Crash of a Bristol 175 Britannia 301 in Bristol: 15 killed

Date & Time: Nov 6, 1957
Type of aircraft:
Operator:
Registration:
G-ANCA
Flight Type:
Survivors:
No
Schedule:
Bristol - Bristol
MSN:
12917
YOM:
1956
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
11
Pax fatalities:
Other fatalities:
Total fatalities:
15
Aircraft flight hours:
721
Aircraft flight cycles:
268
Circumstances:
The Bristol 175 had just completed a test flight of 1 and 40 minutes. Tests included a strain-gauge measurements on the non-standard propeller of the no. 2 engine, and high speed upset manoeuvre recovery tests in connection with the US certification. Returning to Filton, the aircraft entered a circuit and partial gear extensions occurred for unknown reasons. Attempts may have been made to complete undercarriage free fall tests as these had failed the previous day; such test were not on the programme however. At 1500 feet a left turn to base leg was initiated. The right wing suddenly dropped and the aircraft went into a very steeply banked right hand turn. The Britannia briefly recovered but banked steeply again and struck the ground in a wood near a residential area.
Probable cause:
The accident was the result of the aircraft developing a very steep descending turn to the right which the pilot was unable to control. The reason for this could not be determined, but the possibility that it occurred as the result of malfunctioning of the autopilot cannot be dismissed.

Crash of a Fairchild C-82A-FA Packet in Mérida: 3 killed

Date & Time: Oct 28, 1957
Type of aircraft:
Operator:
Registration:
XA-LIW
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Mérida - Mérida
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
The crew was involved in a local test flight when the airplane crashed in unknown circumstances shortly after takeoff from Mérida-Rejon Airport. The wreckage was found five km from the airfield and all three occupants were killed.

Crash of a Vickers 806 Viscount in Johannesburg

Date & Time: Oct 20, 1957 at 1100 LT
Type of aircraft:
Operator:
Registration:
G-AOYF
Flight Type:
Survivors:
Yes
Schedule:
Johannesburg - Johannesburg
MSN:
255
YOM:
1957
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The aircraft was temporarily based at the Jan Smuts Airport where the manufacturers were conducting experimental flights which included measured takeoff s and landings. The data had to be obtained for incorporation in the Aircraft Flight Manual to be associated with the certification for public transport operation. The aircraft was being operated in the special categories Research or Experimental and Demonstration. The captain was cleared to use runway 03, the main instrument runway, and took off at 1040 hours on an experimental flight. After completing a circuit, the captain was cleared to land back on runway 03. He approached the runway, holding at 300 - 400 feet until he passed over the threshold. At this point the angle of descent increased to about 45°. The descent continued until the aircraft was about 70 feet above the surface of the runway where it leveled out, but the path of descent appeared to remain fixed at about 45° until touchdown where upon the main bogies appeared to move rearwards and inwards with the starboard side moving rearwards somewhat further than the port side. After this the aircraft bounced a few feet before settling down further along the runway. At this stage heavy smoke was emitted from both bogies as the aircraft continued forward. It finally swung to the right and off the runway and came to rest on a heading of 180° M at a point approximately 1,590 yards from the threshold. No one was killed or injured, but the aircraft was substantially damaged.
Probable cause:
The misjudged roundout resulted in a heavy landing which caused the star- board undercarriage to collapse.
Final Report:

Crash of a Junkers JU.52/3msai in Cafayate

Date & Time: Oct 12, 1957
Type of aircraft:
Operator:
Registration:
T-153
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Cafayate - Cafayate
MSN:
4078
YOM:
1935
Location:
Country:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Christened 'Misiones', the three engine aircraft crashed in unknown circumstances in Cafayate while engaged in a local test flight. There were no injuries but the airplane was destroyed.

Crash of a Nord 2501E Noratlas at Melun-Villaroche: 5 killed

Date & Time: Apr 26, 1957
Type of aircraft:
Operator:
Registration:
40
Flight Type:
Survivors:
No
Schedule:
Melun - Melun
MSN:
40
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
5
Circumstances:
The crew was returning to Melun-Villaroche following an uneventful test flight on behalf of the Direction Technique et Industrielle de l’Aéronautique (DTI). On short final, the airplane went out of control and crashed on runway 29 threshold. All five crew members were killed.
Crew:
Michel Chalard, test pilot,
Marcel Perrin, test pilot,
Louis Pruneau, test engineer,
Jean Duchemin, test mechanic,
Jean Coupet, air engineer.

Crash of a Boeing JB-52C-50-BO Stratofortress in Skiatook: 3 killed

Date & Time: Mar 29, 1957
Type of aircraft:
Operator:
Registration:
54-2676
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Wichita - Wichita
MSN:
17171
YOM:
1954
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
While on a test flight out from Wichita, the aircraft suffered a loss of electrical power while flying in negative G conditions. The aircraft went out of control and crashed near Skiatook, about 15 miles north of Tulsa. A crew member was injured while three other were killed.
Probable cause:
Loss of electrical power due to a defective constant speed drive.

Crash of a Douglas DC-7B in Sunland: 7 killed

Date & Time: Jan 31, 1957 at 1118 LT
Type of aircraft:
Operator:
Registration:
N8210H
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Santa Monica - Santa Monica
MSN:
45192
YOM:
1957
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
7
Captain / Total flying hours:
11757
Captain / Total hours on type:
598.00
Copilot / Total flying hours:
7115
Copilot / Total hours on type:
287
Aircraft flight hours:
1
Circumstances:
On January 31, at 1015, N8210H took off tram runway 03 of the Santa Monica, California, Airport. The aircraft was a new DC-7B being flown for the first time for the purpose of functionally checking the aircraft and its components in flight following production. The flight crew were Douglas Aircraft employees consisting of Pilot William G. Carr; Copilot Archie R. Twitchell; Flight Engineer Waldo B. Adams; and Radio Operator Roy Nakazawa. The aircraft had been subject to many regular inspections during its manufacture and numerous inspections which were required after production preceding the first flight. Accordingly, it was presumed the DC-7B was in airworthy condition. Preparations for the flight by its crew were routine, Departure was on a local VFR flight plan filed with the operations office of the company. The plan showed six hours of fuel aboard end that the flight duration wee estimated as 2 hours 15 minutes. It also showed the gross takeoff night of N8210H was 88,000, pounds, well under the maximum allowable. The load was properly distributed with respect to center of gravity limitations. According to routine procedure the flight switched to the Douglas company radio frequency after takeoff and made periodic progress reports. At 1030 the crew reported over the Catalina intersection, 9,000 feet, routine, and thereafter, at 1106, over Ontario, 25,000 feet, routine. At 1050 that morning, the Northrop operated F-89J, 52-1870, took off from runway 25 of the Palmdale, California, Airport, accompanied by another F-89J, 53-25 6A. The flight of 52-1870 was one of a series of functional flight checks following the completion of IRAN (inspection and repair as necessary), an overhaul project performed under contract by Northrop Aircraft for the United States Air Force. The specific flight was in accordance with provisions of the contract and its purpose was to check the radar fire control systems of both of the all-weather interceptors. The two-member flight crew of 52-1870 consisted of Pilot Roland E. Owen and Radar Operator Curtiss A. Adams, both employees of Northrop. Preparations for the operation were routine and departure was in accordance with a local VFR flight plan filed with the flight department of the company. The plan indicated the estimated duration of the operation as one hour with sufficient fuel aboard for approximately 1 hour and 45 minutes, considering afterburner time, altitude, and power settings for the mission. The F-89's took off individually, using afterburners, with a separation interval, of 20 seconds. In a wide starboard orbit the pilots utilized radar in a “snake climb” to 25,000 feet. At that altitude, a predetermined scissoring flight pattern was utilized which positioned the F-89's, without ground radar control, for simulated all-weather interceptor attacks on each other, during which the operation of airborne radar equipment could be checked. Radio transmissions, on company frequency, were recorded by ground facilities. These were routine commands between the pilots as they executed the radar check pattern and intercepts. At 1118 activity in the Douglas radio roan was interrupted by an emergency transmission from N 8210H. The voices were recognized by radio personnel familiar with the crew members. Pilot Cart first transmitted, “Uncontrollable," Copilot Twitchell then said, “We‘re a midair collision - midair collision, 10 How (aircraft identification using phonetic How for H) we are going in-uncontrollable - uncontrollable - we are . . . we've had it boy - poor jet too - told you we should take chutes - say goodbye to everybody.” Radio Operator Nakazawa’s voice was recognized and he concluded the tragic message with, "We are spinning In the valley.” This final transmission from the flight is presented because it contained important information relative to the accident investigation. It not only establishes the midair collision but also indicates the DC-7 was rendered uncontrollable. It further indicates that Mr. Twitchell at least recognized the aircraft with which they collided as a jet. Further, the DC-7 spun during its descent to the ground. All four crew members on board the DC-7 were killed plus three people on the ground. Seventy others have been injured. Weather conditions in the area at the time of the accident were reported by the Weather Bureau as clear, visibility 50 miles. Winds aloft at 25,000 were approximately 30 knots from 320 degrees.
Probable cause:
The Board determines that the probable cause of this midair collision was the high rate of near head-on closure at high altitude which, together with physiological limitations, resulted in a minimum avoidance opportunity during which the pilots did not see the other’s aircraft. The following findings were reported:
- The flights were operated in clear weather conditions and in accordance with the provisions of local VFR flight plans,
- Under VFR weather conditions and VFR flight plans collision avoidance rested in visual separation, a pilot responsibility,
- The DC-7 and F-89 collided in flight on approximately west and east headings, respectively. They were at 25,000 feet over a non-congested area between one and two miles northeast of the Hansen Dam Spillway,
- At impact the F-89 was rolled about 30 degrees left, both aircraft were about level in the pitch plane, and the convergence angle was about five degrees from head-on,
- Both aircraft tell out of control and the DC-7 crashed in a populated area,
- From visual range, estimated at 3.5 miles, the closure speed between the two aircraft was 700 knots and over the probable flight paths the tine to collision from visual range was about 15 seconds,
- The nature and purpose of the flights did not prevent all pilots from maintaining a lookout for other aircraft,
- There was no evidence found to indicate that any malfunction or failure of the aircraft or their components was a factor in the accident.
Final Report:

Crash of an Avro 696 Shackleton MR.3 near Foolow: 4 killed

Date & Time: Dec 7, 1956
Type of aircraft:
Operator:
Registration:
WR970
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Woodford - Woodford
YOM:
2
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
The crew departed Woodford for a stall-warning test flight. En route, while cruising at a relative low altitude, the crew initiated a stall when control was lost. The airplane dove into the ground and crashed in a prairie located near Foolow. All four crew members were killed, among them Jack Bertram Wales, test pilot by Avro.
Probable cause:
Loss of control during a stall-warning test flight. The stall was initiated at an insufficient altitude to expect a recovery.

Crash of an Avro 683 Lancaster I near Malmen AFB: 2 killed

Date & Time: May 8, 1956
Type of aircraft:
Operator:
Registration:
80001
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Malmen - Malmen
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The crew (two pilots and two engineers) were involved in a local test flight following engine maintenance and modification. Shortly after takeoff from Malmen AFB, while climbing, the engine number one caught fire. Both engineers were able to bail out and were found alive while both pilots were killed when the aircraft crashed in a huge explosion in Slaka Kyrka, about 4 km south of the airbase.
Probable cause:
Loss of control during initial climb following fire on engine number one.

Crash of a De Havilland U-1A Otter in Goose Bay: 3 killed

Date & Time: Apr 10, 1956 at 1856 LT
Type of aircraft:
Operator:
Registration:
3666
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Goose Bay - Goose Bay
MSN:
12
YOM:
1953
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
The crew (two pilots and one mechanic) was engaged in a post-maintenance check flight. Two minutes after takeoff from Goose Bay Airport, while climbing, the crew raised the flaps when the aircraft stalled. Simultaneously, the left wing broke out at its root. Out of control, the airplane dove into the ground and crashed, killing all three occupants. It was reported that ground maintenance was provided on the left port inner trailing edge flap.
Probable cause:
A sudden spontaneous full flap retraction caused the nose of the aircraft to drop. Loads on the wing exceeded the design strength, causing the left hand wing to break off. It struck the tail, causing the airplane to crash.