Crash of a Cessna 425 Conquest in London

Date & Time: Jan 18, 1994 at 1750 LT
Type of aircraft:
Registration:
N303MC
Flight Type:
Survivors:
Yes
Schedule:
Charleston - Dallas
MSN:
425-0034
YOM:
1980
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2758
Captain / Total hours on type:
510.00
Aircraft flight hours:
2589
Circumstances:
The pilot stated that the airplane was cruising at an altitude of 18,000 feet 30 minutes after refueling when the left engine lost power. He stated that he was in radio contact with Indianapolis ARTCC so he advised them of the situation and requested a lower altitude. The center cleared the flight to 10,000 feet msl. The pilot stated that his attempt to restart the engine was unsuccessful. Shortly thereafter the pilot reported that the right engine lost power. According to the controller at the center, the pilot was nine miles from the nearest airport and he provided the pilot with radar vectors to the nearest airport, and the weather conditions. The airplane touched down in a wooded area. The faa examined the airplane at the accident site. The engines were removed to Pratt & Whitney for further examination. The examination of the engine and engine accessories did not disclose any pre-existing defects. Fuel samples were removed and tested at the laboratory at Pratt & Whitney. The tests revealed evidence of contaminants.
Probable cause:
Loss of engine power due to fuel contamination.
Final Report:

Crash of a Learjet 24D in Kinshasa: 2 killed

Date & Time: Jan 18, 1994
Type of aircraft:
Operator:
Registration:
9Q-CBC
Flight Type:
Survivors:
No
Schedule:
Cotonou - Kinshasa
MSN:
24-248
YOM:
1972
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The crew was cleared for a night visual approach to Kinshasa-N'Djili Airport. Weather conditions were good with a visibility over 10 km. On approach, ATC asked the crew to turn on the approach lights. Shortly later, the aircraft struck the ground and crashed 20 km short of runway 24 threshold. Both pilots were killed.

Crash of a Rockwell Grand Commander 690 off Sydney: 1 killed

Date & Time: Jan 14, 1994 at 0114 LT
Registration:
VH-BSS
Flight Type:
Survivors:
No
Schedule:
Canberra - Sydney
MSN:
690-11044
YOM:
1972
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1800
Captain / Total hours on type:
50.00
Aircraft flight hours:
7975
Circumstances:
On 14 January 1994 at 0114, Aero Commander 690 aircraft VH-BSS struck the sea while being radar vectored to intercept the Instrument Landing System approach to runway 34 at Sydney (Kingsford-Smith) Airport, NSW. The last recorded position of the aircraft was about 10 miles to the south-east of the airport. At the time of the accident the aircraft was being operated as a cargo charter flight from Canberra to Sydney in accordance with the Instrument Flight Rules. The body of the pilot who was the sole occupant of the aircraft was never recovered. Although wreckage identified as part of the aircraft was located on the seabed shortly after the accident, salvage action was not initially undertaken. This decision was taken after consideration of the known circumstances of the occurrence and of the costs of salvage versus the potential safety benefit that might be gained from examination of the wreckage. About 18 months after the accident, the wing and tail sections of the aircraft were recovered from the sea by fishermen. As a result, a detailed examination of that wreckage was carried out to assess the validity of the Bureau’s original analysis that the airworthiness of the aircraft was unlikely to have been a factor in this accident. No evidence was found of any defect which may have affected the normal operation of the aircraft. The aircraft descended below the altitude it had been cleared to by air traffic control. From the evidence available it was determined that the circumstances of this accident were consistent with controlled flight into the sea.
Probable cause:
Findings
1. The pilot held a valid pilot licence, endorsed for Aero Commander 690 aircraft.
2. The pilot held a valid multi-engine command instrument rating.
3. There was no evidence found to indicate that the performance of the pilot was adversely affected by any physiological or psychological condition.
4. The aircraft was airworthy for the intended flight, despite the existence of minor anomalies in maintenance and serviceability of aircraft systems.
5. The aircraft carried fuel sufficient for the flight.
6. The weight and balance of the aircraft were estimated to have been within the normal limits.
7. Recorded radio communications relevant to the operation of the aircraft were normal.
8. Relevant ground-based aids to navigation were serviceable.
9. At the time of impact the aircraft was capable of normal flight.
10. The aircraft was fitted with an altitude alerting system.
11. The aircraft was not fitted with a ground proximity warning system.
12. The aircraft was equipped with a transponder which provided aircraft altitude information to be displayed on Air Traffic Control radar equipment.
3.2 Significant factors
1. The pilot was relatively inexperienced in single-pilot Instrument Flight Rules operations on the type of aircraft being flown.
2. The aircraft was being descended over the sea in dark-night conditions.
3. The workload of the pilot was significantly increased by his adoption of a steep descent profile at high speed, during a phase of flight which required multiple tasks to be completed in a limited time prior to landing. Radio communications with another company aircraft during that critical phase of flight added to that workload.
4. The pilot probably lost awareness of the vertical position of the aircraft as a result of distraction by other tasks.
5. The aircraft was inadvertently descended below the altitude authorized by Air Traffic Control.
6. The secondary surveillance radar system in operation at the time provided an aircraft altitude readout which was only updated on every sixth sweep of the radar display.
7. The approach controller did not notice a gross change of aircraft altitude shortly after a normal radio communication with the pilot.
Final Report:

Crash of a Piper PA-31-310 Navajo C in Lourdes-de-Blanc-Sablon: 2 killed

Date & Time: Jan 11, 1994 at 1854 LT
Type of aircraft:
Operator:
Registration:
C-GDOU
Flight Type:
Survivors:
No
Schedule:
Saint Anthony - Lourdes-de-Blanc-Sablon
MSN:
31-7612033
YOM:
1976
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
8000
Captain / Total hours on type:
1550.00
Copilot / Total flying hours:
1079
Copilot / Total hours on type:
650
Aircraft flight hours:
11050
Circumstances:
On 11 January 1994, the crew were on a chartered round-robin flight on a PA-31 Navajo, between Lourdes-de-Blanc-Sablon airport, Quebec, and St. Anthony, Newfoundland, in accordance with visual flight rules (VFR) . During the return flight, at night, the crew advised the St. Anthony flight service station (FSS) that they departed at 1813 Newfoundland standard time (NST). At 1846 NST, the crew transmitted that they were flying at 2,500 feet and that they were 32 nautical miles (nm) and 13 minutes southeast of Blanc-Sablon. Seven minutes later, the crew called the Sept-Iles FSS through the Blanc-Sablon repeater. They requested airport information and reported being 16 nm and six minutes from the airport. After receiving information on the winds and the altimeter setting, the crew reported that they would use runway 05 and would call back on final. No further transmissions were received from the crew. Fishermen found the wreckage seven months later.
Probable cause:
The cause of the occurrence could not be determined; however, it is probable that the pilots did not monitor the altimeter properly and allowed the aircraft to descend until it struck the surface of the ice.
Final Report:

Crash of a Beechcraft A100 King Air in Bacău

Date & Time: Jan 8, 1994 at 0937 LT
Type of aircraft:
Operator:
Registration:
OO-TLS
Survivors:
Yes
Schedule:
Oradea – Iaşi
MSN:
B-188
YOM:
1974
Location:
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The aircraft took off Oradea Airport at 0805LT with destination Iași Airport, having as alterne airport Bacău Airport. At 08.53 hrs, due to bad meteorological conditions on Iași Airport the crew requested to Bacău ACC permission for landing on Bacău Airport. Bacău ACC has granted permission and informed the crew about the meteorological conditions in that moment at Bacău Airport. The crew confirmed. During the aircraft was performing the approach procedure, the crew was instructed to contact the precision radar (PAR) and was informed that at that moment the visibility range was 800 metres. At the first approach PAR sent to the crew all the appropriate data for the radar assistance and in the final stage has asked the crew to perform a missed landing, go up to 900 metres and to contact Bacău TWR because the aircraft was away from the runway centerline (approx. 60 metres left). On Bacău TWR frequency the crew received the indication to perform a right turn to intercept the QDM 342 degrees at Bacău. It was also stated that the runway beacon is running. The crew was instructed, also, to contact PAR which assisted the aircraft, with the necessary corrections, during the approach procedure and landing until the crew reported the accident at 0930LT.
Probable cause:
Further the analysis of the flight recordings between the aircraft and the Romanian Air Traffic Services, statements and all other data contained by the investigation file the following conclusions have been reached:
- The meteorological conditions at Iași Airport were difficult and have not permitted the landing of the aircraft,
- The decision for landing on Bacău Airport was made by the crew,
- At the moment the meteorological conditions at Bacău Airport assured the minimum conditions for landing the aircraft,
- The air traffic control was performed by Bacău TWR and PAR, according to international regulations, providing permanent information regarding the aircraft during the final approach for landing.
We mention that after the first missed landing the crew maintained its decision to perform a second approach for landing, knowing the meteorological conditions on Bacău Airport.
Final Report:

Crash of a Bae 4101 Jetstream 41 in Columbus: 5 killed

Date & Time: Jan 7, 1994 at 2321 LT
Type of aircraft:
Operator:
Registration:
N304UE
Survivors:
Yes
Site:
Schedule:
Washington DC - Columbus
MSN:
41016
YOM:
1993
Flight number:
UA6291
Crew on board:
3
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
3660
Captain / Total hours on type:
192.00
Copilot / Total flying hours:
2430
Copilot / Total hours on type:
31
Aircraft flight hours:
1069
Aircraft flight cycles:
1000
Circumstances:
The airplane stalled and crashed 1.2 nautical miles east of runway 28L during an ILS approach. The captain initiated the approach at high speed & crossed the FAF at a high speed without first having the airplane properly configured for a stabilized approach. The airspeed was not monitored nor maintained by the flightcrew. The airline had no specified callouts for airspeed deviations during instrument approaches. The captain failed to apply full power & configure the airplane in a timely manner. Both pilots had low flight time and experience in in the airplane and in any EFIS-equipped airplane. Additionally, the captain had low time and experience as a captain. Inadequate consideration was given to the possible consequences of pairing a newly upgraded captain, on a new airplane, with a first officer who had no airline experience in air carrier operations, nor do current FAA regulations address this issue.
Probable cause:
The accident was the consequence of the following factors:
(1) An aerodynamic stall that occurred when the flightcrew allowed the airspeed to decay to stall speed following a very poorly planned and executed approach characterized by an absence
of procedural discipline;
(2) Improper pilot response to the stall warning, including failure to advance the power levers to maximum, and inappropriately raising the flaps;
(3) Flightcrew inexperience in 'glass cockpit' automatic aircraft, aircraft type, and in seat position, a situation exacerbated by a side letter of agreement between the company and its pilots;
(4) The company's failure to provide adequate crew resource management training, and the FAA's failure to require such training;
(5) The company's failure to provide adequate stabilized approach criteria, and the FAA's failure to require such criteria; and
(6) The unavailability of suitable training simulators that precluded fully effective flightcrew training.
Note: Items 1, 2, and 3 were approved by a Board vote of 4-0. Item 5 was adopted 3-1, with the dissenting Member believing the item was a contributory cause. The Board was divided 2-2 on items 4 and 6, two Members believing them causal and two Members, contributory.
Final Report:

Crash of a Beechcraft C90 King Air near Okeechobee: 10 killed

Date & Time: Jan 5, 1994 at 1829 LT
Type of aircraft:
Registration:
N230TW
Flight Type:
Survivors:
No
Schedule:
Kissimmee - Miami
MSN:
LJ-445
YOM:
1969
Crew on board:
1
Crew fatalities:
Pax on board:
9
Pax fatalities:
Other fatalities:
Total fatalities:
10
Captain / Total flying hours:
12000
Captain / Total hours on type:
130.00
Aircraft flight hours:
7072
Circumstances:
The pilot (or pilot-rated passenger) reported an 'indication' problem and said they intended to land at Okeechobee, but couldn't find the airport. They then reported engine trouble and said that they would try to land on a road. They circled the area and approached a dirt road with landing lights on. A car was proceeding on the road in the opposite direction. The plane began to climb, and it entered a left turn. It then rolled into a steep right bank, descended nose down, crashed and was consumed by fire. An exam revealed indications that both engines were operating at high rpm. A teardown revealed a right engine fuel control bearing had failed, which would have allowed improper movement of the fuel control drive shaft. The plane was last inspected on 11/25/92 and was 13 hours over a required 150 hour inspection. A service bulletin for maintenance of the fuel control bearings had not been complied with. The owner/pilot had not completed formal ground school instruction on the airplane systems and operation. The plane had 9 seats; 10 occupants were aboard.
Probable cause:
The pilot's improper remedial action concerning a right engine power anomaly, and his failure to maintain adequate airspeed during go-around from an aborted precautionary landing, which resulted in a loss of aircraft control and an uncontrolled descent. Factors related to the accident were: failure of the owner/operator/pilot to assure proper maintenance inspection of the aircraft, failure to comply with a service bulletin concerning the engine fuel controls, subsequent bearing failure in the right engine fuel control, and the pilot's lack of familiarity with this make and model of aircraft.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in Bathurst: 2 killed

Date & Time: Jan 4, 1994 at 1845 LT
Registration:
C-GNPG
Flight Type:
Survivors:
No
Schedule:
Moncton - Bathurst
MSN:
31-7752119
YOM:
1977
Flight number:
Empress204
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
3500
Captain / Total hours on type:
2600.00
Copilot / Total flying hours:
685
Copilot / Total hours on type:
350
Aircraft flight hours:
8162
Circumstances:
At 1805 Atlantic standard time (AST), C-GNPG, a Piper Navajo Chieftain operating as Empress 204, departed Moncton, New Brunswick, on a scheduled courier flight to Bathurst. The aircraft carried a two-pilot crew, and there was no cargo on board. The aircraft proceeded direct to Bathurst at 8,000 feet above sea level (asl) and at 1820 AST was cleared by Moncton Area Control Centre (ACC) for an approach at Bathurst. The co-pilot contacted the Bathurst UNICOM and advised the operator that the crew would be flying the non-directional beacon/distance measuring equipment (NDB/DME) runway 10 approach. During the non-precision instrument approach to runway 10, the aircraft struck trees .75 nautical miles (nm) inside the Bathurst beacon and 3.75 nm from the airport. The accident occurred at approximately 1845 AST, during the hours of darkness in instrument meteorological conditions, at an elevation of 450 feet asl. Both pilots were killed.
Probable cause:
The crew of Empress 204 allowed the aircraft to descend below the minimum descent altitude for the approach.
Final Report:

Crash of a Piper PA-46-310P Malibu in Destin: 2 killed

Date & Time: Jan 1, 1994 at 1420 LT
Registration:
N243KW
Flight Type:
Survivors:
No
Schedule:
Naples - Destin
MSN:
46-8508089
YOM:
1985
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
4000
Captain / Total hours on type:
1262.00
Aircraft flight hours:
1262
Circumstances:
The pilot was executing an ASR approach to runway 32 and 9 seconds after the approach controller advised the pilot that the flight was over the missed approach point, the pilot advised the controller that the airport was in sight and he would be circling to land. The controller acknowledged this and witnesses observed the airplane flying northwesterly west of runway 32 about 150-200 feet above ground level. They then observed the airplane enter a left bank between 60-80 degrees and the airplane pitched nose down and collided with trees then a fence and the ground. There was a small post crash fire which was extinguished by the fire department. Examination of the airframe revealed no evidence of preimpact failure or malfunction of the flight controls. The engine was removed and placed on a test bench and after replacement of several components which were impact damaged, the engine started and operated normally. The passenger was seated in the furthest aft right seat and the lap belt attach point on the right side of this seat failed due to overload.
Probable cause:
Airspeed not maintained, inadvertent stall/mush, and altitude inadequate for recovery from the inflight loss of control by the pilot-in-command while circling for landing.
Final Report:

Crash of an Antonov AN-26 in Playa Baracoa

Date & Time: Dec 31, 1993
Type of aircraft:
Operator:
Registration:
CU-T1240
Flight Type:
Survivors:
Yes
Schedule:
Playa Baracoa - Playa Baracoa
MSN:
112 10
YOM:
1981
Country:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was performing a brake test when control was lost. The aircraft veered off runway and came to rest. There were no injuries but the aircraft was damaged beyond repair. The exact date of the mishap remains unknown, somewhere in 1993.