Crash of a Douglas C-54A-10-DC Skymaster near Missoula: 12 killed

Date & Time: Oct 28, 1960 at 1139 LT
Type of aircraft:
Operator:
Registration:
N48762
Survivors:
No
Site:
Schedule:
Portland – Yakima – Spokane – Missoula
MSN:
10320
YOM:
1944
Flight number:
NW104
Crew on board:
4
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
12
Captain / Total flying hours:
11620
Captain / Total hours on type:
8070.00
Copilot / Total flying hours:
3221
Copilot / Total hours on type:
446
Aircraft flight hours:
36842
Circumstances:
On October 28, 1960, at 1139 m. s. t., a Douglas C-54A-DC, N 48762, operated by Northwest Airlines, Inc., as Flight 104, crashed and burned approximately 13 nautical miles northwest of the Missoula, Montana Airport. The captain, first officer, two hostesses and all eight passengers died in the crash. The flight took off from Spokane, Washington, on an instrument flight plan. En route radio reports were routine and indicated the flight was on schedule, and in no difficulty. The aircraft was observed from the ground flying on course toward Missoula in and along the Clark Fork Valley within six nautical miles west of the scene of the crash. The engines were running and the aircraft was descending as if on an approach to a landing. As the aircraft descended deeper into the valley, flight visibility became restricted by light snow showers, and the tops of the mountains surrounding the valley were obscured by the overcast. The aircraft entered a steep left banking turn and the nose was raised in an apparent attempt to turn and climb out through an intersecting valley; however, the aircraft continued to sink toward the ground, rolled to the left and crashed inverted. The Board believes the accident was caused by the failure of the pilot to continue in accordance with his IFR flight plan by attempting a VFR approach during instrument weather conditions.
Probable cause:
The probable cause of this accident was the failure of the pilot to continue in accordance with his IFR flight plan by attempting a VFR approach during instrument weather conditions.
Final Report:

Crash of a Douglas DC-7C into the Philippines Sea: 1 killed

Date & Time: Jul 14, 1960 at 0430 LT
Type of aircraft:
Operator:
Registration:
N292
Flight Phase:
Survivors:
Yes
Schedule:
New York – Seattle – Anchorage – Cold Bay – Tokyo – Naha – Manila
MSN:
45462
YOM:
1958
Flight number:
NW1-11
Country:
Region:
Crew on board:
7
Crew fatalities:
Pax on board:
51
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
17780
Captain / Total hours on type:
1071.00
Copilot / Total flying hours:
2964
Copilot / Total hours on type:
1190
Aircraft flight hours:
9233
Circumstances:
While the flight was en route between Okinawa and the Philippine Islands, the No. 2 engine experienced an appreciable power loss followed by overspeeding of the propeller. The crew instituted emergency procedures but was unable to control or feather the propeller. The propeller separated from the engine with a resulting nose section fire. Attempts to extinguish the fire failed, and the crew elected to ditch the aircraft. The ditching was accomplished at night during a rainstorm and while under Instrument conditions. All 58 occupants, including the 7 crew members, successfully evacuated the aircraft. Of these, 44 suffered minor injuries and one woman passenger died.
Probable cause:
The Board determines that the probable cause of this accident was the internal failure of No. 2 engine, resulting in oil contamination, loss of oil supply, subsequent loss of the No. 2 propeller assembly, and fire-in-flight, which necessitated a ditching.
Final Report:

Crash of a Lockheed L-188C Electra near Tell City: 63 killed

Date & Time: Mar 17, 1960 at 1525 LT
Type of aircraft:
Operator:
Registration:
N121US
Flight Phase:
Survivors:
No
Schedule:
Minneapolis – Chicago – Miami
MSN:
1057
YOM:
1959
Flight number:
NW710
Crew on board:
6
Crew fatalities:
Pax on board:
57
Pax fatalities:
Other fatalities:
Total fatalities:
63
Captain / Total flying hours:
27523
Captain / Total hours on type:
254.00
Copilot / Total flying hours:
2974
Copilot / Total hours on type:
200
Aircraft flight hours:
1786
Circumstances:
The four engine aircraft departed Chicago-Midway at 1438LT bound for Miami, carrying 57 passengers and a crew of six. While cruising at an altitude of 18,000 feet over the south of Indiana State, the aircraft entered a dive and crashed in a huge explosion in a snow covered field located east of Tell City. Some debris were also found in a wooded area. The aircraft disintegrated on impact and all 63 occupants were killed. The crew was unable to send any distress call prior to the accident.
Probable cause:
The Board determines that the probable cause of this accident was the separation of the right wing in flight due to flutter induced by oscillations of the outboard nacelles. Contributing factors were a reduced stiffness of the structure and the entry of the aircraft into an area of severe clear air turbulence.
Final Report:

Crash of a Douglas DC-6B in Minneapolis

Date & Time: Aug 28, 1958 at 0329 LT
Type of aircraft:
Operator:
Registration:
N575
Flight Phase:
Survivors:
Yes
Schedule:
Washington DC – Pittsburgh – Cleveland – Detroit – Milwaukee – Minneapolis – Portland – Seattle
MSN:
45200
YOM:
1957
Flight number:
NW537
Crew on board:
4
Crew fatalities:
Pax on board:
58
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
12376
Captain / Total hours on type:
572.00
Copilot / Total flying hours:
9089
Copilot / Total hours on type:
148
Aircraft flight hours:
4471
Circumstances:
At approximately 0329LT, the airplane crashed on takeoff from Wold-Chamberlain Field, Minneapolis, Minnesota. A number of the 62 persons (including 2 infants) aboard suffered serious injuries but there were no fatalities. Fire, which broke out a short time after all occupants were evacuated, consumed the aircraft. The aircraft took off normally and climbed to a height of about 100 feet. It then gradually nosed over and entered a descent which continued until it struck the ground. Sky conditions were clear; however, the prevailing visibility was about three miles in fog, and in localized areas around the airport it was reduced to lens than a mile by patches of denser fog. Takeoff was made on runway 22 and the climbout was a from a lighted, built-up section toward an open, unlighted area. The Board believes that the pilot while trying to remain contact in reduced visibility allowed the nose of the aircraft to drop when flaps were retracted because of inattention to flight instruments. The darkness and reduced visibility during climbout contributed to a sensory illusion which completely obscured the fact of descent from the pilot.
Probable cause:
The Board determines that the probable cause of this accident was the pilot's inattention to flight instruments during takeoff in conditions of reduced visibility.
Final Report:

Crash of a Boeing 377 Stratocruiser 10-30 off Seattle: 5 killed

Date & Time: Apr 2, 1956 at 0810 LT
Type of aircraft:
Operator:
Registration:
N74608
Flight Phase:
Survivors:
Yes
Schedule:
Seattle – Portland – Chicago – New York
MSN:
15954
YOM:
1949
Flight number:
NW002
Crew on board:
6
Crew fatalities:
Pax on board:
32
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
14030
Captain / Total hours on type:
1557.00
Copilot / Total flying hours:
7297
Copilot / Total hours on type:
1143
Aircraft flight hours:
18489
Circumstances:
Flight 2 was scheduled daily between Seattle, Washington. and New York, New York, with intermediate stops at Portland, Oregon, and Chicago., Illinois. It departed Seattle-Tacoma Airport at 0806 on an IFR flight plan to Portland, Oregon, via Victor Airway 23 to cruise at 6,000 feet. There were 32 passengers arid a crew of six consisting of Captain Robert Reeve Heard, First Officer Gene Paul Johnson, Flight Engineer Carl Vernon Thomsen, Flight Service Attendant David V. Razey, Senior Stewardess Elinor A. Whitacre. and Junior Stewardess Dorothy L. Oetting. Takeoff was made on runway 20 and the flight climbed to an altitude of 1,000 to 1,200 feet. At this time power reduced and the wing flaps which had been set at the normal 25-degree takeoff position, were retracted at an airspeed of 145 knots. Immediately the crew became aware of severe buffeting and a strong tendency of the aircraft to roll to the left. Because the buffeting began almost immediately after the flaps ware retracted, the captain believed that it was due to a split-flap condition, i. e., the wing flaps on one side of the aircraft being retracted while the flaps on the other side remained partially or fully down. Power was reduced momentarily in an attempt to alleviate the buffeting but this was not effective and maximum continuous power was again restored. After being cleared by the Seattle tower for return the captain decided not to turn the aircraft because of control difficulty and advised that he would proceed to McChord Air Force Base at Tacoma. Thereafter, the captain testified the trouble became worse and the aircraft continued to lose altitude. The captain elected to ditch and did so at approximately 0810. Touchdown was on smooth water at an airspeed of approximately 120 knots and there was no abrupt deceleration. Passengers and crew members, except the captain and first officer, left the aircraft through the main cabin door and emergency exits. The captain and first officer, after a passenger count, left the aircraft through cockpit windows and swam to the left and right wings, respectively. The aircraft sank in approximately 15 minutes and by that time all persons on the wings had been supplied with buoyant cushions from the cabin seats. Those who survived were rescued by surface craft from the 42-degree F. water within 30 to 35 minutes from the time of ditching.
Probable cause:
The Board determines that the probable cause of the accident Was the incorrect analysis of control difficulty which occurred on retraction of the wing flaps as a result of the flight engineer's failure to close the engine cowl flaps - the analysis having been made under conditions of great urgency and within an extremely short period of time available for decision. The following findings were reported:
- Two minutes after takeoff an emergency was declared because of severe buffeting and control difficulty,
- The flight engineer did not close the cowl flaps to takeoff position,
- The cause of the buffeting and control difficulty was not determined by the flight crew and the captain made a decision to ditch the aircraft in Puget Sound,
- The ditching was made under favorable circumstances. The aircraft sank in about 15 minutes and all survivors were rescued from the water shortly thereafter,
- The aircraft was recovered from aver 400 feet of water and examination disclosed that all engine cowl flaps were approximately full-open,
- The buffeting and control difficulty was caused by the improper setting of the engine cowl flaps,
- There was no failure or malfunction of the aircraft, the powerplants, or control systems prior to the ditching.
Final Report:

Crash of a Lockheed L-1049 Super Constellation in McChord AFB

Date & Time: Sep 6, 1953 at 0231 LT
Operator:
Registration:
N6214C
Survivors:
Yes
Schedule:
Seattle – Chicago
MSN:
4014
YOM:
1952
Flight number:
NW008
Crew on board:
6
Crew fatalities:
Pax on board:
26
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
10863
Captain / Total hours on type:
263.00
Copilot / Total flying hours:
4230
Copilot / Total hours on type:
206
Aircraft flight hours:
4509
Circumstances:
Northwest Airlines' Flight 8 departed Seattle-Tacoma Airport at 0148, September 6, 1953, for a nonstop flight to Chicago, Illinois. Gross weight on takeoff was 105,839 pounds; maximum allowable for takeoff was 116,740; maximum allowable for landing was 98.500 pounds. The location of the center of gravity was within prescribed limits. Weather at Seattle-Tacoma Airport during takeoff was: ceiling 200 feet and one-fourth mile visibility. Just after the aircraft became airborne No. 3 propeller oversped. Attempts by the flight engineer to correct this condition were unsuccessful and feathering was started one and one-half minutes later. However, the propeller continued to rotate at about 400 r.p.m. The flight's takeoff alternate was Yakima, Washington (a distance of 122 miles), but due to high terrain en route the captain elected to request clearance to proceed to Portland, Oregon (a distance of 132 miles), at 5,000 feet. This clearance was granted immediately. Using METO 2 power the aircraft reached 5,000 feet, well above the overcast, about 14 minutes after takeoff. Near the end of this climb the oil temperature of No. 4 engine was exceeding limits and the oil supply was being rapidly reduced. The flight engineer attempted to lower the temperature by fully opening the oil cooler flap. Temperature, however, remained high and the oil quantity continued to dwindle fast. Accordingly, the No. 4 propeller was feathered at about 0205 at the order of the captain who then declared an emergency and elected to land at McChord Air Force Base. Radio communication was established with McChord and arrangements made for a GCA approach after a short delay in establishing a frequency. No. 3 propeller had not feathered fully and was still windmilling at approximately 400 r.p.m. Meanwhile the captain had requested "takeoff" flaps, but the flaps would not extend hydraulically, and the copilot went to the cabin to crank them down. He stated that he turned the crank about 15-20 turns, at which point he found that it would no longer turn freely, whereupon he backed it to its original position. He was then called back to the cockpit to assist the captain in controlling the aircraft. Control difficulty had been continuously experienced with the aircraft yawing sharply and dropping a wing. The captain had placed the trim controls approximately in neutral, believing that he had a better feel and control of the aircraft without them at the recommended minimum speed of 130 knots. The aircraft, which had re-entered the overcast at about 2,000 feet, was then several miles from McChord Field under GCA direction on its first approach when its position and heading became such that the GCA operator directed a box pattern be flown to establish a proper approach. The second approach was executed in accordance with the directed pattern and the final approach was in line with Runway 34. The landing gear control was not actuated for gear extension until the aircraft broke out of the overcast at an altitude estimated at between 500 and 800 feet on a GCA controlled straight-in approach to Runway 34. At this time the captain ordered that No. 3 be unfeathered but it would not unfeather and continued to windmill. Only the right main gear extended fully and locked, as Indicated by its green light, but the landing was then committed. Shortly after touchdown retraction of the unlocked nose and left main gears allowed the aircraft to veer off the runway to the left. It then skidded sideways to its right, folding the right main gear inward, and the No. 2 engine was torn free. The aircraft came to rest on a heading of 212 degrees some 3,000 feet from the point of touch and about 7,000 feet short of the far end of the 10,000-foot runway. At about that time a gasoline fire started and spread rapidly over the ground below the airplane. Previously alerted fire apparatus, already standing by, kept the fire from spreading while all passengers and four of the crew left quickly by the main cabin door, the door sill being five or six feet above the ground. The flight engineer and the captain left by the cockpit crew door after ascertaining the cabin to be empty. All 32 occupants ware clear within an estimated two minutes. There were no fatalities although several persons were treated for burns at the McChord Air Force Base Hospital.
Probable cause:
The Board determines that the probable cause of this accident was a sequence of mechanical failures resulting in an emergency landing under adverse weather conditions with insufficient hydraulic pressure in the secondary system to extend fully the landing gear in the time available. A contributing factor was the design of the hydraulic system which did not permit use of the available pressure in the primary system for that purpose. The following findings were pointed out:
- Shortly after takeoff the aircraft lost the use of No. 3 engine due to an overspeeding propeller, and continued windmilling,
- Weather conditions at Seattle-Tacoma were satisfactory for takeoff but were below landing minimums and the captain elected to proceed to Portland,
- After reaching cruising altitude No. 4 propeller was feathered because of high engine oil temperature and depletion of oil supply,
- After losing the use of No. 4 engine, the captain declared an emergency and set up a GCA approach to McChord Air Force Base,
- A malfunction of the landing gear selector valve prevented normal use of the diminished hydraulic pressure to extend the flaps,
- A GCA instrument approach to McChord was necessary because of weather conditions. The captain decided that he would extend the gear only after breaking out under the low overcast,
- The short time interval between breaking out and touchdown was insufficient for extension and locking of all three landing gears with the existing hydraulic pressure,
- After touchdown the unlocked and partially extended left main and nose gears were forced up into their wheel wells with complete loss of control of the aircraft's ground movement, and fire occurred after rupture of the fuel tanks,
- The functional failure of No. 3 propeller governor was due to foreign metallic particles,
- The reason for the loss of oil supply for No. 4 engine was undetermined,
- The landing gear selector valve was improperly seated, resulting in insufficient hydraulic pressure.
Final Report:

Crash of a Douglas C-54E-5-DO Skymaster off Sandspit: 36 killed

Date & Time: Jan 19, 1952 at 0138 LT
Type of aircraft:
Operator:
Registration:
N45342
Survivors:
Yes
Schedule:
Seoul – Tokyo – Shemya – Elmendorf – McChord
MSN:
27279
YOM:
1944
Flight number:
NW324
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
40
Pax fatalities:
Other fatalities:
Total fatalities:
36
Captain / Total flying hours:
8557
Captain / Total hours on type:
1762.00
Copilot / Total flying hours:
4197
Copilot / Total hours on type:
1698
Aircraft flight hours:
18859
Circumstances:
Flight 324 departed Elmendorf Air Force Base at 2111, January 18, with the same 40 passengers who had enplaned at Haneda Air Force Base, Tokyo. The aircraft had 2,600 gallons of fuel and 100 gallons of oil aboard. Gross weight at takeoff was 68,275 pounds (permissible 71,800), and the load was properly distributed with relation to the center of gravity. The flight climbed to the 10,000-foot assigned altitude and at 2213, shortly after passing Middleton Island, requested permission to descend to 8,000 feet. ARTC cleared the flight to descend and the new cruising altitude was reached at 2222. The trip was uneventful until opposite Sitka, Alaska, when the pilot reported, at 0003 (January 19), that No. 1 propeller had been feathered. In another radio transmission (0029), the pilot ascribed the trouble to a "broken" oil cooler, and advised that the flight was proceeding to Sandspit. In other transmissions, he requested weather forecasts for Annette, Sandspit, and Port Hardy. Following receipt of this information, which revealed that Annette weather was below minimums, he again advised that a precautionary landing would be made at Sandspit, and gave 0128 as the estimated time of arrival. The flight was cleared to that point and proceeded without further incident on three engines. The aircraft touched down at a point about one-third down the runway. After a short roll, power was applied at about the mid-point of the strip and the aircraft took off, barely clearing a low fence and driftwood which was approximately two feet high at the end of the runway. After it failed to reappear at the approach end of the landing strip, the Sandspit radio operator discovered from the shouting of survivors that the flight had crashed in Hecate Strait. The radio operator immediately sent notification messages to place Search and Rescue facilities in operation. The wreckage could not be seen because of limited visibility, In company with a Canadian customs official, he launched his small boat and effected the rescue of the seven survivors standing on and clinging to the right wing tip of the partially submerged aircraft. Following the alerting of Search and Rescue facilities, messages were relayed by Annette Flight Control to two other aircraft in the area. They attempted to light the area with flares and locate the wreckage, but were unsuccessful in their efforts.
Probable cause:
The Board determines that the probable cause of this accident was the high approach to the airstrip and the attempt to again become airborne at insufficient air speed, which resulted in the aircraft settling into the water. The following findings were pointed out:
- The No. 1 engine suffered an oil loss, which necessitated shutting down the engine and feathering the propeller,
- In accordance with company operating procedures, the captain elected to land at Sandspit, British Columbia, the first available airport, rather than continue to destination on three engines,
- The aircraft, following an aborted landing at Sandspit and when last observed by a ground witness, was in a shallow left bank at low altitude,
- The aircraft, at near stalling speed during the attempted climb-out, settled into the water, bounced, and came to rest 26 degrees to the left and approximately 4,500 feet from the end of the runway,
- All or nearly all of the passengers evacuated the aircraft, with no known serious injuries,
- Air and water temperatures were near freezing; drowning and exposure accounted for 36 fatalities,
- No steps were taken to prepare passengers for a crash landing or possible ditching,
- Emergency lighting in the cabin was not utilized, nor were any effective measures taken to remove life rafts at the rear of the cabin,
- Search and Rescue facilities were not alerted until after the accident because three-engine operation over water was considered a potential, not an actual, emergency.
Final Report:

Crash of a Martin 202 in Davenport: 10 killed

Date & Time: Jan 16, 1951 at 1214 LT
Type of aircraft:
Operator:
Registration:
N93054
Flight Phase:
Survivors:
No
Site:
Schedule:
Minneapolis – Billings – Spokane – Wenatchee – Seattle
MSN:
9144
YOM:
1948
Flight number:
NW115
Crew on board:
3
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
10
Captain / Total flying hours:
4850
Captain / Total hours on type:
277.00
Copilot / Total flying hours:
692
Copilot / Total hours on type:
84
Aircraft flight hours:
5874
Circumstances:
At Spokane the aircraft was checked visually, and departed Geiger Field at 1204 with the same crew, seven passengers, and 800 gallons of fuel. The flight plan was under Instrument Flight Rules to cruise at 6,000 feet Mean Sea Level between Spokane and Wenatchee, Washington. At takeoff the aircraft’s total weight was 33,822 pounds, as compared with a maximum allowable of 37,780 pounds. The disposable load was distributed in such a manner that the aircraft’s center of gravity was within prescribed limits. Four minutes after takeoff, at 1208, the flight reported having reached the cruising level of 6,000 feet MSL at 1207. At 1212 it was given the Wenatchee weather which was below minima. The flight immediately asked clearance to the next scheduled stop, Yakima, where the weather was above minima. While the Spokane radio operator was obtaining the requested clearance, the flight broadcasted an emergency message. This was at about 1213, only some 15 seconds after asking for the new clearance. No difficulty of any sort had been reported previously. This emergency message was copied by company operators at Spokane, Yakima and Seattle. At the latter place it was also recorded on a magnetic tape by Aeronautical Radio, Inc., an independent radio organization serving several air carriers. The message was in three short sentences. All operators agree that the first was, “We are in trouble,” and that the last was, “Going down fast.” The middle sentence was interpreted by one operator as, “Plane gone nuts” and by the second as, “Right engine haywire.” The third operator put down a series of Q’s, meaning not understood. The actual context of the message will be discussed later in this reports. There was no further radio contact with the flight. At or about 1214 the aircraft crashed on the Pundy farm about three miles west of Reardan, Washington, and approximately 20 miles from Geiger Field. All aboard were killed. A flash fire followed impact and burning continued for some time at the end location throughout the wreckage area. Weather conditions during the short flight from Geiger Field to the impact site included restricted visibility due to light snow. At the flight level there was no icing or turbulence either forecast or reported. Instrument conditions prevailed at the flight’s altitude. At the place and time of the crash the ceiling was about 200 feet and the surface visibility about one-third mile.
Probable cause:
The Board, after extensive study of all evidence determines that the probable cause of this accident was a sudden loss of control for reasons unknown, resulting in rapid descent to the ground. The following items were reported:
- Weather was not contributory since there was no icing and little turbulence,
- The flight was uneventful until 30 to 90 seconds before the crash,
- A difficulty of undetermined origin resulted in loss of control and rapid descent to the ground,
- Examination of the wreckage remaining failed to disclose any evidence of structural failure and/or fire in flight.
Final Report:

Crash of a Martin 202 in Butte: 21 killed

Date & Time: Nov 7, 1950 at 0815 LT
Type of aircraft:
Operator:
Registration:
N93040
Survivors:
No
Schedule:
Chicago – Minneapolis – Billings – Great Falls – Helena – Butte – Seattle
MSN:
9161
YOM:
1947
Flight number:
NW115
Location:
Crew on board:
4
Crew fatalities:
Pax on board:
17
Pax fatalities:
Other fatalities:
Total fatalities:
21
Captain / Total flying hours:
8291
Captain / Total hours on type:
610.00
Copilot / Total flying hours:
2873
Copilot / Total hours on type:
80
Aircraft flight hours:
6166
Circumstances:
The flight left Helena at 0753LT, using Runway 29. The flight plan, amended before takeoff, specified an altitude of 10,500 feet MSL under instrument flight rules via Amber Airway number 2 to the Whitehall (Montana) Range Station and from there to the Butte Airport via Red Airway number 2. Also, before taking off, the pilot asked the Helena Tower if the Homestake Fan normally and was informed that Butte Radio advised that it was. Following takeoff from Runway 29, the aircraft was flown in a climbing right turn so that it passed approximately over the Station as it headed south toward the Whitehall Range Station. At 0801 the flight reported to Helena that it had reached its cruising altitude. This message was acknowledged. The next message from the flight was to Butte at 0814 stating that it was over Whitehall (Range Station) at 0811 and starting descent. Butte acknowledged this message, gave that flight the station altimeter setting of 29.97, advised that the wind was south, calm, and that the Weather Bureau advised what the ceiling was lower to the east and north and better to the south and southwest. Flight 115 replied that it had vertical visibility at 10,500 feet. This was the last radio contact with the flight. A search was instituted after several futile attempts to contact the aircraft. On the following morning, the wreckage was sighted from a local search aircraft at about 0900. Ground parties immediately started for the crash site. All debris were found in a snow covered wooded area and all 21 occupants were killed.
Probable cause:
The Board determines that the probable cause of this accident was the failure of the captain to conduct the flight in accordance with the proscribed approach procedure. The following findings were reported:
- The pilot failed to follows the carrier's prescribed number 2 instrument approach procedure to the Butte Airport, which procedure is approved by the Civil Aeronautics Administration,
- The aircraft struck a mountain at about the 8,250-foot level, while on a heading of approximately 290 degrees magnetic,
- The accident occurred during a local snowstorm and under conditions of variable ceiling and visibility.
Final Report:

Crash of a Martin 202 in Almelund: 6 killed

Date & Time: Oct 13, 1950 at 1049 LT
Type of aircraft:
Operator:
Registration:
NC93037
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Minneapolis - Minneapolis
MSN:
9158
YOM:
1947
Crew on board:
3
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
9800
Captain / Total hours on type:
769.00
Copilot / Total flying hours:
8228
Copilot / Total hours on type:
368
Aircraft flight hours:
5289
Circumstances:
Northwest Airlines' NC93037 departed from the Minneapolis- St Paul International Airport at 0946LT on a local flight. The purpose of the flight was a six-month instrument competency check of Captain John R. Galt under the supervision of Captain Ray Render, a company cheek pilot. Also on board and listed as official observers were William H Solomon, CAA air carrier agent, who was sitting on the jump seat between and immediately behind the pilots' seats, and CAA personnel from the Minneapolis Control Tower, E. Bergstrom, R. Olsen and B. Erickson, who were sitting in the main cabin. At the time of takeoff there were 800 gallons of fuel on board which resulted in a total aircraft weight of 32,943 pounds. This weight was within the allowable limit of 38,000 pounds and the aircraft was properly loaded. The weather was clear and visibility was unlimited. Following takeoff, two simulated US (Instrument landing system) approaches were made to the airport and at 1025LT the crew radioed the control tower that this phase of the check flight was completed. This was the last known contact with the flight. After departing the Minneapolis area, the aircraft was first seen near Center City, Minnesota, 43 miles northwest of Minneapolis. At this time it was making a steep left turn at an altitude estimated to he between 4,000 and 5,000 feet, and landing gear was down. At the completion of this turn a shallow climb was started. Throughout these maneuvers the engines sounded as if they were operating in a normal manner. The attention of the ground witness was then diverted for a few moments, and when he again saw the aircraft it was in a partially inverted position and starting a steep dive. After losing approximately 2,500 feet in the dive, an apparently normal recovery was made to a level flight attitude and the aircraft proceeded in a northeasterly direction. Shortly thereafter it was seen to make two or three pitching oscillations about its lateral axis. These maneuvers may he described as a series of steps made by the aircraft as it was being lowered abruptly, followed by a recovery to level flight. During each oscillation approximately 400 feet in altitude was lost and a noise was heard such as is usually associated with a surge of engine power. The aircraft continued on a northeast heading. Two miles south of Almelund, Minnesota, which is 14 miles northeast of Center City, the aircraft was seen to make a shallow right turn of approximately 270 degrees and once more to return to a level attitude heading in a northwesterly direction. Throughout the above-mentioned maneuvers, the aircraft was gradually losing altitude, and the right propeller was observed to be turning slowly during the latter part of the flight. Nearing Almelund and at an altitude of approximately 500 or 600 feet above the ground, a steep right turn was begun. Altitude was lost rapidly and after turning approximately 90 degrees, the aircraft's right wing struck the ground. All but one of the six occupants were killed at impact, the injured person died several days later without regaining consciousness. The aircraft was demolished.
Probable cause:
The Board determines that the probable cause of this accident was the unwanted reversal of the right propeller during flight, as a result of which the crew was unable to maintain control of the aircraft. The following findings were reported:
- The fuel feed valve of the right engine malfunctioned when tested,
- The right propeller was found in 7 degrees to 10 degrees of reverse thrust,
- A review of the evidence of a similar occurrence indicated that with a propeller in the reverse thrust position the aircraft would assume dangerous flight characteristics,
- The fact that the aircraft's wing flaps were retracted may have contributed to the uncontrollability of the aircraft at speeds below 140 miles per hour.
Final Report: