Crash of a Learjet 35A in Marigot

Date & Time: Aug 11, 2007 at 1635 LT
Type of aircraft:
Operator:
Registration:
N500ND
Survivors:
Yes
Schedule:
Saint John's - Marigot
MSN:
35A-351
YOM:
1980
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On August 11, 2007, at 1635 Atlantic standard time, a Gates Learjet 35A, N500ND, registered to World Jet of Delaware Inc, and operated by World Jet II as a 14 CFR 135 on-demand on-scheduled international passenger air taxi flight, went off the end of runway 09 at Melville Hall, Dominica, on landing roll out. Visual meteorological conditions prevailed and an instrument flight rules flight plan was filed. The airplane received substantial damage. The airline transport rated pilot in command (PIC), first officer (FO), and four passengers reported no injuries. The flight originated from Saint John's Antigua Island on August 11, 2007, at 1600. The PIC stated the first officer was flying the airplane and the tower cleared them to enter a left downwind. On touchdown the FO requested spoilers, and noticed poor braking. The PIC pumped the brakes with no response. The drag chute was deployed but was not effective. The PIC stated he took over the flight controls and applied maximum braking. The airplane continued to roll off the end of the runway, down an embankment, through a fence, and came to a stop on a road.

Crash of a Piper PA-46-350P Malibu Mirage in Sitka: 4 killed

Date & Time: Aug 6, 2007 at 1255 LT
Registration:
N35CX
Flight Type:
Survivors:
No
Schedule:
Victoria - Sitka
MSN:
46-36127
YOM:
1997
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
1800
Aircraft flight hours:
2042
Circumstances:
The private, instrument-rated pilot, was on an IFR cross-country flight, and had been cleared for a GPS approach. He reported that he was 5 minutes from landing, and said he was circling to the left, to land the opposite direction from the published approach. The traffic pattern for the approach runway was right traffic. Instrument meteorological conditions prevailed, and the weather conditions included a visibility of 3 statute miles in light rain and mist; few clouds at 400 feet, 1,000 feet overcast; temperature, 55 degrees F; dew point, 55 degrees F. The minimum descent altitude, either for a lateral navigation approach, or a circling approach, was 580 feet, and required a visibility of 1 mile. The missed approach procedure was a right climbing turn. A circling approach north of the runway was not approved. Witnesses reported that the weather included low clouds and reduced visibility due to fog and drizzle. The airplane was heard, but not seen, circling several times over the city, which was north of the runway. Witnesses saw the airplane descending in a wings level, 30-45 degree nose down attitude from the base of clouds, pitch up slightly, and then collide with several trees and an unoccupied house. A postcrash fire consumed the residence, and destroyed the airplane. A review of FAA radar data indicated that as the accident airplane flew toward the airport, its altitude slowly decreased and its flight track appeared to remain to the left side (north) of the runway. The airplane's lowest altitude was 800 feet as it neared the runway, and then climbed to 1,700 feet, where radar contact was lost, north of the runway. During the postaccident examination of the airplane, no mechanical malfunction was found. Given the lack of any mechanical deficiencies with the airplane, it is likely the pilot was either confused about the proper approach procedures, or elected to disregard them, and abandoned the instrument approach prematurely in his attempt to find the runway. It is unknown why he decided to do a circle to land approach, when the tailwind component was slight, and the shorter, simpler, straight in approach was a viable option. Likewise, it is unknown why he flew towards rising terrain on the north side of the runway, contrary to the published procedures. From the witness statements, it appears the pilot was "hunting" for the airport, and intentionally dove the airplane towards what he perceived was an area close to it. In the process, he probably saw
trees and terrain, attempted to climb, but was too low to avoid the trees.
Probable cause:
The pilot's failure to maintain altitude/distance from obstacles during an IFR circling approach, and his failure to follow the instrument approach procedure. Contributing to the accident was clouds.
Final Report:

Crash of a Beechcraft B200 Super King Air in Garissa

Date & Time: Aug 6, 2007
Operator:
Registration:
5Y-HHM
Flight Type:
Survivors:
Yes
Schedule:
Nairobi - Garissa
MSN:
BB-1152
YOM:
1983
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was completing a positioning flight from Nairobi to Garissa. On final approach to Garissa, a donkey entered the runway. The crew initiated a go-around procedure but the aircraft stalled and landed very hard. Both pilots escaped uninjured while the aircraft was damaged beyond repair.

Crash of a De Havilland DHC-2 Beaver in Dodger Channel

Date & Time: Jul 31, 2007 at 1258 LT
Type of aircraft:
Operator:
Registration:
N340KA
Survivors:
Yes
Schedule:
Patricia Bay - Dodger Channel
MSN:
1127
YOM:
1957
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The Sound Flight DHC-2 float-equipped Beaver aircraft, N340KA, flew from Patricia Bay to Dodger Channel where the pilot planned to land. He set up an approach to land to the south in Dodger Channel, into the wind. On short final, the pilot noticed a shoal so he decided to overshoot, make a circuit, and land beyond the shoal. He applied power, established a climb and began a left turn. As the aircraft turned, it came into the lee of Diana Island. The aircraft encountered subsiding air and began to descend. The pilot was unable to arrest the descent. The aircraft struck the water and sank. All six occupants escaped without any injury but the aircraft was damaged beyond repair.

Crash of a Learjet 25 in Saint Augustine

Date & Time: Jul 21, 2007 at 1410 LT
Type of aircraft:
Operator:
Registration:
N70SK
Flight Type:
Survivors:
Yes
Schedule:
Gainesville - Saint Augustine
MSN:
25-49
YOM:
1970
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4620
Captain / Total hours on type:
250.00
Copilot / Total flying hours:
2453
Copilot / Total hours on type:
368
Aircraft flight hours:
15812
Circumstances:
About 5 miles from the destination airport, the flight was cleared by air traffic control to descend from its cruise altitude of 5,000 feet for a visual approach. As the first officer reduced engine power, both engines "quit." The captain attempted to restart both engines without success. He then took control of the airplane, and instructed the first officer to contact air traffic control and advise them that the airplane had experienced a "dual flameout." The captain configured the airplane by extending the landing gear and flaps and subsequently landed the airplane on the runway "hard," resulting in substantial damage to the airframe. Both engines were test run following the accident at full and idle power with no anomalies noted. Examination of the airplane revealed that it was equipped with an aftermarket throttle
quadrant, and that the power lever locking mechanism pins as well as the throttle quadrant idle stops for both engines were worn. The power lever locking mechanism internal springs for both the left and right power levers were worn and broken. Additionally, it was possible to repeatedly move the left engine's power lever directly into cutoff without first releasing its power lever locking mechanism; however, the right engine's power lever could not be moved to the cut off position without first releasing its associated locking mechanism. The right throttle thrust reverser solenoid installed on the airplane was found to be non-functional, but it is not believed that this component contributed to the accident. No explicit inspection or repair instructions were available for the throttle quadrant assembly. Other than the throttle quadrant issues, no other issues were identified with either the engines or airframe that could be contributed to both engines losing power simultaneously.
Probable cause:
A loss of power on both engines for an undetermined reason.
Final Report:

Crash of an Airbus A320-233 in São Paulo: 199 killed

Date & Time: Jul 17, 2007 at 1854 LT
Type of aircraft:
Operator:
Registration:
PR-MBK
Survivors:
No
Site:
Schedule:
Porto Alegre – São Paulo
MSN:
789
YOM:
1998
Flight number:
JJ3054
Country:
Crew on board:
6
Crew fatalities:
Pax on board:
181
Pax fatalities:
Other fatalities:
Total fatalities:
199
Captain / Total flying hours:
13654
Captain / Total hours on type:
2236.00
Copilot / Total flying hours:
14760
Copilot / Total hours on type:
237
Aircraft flight hours:
20000
Aircraft flight cycles:
9300
Circumstances:
On 17 July 2007, at 17:19 local time (20:19 UTC), the Airbus aircraft, model A320, registration PR-MBK, operating as flight JJ3054, departed from Porto Alegre (SBPA) destined to Congonhas Airport (SBSP) in São Paulo city, São Paulo State. There were a total of 187 souls on board the aircraft, being six active crew members and 181 passengers, including 2 infants and 5 extra crew members (not on duty). The weather prevailing along the route and at the destination was adverse, and the crew had to make a few deviations. Up to the moment of the landing, the flight occurred within the expected routine. The aircraft was operating with the number 2 engine reverser de-activated, in accordance with the Minimum Equipment List (MEL). According to information provided to the TWR by crews that had landed earlier, the active runway at Congonhas (35L) was wet and slippery. During the landing, at 18:54 local time (21:54 UTC), the crew noticed that the ground spoilers had not deflected, and the aircraft, which was not slowing down as expected, veered to the left, overran the left edge of the runway near the departure end, crossed over the Washington Luís Avenue, and collided with a building in which the cargo express service of the very operator (TAM Express) functioned, and with a fuel service station. All the persons on board perished. The accident also caused 12 fatalities on the ground among the people that were in the TAM Express building. The aircraft was completely destroyed as a result of the impact and of the raging fire, which lasted for several hours. The accident caused severe damage to the convenience shop area of the service station and to some vehicles that were parked there. The TAM Express building sustained structural damages that determined its demolition. The aircraft was completely destroyed.
Probable cause:
Human factors
1.1 Medical aspect
a. Pain - Undetermined
At a certain moment, during the approach, the PIC reported having a mild headache. Although it was not possible to verify which type of headache it was, or even to evaluate its intensity, it is possible that this trouble may have influenced his cognitive and psychomotor capabilities during the final moments of the flight, when the unpredictability of the situation demanded a higher effectiveness of performance. This factor was considered undetermined due to the impossibility of confirming its contribution in factual terms.

1.2 Operational aspect
a. Training - A contributor
The theoretical qualification of their pilots was founded on the exclusive use of computer interactive courses (CBT), which allowed a massive training, but did not ensure the quality of the training received. In addition, the formation of the SIC was restricted to the “Right Seat Certification”, something that proved insufficient for him to deal with the critical situation experienced after the landing. Lastly, there was a perception among the crews interviewed that the training through the years and on account of the high demand resulting from the company’s growth was being abbreviated.

b. Application of the commands - Undetermined
One of the hypotheses considered in this investigation was that the pilot may have attempted to perform a procedure no longer in force at the time of the accident for the landing with a pinned reverser. This procedure consisted in the receding of both levers to the “IDLE” position during the flare at about a 10-foot altitude, and, after touching down, in activating the only reverser available, maintaining the thrust lever of the other engine in the “IDLE” position.
This procedure, though being more efficient from a braking perspective, could induce the crew to making mistakes, as there were several reports of occurrences in which there was a wrong setting of the levers, motivating the manufacturer to establish a new procedure, months before the accident. Thus, there is a high probability that the PIC inadvertently left one of the thrust levers in the “CL” position, placing the other one first in “IDLE” and later in the “REV” position. This factor was considered undetermined due to the impossibility of confirming its contribution in factual terms.

c. Cockpit coordination - A contributor
Independently of the hypothesis considered, the monitoring of the flight at the landing was not appropriate, since the crew did not have perception of what was happening in the moments that preceded the impact. This loss of situational awareness hindered the adoption of an efficient and timely corrective action.

d. Forgetfulness by the pilot - Undetermined
It is possible that the pilot has inadvertently left one of the levers at the “CL” position, while trying to perform a procedure no longer in force for the operation with a pinned reverser. This factor was considered undetermined due to the impossibility of confirming its contribution in factual terms.

e. Flight indiscipline - Undetermined
The procedure prescribed for the operation with a pinned reverser had been modified by the manufacturer and, according to the FDR recordings, the procedure in force was known to the crew and executed by them on the leg that preceded the accident. However, as this procedure imposed an increase of up to 55 meters in the calculations of runway distance required for landing, it is possible that the PIC deliberately tried to perform adoption of a procedure no longer in force would characterize flight indiscipline. This factor was considered undetermined due to the impossibility of confirming its contribution in factual terms.

f. Influence from the environment - Undetermined
The operating conditions of the Congonhas runway, may have affected the crew’s performance from a psychological perspective, considering the state of anxiety that was present in the cockpit.
In addition, the lack of luminosity resulting from the operation at night time, associated with the size and color of the thrust levers may have hindered the verification of a contingent inappropriate positioning of those controls during the landing. This factor was considered undetermined due to the impossibility of confirming, in factual terms, the psychological influence of the runway operating conditions and/or lack of luminosity on the performance of the crew.

g. Judgment of pilotage - Undetermined
In view of all the operation scenario - the 55 meters added on account of the reverser procedure, the 2.4 extra tons of fuel on account of the tankering, the crowded aircraft, the pressure to proceed to Congonhas, the PIC’s physiological condition (headache), a SIC with little experience in the A-320 and in its autothrust system, the wet and slippery runway, the occurrences of the preceding days - there is a high probability that the PIC deliberately tried to perform the procedure no longer in force for the operation with a pinned reverser, in order to increase the braking efficiency, inadvertently leaving the number 2 engine thrust lever in the “CL” position. Considering this hypothesis, the diversion to an alternate airport would be desirable, instead of trying to perform a procedure that was not prescribed. This factor was considered undetermined due to the impossibility of confirming its contribution in factual terms.

h. Management planning - A contributor
At the time of the accident, the operator had a disproportional number of captains in comparison with the number of co-pilots, a fact that obliged the scheduling sector to form crews with 2 captains. Thus, although complying with the minimum requirements of the regulation in force, such a practice may have contributed to the creation of a climate of complacency in the cockpit of the JJ3054. Besides, the long experience of the SIC as a captain was not a guarantee of his competence in the co-pilot function - for which he had done only the “Right Seat Certification” training - and, added to his little experience in that aircraft, it contributed to the loss of situational awareness in the most critical moments of the flight.

i. Flight planning - Undetermined
Thus, considering the hypothesis that the PIC deliberately tried to perform the old procedure for a landing with a pinned reverser to increase the braking efficiency, it is possible that the use of that procedure was not appropriately prepared, something that could have favored the wrong positioning of the levers (according to the hypothesis mentioned above, it is possible that the PIC inadvertently left the nº2 engine thrust lever in the “CL” position.). The lack of a briefing for the descent in the CVR recording hindered the confirmation of a possible intention of applying the old procedure, no longer in force at the time. This factor was considered undetermined due to the impossibility of confirming its contribution in factual terms.

j. Little experience of the pilot - A contributor
Despite his long experience in commercial jets, the SIC possessed only about 200 flight hours in aircraft of the A320 type. Besides, his experience in the function of co-pilot was restricted to the “Right Seat Certification” training, which proved insufficient to deal with the emergency situation.

k. Management oversight - A contributor
The operator allowed the crew to be composed of two captains, with the occupant of the right-hand seat having done only the “Right Seat Certification” training. Besides, the lack of coordination between the several sectors of the company, especially between the sectors of operation and training, determined the lack of an appropriate monitoring of the processes and of the quality of the pilots’ professional formation.

Psychological aspect
a. Anxiety - Undetermined
The CVR recording allows to perceive that the PIC was showing anxiety in relation to the runway conditions for landing, and on two different occasions he asked the SIC to request from the TWR-SP the rain and runway conditions, and on one of them specifically, whether the runway was slippery. It is possible that the state of anxiety present in the PIC may have influenced the performance of the crew to some extent. This factor was considered undetermined due to the impossibility to confirm that this anxiety has effectively influenced the performance of the crew.

b. Perception error - A contributor
Although perceiving that the ground spoilers had not deflected, the pilots were not able to associate the non-deflection with the positioning of the thrust levers. In addition, there is a high probability that the pilots were led to believe that the lack of the expected deceleration after landing was a result of the conditions of operation with a wet runway, the influence of which, from a psychological aspect perspective in the field of individual variables, was perceived along the investigation.

c. Stress - Undetermined
The stress has effect on the cognitive level (diminution of the concentration, diminution of the response speed, degradation of the memory, etc.), emotional level (alteration of the characteristics of personality, weakening of the emotional control, lowering of the self-esteem, etc.), behavioral level (alterations of the sleep pattern, diminution of interests, verbal articulation problems, etc.), and physiological level (sudoresis, tachycardia, sleep pattern alterations, gastric and dermatologic symptoms, etc.). The presence of stress triggering stimuli was perceived, such as the state of anxiety on the part of the pilots, especially regarding the runway conditions, the cephalalgia of the PIC, the issues concerning the operation in Congonhas with a wet runway, the crowded aircraft and the inoperative reverser. However, it was not possible to determine whether those stimuli effectively led any of the two pilots to a high level of stress. This factor was considered undetermined due to the impossibility to confirm its contribution in factual terms.

d. Lack of perception - A contributor
Considering the hypothesis of a failure in the thrust control system, the contingent stimulus generated from the loss of resistance to the movement of the thrust levers may not have been perceived by the pilot(s), according to the CVR recordings. On the other hand, if one considers the hypothesis that the nº 2 engine thrust lever was inadvertently left in the “CL” position, while the pilots were trying to perform a procedure no longer in force, the characteristics of the autothrust system, which keep the levers motionless during the variations of thrust, in addition to the size and color of those control levers, hard to be observed on a night flight, were not sufficiently evident to be perceived by the pilots. This situation was aggravated by the lack of a warning device relative to the conflicting positioning of the thrust levers.

e. Loss of situational awareness - A contributor
Thus, no matter which hypothesis is considered, the loss of the situational awareness emerged as a result of the very lack of perception on the part of the pilots. In this sense, the automation of the aircraft, however complex, was not capable of providing the pilots with sufficiently clear and accurate stimuli, to the point of favoring their understanding of what was happening in the moments just after the landing in Congonhas.

f. Organizational climate - Undetermined
In relation to the crews of the company, the investigation identified the perception that there was a pressure on the part of the management against diversions, on account of the inconvenience they could arise for the passengers and for the company itself. If the pilots of the JJ3054 shared that perception, it is possible that this factor could have some influence on the pilot’s decision to proceed for the landing in Congonhas, in spite of his concern with the runway operating conditions. This factor was considered undetermined due to the impossibility to confirm its contribution in factual terms.

g. Regulation - A contributor
The regulatory organization, although having already considered the availability of the reversers as a requirement for the operation in Congonhas, at least since April 2006, such a requirement was only formalized as a norm in May 2008. The opportune regulation of this requisite would have prevented the aircraft from operating in Congonhas with a wet runway condition.

h. Training - Undetermined
In relation to the training, the investigation identified in the crews a perception that the company seemed to have reduced the contact hours applied to it, although in formal terms those contact hours had remained unaltered. In relation to crew professional formation, the investigation identified a tendency on the part of the company to reduce the number of hours assigned to training, which remained unaltered in formal terms. Moreover, the FDR recordings showed that, during the period in which the aircraft operated with the pinned reverser, 5 different types of landing procedures were performed by the various crews who operated it. This factor was considered undetermined due to the impossibility to confirm, in factual terms, that the crews’ perception of a shortening in the training processes being applied was consistent with reality and/or whether such alleged shortening effectively influenced the performance of the crew, contributing to the accident.

2 Material factors
a. Design - A contributor
It was verified that, for an A320 airplane proceeding to land, it is possible to place one of the thrust levers at the “REV” position and the other at “CL”, and no alerting device will advise the pilots in an efficient way. This situation may put the aircraft in a critical condition and, depending on the time it takes the crew to identify this configuration, and on the runway parameters, a catastrophic situation may occur. In the specific case of this accident, even with the aircraft on the ground (Weight on Wheels - WOW), with the number 1 engine thrust lever at the “REV” position, with the ground spoilers armed, with the autobrake selected, and with application of maximum braking pressure on the pedals, the power control system gave priority to the information that one of the levers was at “CL”, and this lever did not have any safety devices regarding a possible inadvertent setting.
Final Report:

Crash of an Embraer ERJ-190-100 IGW in Santa Marta

Date & Time: Jul 17, 2007 at 1519 LT
Type of aircraft:
Operator:
Registration:
HK-4455
Survivors:
Yes
Schedule:
Cali - Santa Marta
MSN:
190-00076
YOM:
2007
Flight number:
RPB7330
Country:
Crew on board:
6
Crew fatalities:
Pax on board:
54
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
13737
Captain / Total hours on type:
238.00
Copilot / Total flying hours:
2148
Copilot / Total hours on type:
233
Aircraft flight hours:
998
Circumstances:
Following an uneventful flight from Cali, the crew started the approach to Santa Marta-Simón Bolívar Airport runway 01. On final approach, the crew encountered poor weather conditions with heavy rain falls, turbulences and windshear. As the aircraft was unstable, the captain decided to abandon the approach and initiated a go-around procedure. Few minutes later, the crew started a second approach. Still unstable, the aircraft landed too far down the wet runway 01 at an excessive speed, about 490 metres from the runway end. Unable to stop within the remaining distance, the aircraft overran, went through a fence, collided with pylons, went down a concrete embankment and came to rest with the cockpit in the sea. All 60 occupants evacuated safely while the aircraft was damaged beyond repair.
Probable cause:
 Continuation of the approach and landing without being stabilized on finals with an excessive speed caused the aircraft to cross the threshold of the runway with an additional 41 knots during a low angle approach, which caused the aircraft wheels to touch down positively when there were only 490 meters of runway available, an insufficient distance to stop the aircraft within the runway.
The following contributing factors were identified:
- Lack of situational awareness regarding the approach and landing speed, after having disconnected the automated systems of the aircraft.
- Omission of call outs by the Pilot Monitoring to warn the pilot in control of speeding in order to persuade him to execute a missed approach.
- The delay in initiating a missed approach procedure / interrupted landing in circumstances that indicated the desirability to take such a measure during a destabilized approach.
- Misperception to believe that the aircraft could be stopped within the limited remaining available runway without analyzing the status and distance without having positive contact due to speeding.
Final Report:

Crash of an ATR42-300 in São Paulo

Date & Time: Jul 16, 2007 at 1242 LT
Type of aircraft:
Operator:
Registration:
PT-MFK
Survivors:
Yes
Schedule:
Araçatuba – Bauru – São Paulo
MSN:
225
YOM:
1991
Flight number:
PTN4763
Country:
Crew on board:
4
Crew fatalities:
Pax on board:
21
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7420
Captain / Total hours on type:
4993.00
Copilot / Total flying hours:
947
Copilot / Total hours on type:
797
Circumstances:
The aircraft departed Araçatuba on a flight to São Paulo with an intermediate stop in Bauru, carrying 21 passengers and a crew of four. After touchdown on wet runway 17R at Congonhas Airport, the crew started the braking procedure when the aircraft deviated to the left and veered off runway. While contacting soft ground, the aircraft collided with a concrete block housing the electrical device supplying the runway light system. On impact, the nose gear was torn off and the aircraft came to rest. All 25 occupants evacuated safely while the aircraft was damaged beyond repair.
Probable cause:
Loss of control upon landing after the aircraft suffered aquaplaning. The following contributing factors were identified:
- A light rain caused the presence of water on the runway, enabling the occurrence of hydroplaning.
- The accumulation of water on the surface of the runway, as a result of inadequate drainage, lack of "grooving", enabled the hydroplaning.
- The pilot applied full pressure on the right pedal, generating a force to the left that contributed to the departure off the runway.
- During hydroplaning, the pilot should not apply pedal to the opposite side to which the aircraft slides; this fact was not covered during the instruction of the pilot.
- In the face of hydroplaning, the pilot applied the right pedal, aggravating the departure of the aircraft to the left.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in Orlando

Date & Time: Jul 11, 2007 at 1215 LT
Operator:
Registration:
N105GC
Flight Type:
Survivors:
Yes
Schedule:
Melbourne - Orlando
MSN:
31-7652130
YOM:
1976
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
13000
Captain / Total hours on type:
200.00
Circumstances:
The airplane had undergone routine maintenance, and was returned to service on the day prior to the incident flight. The mechanics who performed the maintenance did not secure the right engine cowling using the procedure outlined in the airplane's maintenance manual. The mechanic who had been working on the outboard side of the right engine could not remember if he had fastened the three primary outboard cowl fasteners before returning the airplane to service. During the first flight following the maintenance, the right engine's top cowling departed the airplane. The pilot secured the right engine, but the airplane was unable to maintain altitude, so he then identified a forced landing site. The airplane did not have a sufficient glidepath to clear a tree line and buildings, so he landed the airplane in a clear area about 1,500 yards short of the intended landing area. The airplane came to rest in a field of scrub brush, and about 5 minutes after the pilot deplaned, the grass under the left engine ignited. The subsequent brush fire consumed the airplane. Examination of the right engine cowling revealed that the outboard latching fasteners were set to the "open" position. When asked about the security of the cowling during the preflight inspection, the pilot stated that he "just missed it."
Probable cause:
The mechanic's failure to secure the right engine cowling fasteners. Contributing to the incident was the pilot's inadequate preflight inspection.
Final Report:

Crash of a Cessna 208B Grand Caravan in Aerfort na Minna (Aran Island): 2 killed

Date & Time: Jul 5, 2007 at 1449 LT
Type of aircraft:
Registration:
N208EC
Flight Type:
Survivors:
Yes
Schedule:
Inis Meáin - Aerfort na Minna
MSN:
208B-1153
YOM:
2005
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
9001
Captain / Total hours on type:
476.00
Aircraft flight hours:
320
Aircraft flight cycles:
275
Circumstances:
The purpose of the flight was a demonstration of an aircraft to a group of potential investors and interested parties associated with a proposed airport at Clifden, Co. Galway, some 25 nm to the northwest of EICA. The flight was organised by one of this group who requested the aircraft, a Cessna Caravan registration N208EC, through an Aircraft Services Intermediary (ASI) from the aircraft’s beneficial owner. The owner agreed to loan his aircraft and the pilot, to fly the group from EICA to EIMN, (a distance of 9 nm) and back. The aircraft departed from Weston (EIWT) aerodrome, near Dublin, at 08.20 hrs on the day of the accident. It over flew Galway (EICM) to EICA where it landed and shutdown. There were two persons on board, the Pilot and an Aircraft Maintenance Specialist (AMS). After a short discussion with ground staff, the Pilot and AMS flew a familiarisation flight to EIMN where the aircraft landed and taxied to the terminal. It did not stop or shut down but turned on the ramp and flew back to EICA where it shut down and parked while awaiting the arrival of the group. The group assembled at EICA, but as there were too many passengers to be accommodated on one aircraft, two flights were proposed with the aircraft returning to pick up the remainder. The aircraft then departed with the first part of the group. On arrival at EIMN, the Pilot contacted those remaining and informed them that he would not be returning for them. This did not cause a problem because an Aer Arran Islander aircraft, with its pilot, was available at EICA to fly the remainder of the group across to EIMN. Following lunch in a local hotel the AMS made a presentation on behalf of the ASI on the Cessna Caravan, its operation and costing. The Pilot assisted him, answering questions of an operational nature. During the presentation two members of the group, who had a meeting to attend on the mainland, travelled back on the Islander aircraft to EICA. The Islander aircraft subsequently returned to EIMN to assist in transporting the remainder of the group back to EICA. The aircraft was returning on a short flight from Inis Meáin (EIMN), one of the Aran Islands in Galway Bay, to Connemara Airport (EICA), in marginal weather conditions when the accident occurred. There had been a significant wind shift, since the time the aircraft had departed earlier from EICA that morning, of which the Pilot appeared to be unaware. As a result a landing was attempted downwind. At a late stage, a go-around was initiated, at a very low speed and high power setting. The aircraft turned to the left, did not gain altitude and maintained a horizontal trajectory. It hit a mound, left wing first and cartwheeled. The Pilot and one of the passengers were fatally injured. The remaining seven passengers were seriously injured. The aircraft was destroyed but there was no fire. The emergency fire service from the airport quickly attended. Later an ambulance, a local doctor and then the Galway Fire Services arrived. A Coastguard Search and Rescue helicopter joined in transporting the injured to hospital. The Gardaí Síochána secured the site pending the arrival of the AAIU Inspectors.
Probable cause:
The Pilot attempted to land downwind in marginal weather conditions. This resulted in a late go-around during which control was lost due to inadequate airspeed.
Contributory Factors:
1. Communications were not established between the Pilot and EICA thus denying the Pilot the opportunity of being informed of the changed wind conditions and the runway in use.
2. The aircraft was over maximum landing weight.
3. The altimeters were under-reading due to incorrect QNH settings.
4. The additional stress on the Pilot associated with the conduct of a demonstration flight.
Final Report: