Flight number:
LH5634
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
19
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
11924
Captain / Total hours on type:
2003.00
Copilot / Total flying hours:
500
Copilot / Total hours on type:
293
Aircraft flight hours:
5973
Circumstances:
While approaching Paris-Roissy-CDG Airport by night, at a distance of 13 km from runway 27 threshold, the crew was instructed by ATC to modify the approach trajectory and to descent to runway 28. This late request was necessary because runway 27 was just closed to traffic after a Korean Air B747 contacted the runway surface with its engine n°1. While completing a left turn, the airplane lost height and crashed in a field located 1,800 metres short of runway. Four passengers were killed while 19 other occupants were injured. The aircraft was destroyed. At the time of the accident, the visibility was reduced between 700 and 1,400 metres due to light fog and rain. The copilot was in command and it is believed the crew was disturbed by the late runway change. While on descent heading 265°, 100 seconds before FDR stopped recording, at an altitude of 1,600 feet and a speed of 170 knots, both engine torques were at 20%. Twenty seconds later, both engines torque dropped to zero and the automatic pilot system was deactivated. At this time, the flaps were retracted. The sink rate increased then the aircraft entered a nose-up attitude with its speed decreasing. The aircraft struck the ground at a speed of 110 knots and crashed.
Final Report:

Crash of a Mitsubishi MU-2B-35 Marquise near Nome

Date & Time: Jan 5, 1993 at 2021 LT
Type of aircraft:
Operator:
Registration:
N900YH
Flight Type:
Survivors:
Yes
Schedule:
Bethel - Nome
MSN:
584
YOM:
1973
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
11150
Captain / Total hours on type:
512.00
Aircraft flight hours:
6725
Circumstances:
After making a refueling stop, the pilot took off at night and was cruising at FL200. After about 30 minutes of flight, the right engine fuel filter bypass warning light illuminated. About 2 minutes later, the same warning light for the left engine illuminated. Soon thereafter the right engine, then the left engine, lost power. The pilot made a forced landing on a moving ice pack in the Bering sea, which resulted in substantial damage. Ice was found in the engine and main fuel screens. Significant amounts of water and/or ice were found in 3 tanks, which had been refueled before takeoff. A higher than normal amount of water was also found in the fuel sample taken from the nozzle of the refueling tanker. The flight manual required that an approved ice inhibitor be added to the fuel, if not premixed. Fuel at the refueling stop was not premixed and the pilot had no icing inhibitor (prist) with him on this flight. He did not drain fuel from the tanks during preflight, since the temperature was so cold he feared the drain might freeze open.
Probable cause:
Fuel starvation due to improper refueling procedures by the fbo personnel, inadequate preflight by the pilot, and resultant ice in the fuel, which blocked fuel flow to the engines. A factor was the lack of suitable terrain for a forced landing.
Final Report:

Crash of a Saab 340A in Hibbing

Date & Time: Jan 2, 1993 at 1942 LT
Type of aircraft:
Registration:
N342PX
Survivors:
Yes
Schedule:
Minneapolis - Hibbing
MSN:
147
YOM:
1989
Crew on board:
3
Crew fatalities:
Pax on board:
28
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6500
Captain / Total hours on type:
2800.00
Circumstances:
During the approach, the 1st officer (FO) asked the captain if he wanted to '...pop the boots?' to remove ice off the wings. The capt responded '...it's going to the hangar. I'll run'em on the ground...' The FO retarded power over the threshold and the sink rate increased; the capt observed 900 fpm. The FO applied additional back pressure on the yoke, but it was inadequate to arrest the high sink rate. Additional back pressure was applied, and the stall horn sounded followed shortly thereafter by the captain stating 'I got it.' During the hard landing the right main landing gear broke, the fuel tank ruptured, and the right wing rear spar bent upward. Aprx 18 hrs after the accident, 3/16 inch of rime mixed with clear ice was observed on the leading edges of the wing, horizontal stab, and vertical stab. The ice had finger-like protrusions positioned vertically to the wing surfaces. The company's line ops manual does not discuss flight characteristics or landing techniques specific to wing ice. Neither pilot had received company's current crm training.
Probable cause:
The first officer's failure to maintain a proper descent rate during the landing, and the captain's inadequate supervision by not taking timely action to ensure a safe landing. Factors which contributed to the accident were: the company's failure to provide adequate training on the airplane's flight characteristics and/or handling techniques under conditions of wing ice contamination, the company's failure to assure that both pilots had received the current crew resource management (crm) training, and the existing weather conditions which resulted in an accumulation of ice on the airplane's wing.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in South Bimini

Date & Time: Jan 2, 1993 at 0945 LT
Registration:
N4107V
Flight Type:
Survivors:
Yes
Schedule:
Fort Lauderdale - South Bimini
MSN:
31-8253010
YOM:
1982
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Crashed in unknown circumstances upon landing at South Bimini Airport. The pilot, sole on board, was uninjured.

Crash of a Rockwell Gulfstream 690C Jetprop 840 in Golden: 1 killed

Date & Time: Dec 22, 1992 at 2022 LT
Operator:
Registration:
N81TR
Flight Type:
Survivors:
No
Site:
Schedule:
Rifle - Denver
MSN:
690-11690
YOM:
1981
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
5400
Captain / Total hours on type:
910.00
Aircraft flight hours:
7768
Circumstances:
While in a descent for arrival at the destination airport, the aircraft sustained structural failure with the right outer wing, horizontal stabilizer, and vertical stabilizer separating from the aircraft. The aircraft impacted approximately 10 miles from the planned destination. According to radar data and other research, the descent was conducted at vne and known severe turbulence was present in the area at the time of the accident.
Probable cause:
The pilot flying the aircraft beyond the design maneuvering speed and exceeding the design stress limits. A factor was: clear air turbulence.
Final Report:

Crash of a Boeing 727-2L5 in Tripoli: 157 killed

Date & Time: Dec 22, 1992 at 0807 LT
Type of aircraft:
Operator:
Registration:
5A-DIA
Survivors:
No
Schedule:
Benghazi - Tripoli
MSN:
21050
YOM:
1975
Flight number:
LN1103
Country:
Region:
Crew on board:
10
Crew fatalities:
Pax on board:
147
Pax fatalities:
Other fatalities:
Total fatalities:
157
Circumstances:
Following an uneventful flight from Benghazi, the crew was cleared to start the descent to Tripoli Airport. Due to military traffic, the crew was instructed to hold over the Papa Echo beacon located 4,1 DME from runway 27 threshold. At an altitude of 3,000 feet, the Boeing 727 collided with a Libyan Air Force MiG-23 that just took off from Tripoli Airport. The fighter struck the tail of the Boeing that entered a dive and crashed 9 km from the airport after the tail separated. All 157 occupants were killed while both pilots on board the fighter ejected safely.
Final Report:

Crash of a Douglas DC-10-30CF in Faro: 56 killed

Date & Time: Dec 21, 1992 at 0833 LT
Type of aircraft:
Operator:
Registration:
PH-MBN
Survivors:
Yes
Schedule:
Amsterdam - Faro
MSN:
46924
YOM:
1975
Flight number:
MP495
Location:
Country:
Region:
Crew on board:
13
Crew fatalities:
Pax on board:
327
Pax fatalities:
Other fatalities:
Total fatalities:
56
Captain / Total flying hours:
14441
Captain / Total hours on type:
1497.00
Copilot / Total flying hours:
2288
Copilot / Total hours on type:
1787
Aircraft flight hours:
61543
Aircraft flight cycles:
14615
Circumstances:
At 0552LT, the aircraft departed Amsterdam-Schiphol Airport on a charter flight to Faro. The flight had been delayed for 40 minutes due to n°2 engine reverser problems. After a flight of 2 hours and 17 minutes, the crew was cleared to descend to FL070. Shortly afterwards Faro Approach Control provided the crew with the following weather: wind 15°/18 knots; 2,500 metres visibility, thunderstorms with 3/8 clouds at 500 feet, 7/8 clouds at 2,300 feet and 1/8 cumulonimbus at 2,500 feet, OAT 16° C. Clearance to descend to 1,220 metres was given at 0820LT, followed by a clearance to 915 metres and 650 metres 4, respectively 6 minutes later. At 0829LT the crew were informed that the runway was flooded. At an altitude of 303 metres and at a speed of 140 knots, the aircraft became unstable and at 177 metres the first officer switched the autopilot from CMD (command mode) to CWS (control-wheel steering). One minute later it was switched from CWS to manual and the airspeed began falling below approach reference speed. About 3-4 seconds short of touchdown, elevator was pulled to pitch up and engine power was increased. When the n°3 and 5 spoilers extended, the aircraft banked to the right to an angle of 25°. The right main gear struck the the runway surface with a rate of descent of 900 feet per minute and at a speed of 126 knots. With a nose up attitude of 8,79° and a roll angle of 5,62°, the aircraft touched down with a positive acceleration of 1,95 g. Upon impact, the right wing separated while the aircraft slid down the runway and came to rest 1,100 metres from the runway 11 threshold and 100 metres to the right of the centreline, bursting into flames. Two crew members and 54 passengers were killed while 284 other occupants were evacuated, among them 106 were seriously injured.
Probable cause:
The high rate of descent in the final phase of the approach and the landing made on the right landing gear, which exceeded the structural limitations of the aircraft.; The crosswind, which exceeded the aircrafts limits and which occurred in the final phase of the approach and during landing. The combination of both factors determined stresses which exceeded the structural limitations of the aircraft. Contributing factors were: The instability of the approach; the premature power reduction, and the sustaining of this condition, probably due to crew action; the incorrect wind information delivered by Approach Control; the absence of an approach light system; the incorrect evaluation by the crew of the runway conditions; CWS mode being switched off at approx. 80ft RA, causing the aircraft to be in manual control in a critical phase of the landing; the delayed action of the crew in increasing power; the degradation of the lift coefficient due to heavy showers. The Netherlands Aviation Safety Board commented that the probable cause should read: "a sudden and unexpected wind variation in direction and speed (windshear) in the final stage of the approach. Subsequently a high rate of descent and an extreme lateral displacement developed, causing a hard landing on the right-hand main gear, which in combination with a considerable crab angle exceeded the aircraft structural limitations. Contributing factors: From the forecast and the prevailing weather the crew of MP495 did not expect the existence of windshear phenomena.; The premature large power reduction and sustained flight idle thrust, most probable due to crew action.; CWS mode being disengaged at approx. 80ft RA, causing the aircraft to be in manual control at a critical stage in the landing phase.
Final Report: