Crash of a De Havilland Dash-8-Q402 in Aalborg

Date & Time: Sep 9, 2007 at 1557 LT
Operator:
Registration:
LN-RDK
Survivors:
Yes
Schedule:
Copenhagen - Aalborg
MSN:
4025
YOM:
2000
Flight number:
SK1209
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
69
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
17000
Captain / Total hours on type:
1000.00
Copilot / Total flying hours:
6540
Copilot / Total hours on type:
1085
Aircraft flight hours:
12141
Aircraft flight cycles:
14795
Circumstances:
The accident flight was a scheduled domestic flight from Copenhagen Airport, Kastrup (EKCH) to Aalborg Airport (EKYT). The flight was uneventful until the landing gear was selected down during the approach to EKYT runway 26R. The nose landing gear and the left main landing gear (MLG) indicated down and locked. The right MLG indicated “in transit” (not down and locked). The Aalborg Tower was informed about the problem with the right MLG indication. A go-around was initiated at 1100 feet MSL with a climb towards 2000 ft. The flight crew consulted the Quick Reference Handbook (QRH). An alternate landing gear procedure was initiated. The right MLG indication remained in “transit”. A mayday call was made to Aalborg Tower and they were informed about the unsafe landing gear. The flight crew reset the alternate gear extension system and subsequently they tried to make a normal gear up selection. The nose landing gear and the left MLG retracted normally, however the right main landing gear indication remained in “transit”. A second attempt to use the alternate landing gear extension procedure was performed without any changes to the right MLG indication. The aircraft entered a holding pattern in order to reduce the amount of fuel and at the same time to brief the passengers about the situation and to prepare the passengers for an emergency landing. Passengers seated at rows 6, 7 and 8 seats D and F were reseated away from the right propeller area. During the approach the flaps were selected to 10° and the landing gear horn started. The warning horn continued throughout the remaining flight. During the emergency landing the left MLG touched down on the runway first, followed by the right MLG. Shortly after the right MLG contacted the runway the right MLG collapsed. The aircraft departed the runway to the right and came to rest on a heading of 340° at 1357:26 hrs.
Probable cause:
There were five factors’ leading to the accident:
1. There were no specified inspection tasks for inspection of the MLG retraction/extension actuator and rod end either in the MRB’s report or in the Maintenance Requirement Manual in so far as “L”, “A” and “C” checks.
2. The right and left MLG retraction/extension actuator piston and rod end were made of noble martensitic stainless steel and the less noble 4340 steel material, respectively.
3. Severe corrosion in the threaded connection between the right MLG actuator rod and rod end.
4. Separation of the right MLG retraction/extension actuator from the actuator piston rod end.
5. The right MLG stabilizer joint lugs failed.
Final Report:

Crash of a Cessna 208B Grand Caravan in Port-au-Prince

Date & Time: Aug 31, 2007 at 1645 LT
Type of aircraft:
Operator:
Registration:
HH-CAR
Flight Phase:
Survivors:
Yes
Schedule:
Port-au-Prince – Cap Haïtien
MSN:
208B-0699
YOM:
1998
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Shortly after takeoff from Port-au-Prince-Toussaint Louverture Airport runway 10, while in initial climb, the engine lost power. The pilot attempted an emergency landing when the aircraft crash landed in Croix-des-Bouquets, about 5 km east of the airport, coming to rest upside down. A passenger was slightly injured and the aircraft was damaged beyond repair.

Crash of a Britten-Norman BN-2A Islander in La Ceiba

Date & Time: Aug 26, 2007
Type of aircraft:
Operator:
Flight Phase:
Survivors:
Yes
Schedule:
La Ceiba – Puerto Lempira
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
9
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
During the takeoff roll at La Ceiba-Goloson Airport, a tyre burst. The pilot rejected takeoff but the aircraft was unable to stop within the remaining distance. It overran and came to rest 116 metres further. All nine passengers escaped uninjured while the pilot was seriously injured. The aircraft was damaged beyond repair.

Crash of an Antonov AN-26B-100 in Pasto

Date & Time: Aug 22, 2007 at 1510 LT
Type of aircraft:
Operator:
Registration:
HK-4389
Survivors:
Yes
Schedule:
Cali – Villagarzón
MSN:
108 03
YOM:
1981
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
50
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
12243
Captain / Total hours on type:
1133.00
Copilot / Total flying hours:
822
Copilot / Total hours on type:
595
Aircraft flight hours:
17124
Circumstances:
En route from Calí to Villagarzón, the crew contacted ATC and reported technical problems with the left engine. After being cleared to divert to Pasto-Antonio Nariño Airport, the crew modified his route and started the descent. On approach, the flaps were lowered at 38° and the speed was reduced to 250 km/h. After the gears were selected down, the speed increased to 270 km/h so full flaps was selected. After touchdown on runway 02 which is 2,312 metres long, the aircraft was unable to stop within the remaining distance. It overran, went down a 15 metres high embankment and came to rest, broken in two and with its left wing torn off. All 53 occupants were rescued, among them few were injured.
Probable cause:
Taking into account that the operator failed to cooperate with the investigators by sending the necessary documentation on the the anti skid system, the braking system, as well as the propellers and did not manage the reading of the flight recorders; the available evidence establishes as POSSIBLE CAUSE the failure of one or some of the related systems above; in addition to the inadequate operation during the single-engine landing, which finally produced the departure of the aircraft at the end of the runway.
Final Report:

Ground fire of a Boeing 737-809 in Naha

Date & Time: Aug 20, 2007 at 1033 LT
Type of aircraft:
Operator:
Registration:
B-18616
Flight Phase:
Survivors:
Yes
Schedule:
Taipei - Naha
MSN:
30175/1182
YOM:
2002
Flight number:
CI120
Location:
Country:
Region:
Crew on board:
8
Crew fatalities:
Pax on board:
157
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7941
Captain / Total hours on type:
3823.00
Copilot / Total flying hours:
890
Copilot / Total hours on type:
182
Aircraft flight hours:
13664
Circumstances:
The aircraft departed Taipei-Taoyuan Airport at 0814LT on a schedule service to Naha with 157 passengers and a crew of 8. Following an uneventful flight, the crew was cleared to land on runway 18 and vacated via taxiway E6 then A5. After being stopped at spot 41, engines were shot down when a fire broke out somewhere in an area aft of the right engine and spread to the right wing leading edge near the n°5 slat and the apron surface below the right engine. All 165 occupants evacuated safely while the aircraft was totally destroyed by fire.
Probable cause:
It is considered highly probable that this accident occurred through the following causal chain: When the Aircraft retracted the slats after landing at Naha Airport, the track can that housed the inboard main track of the No. 5 slat on the right wing was punctured, creating a hole. Fuel leaked out through the hole, reaching the outside of the wing. A fire started when the leaked fuel came into contact with high-temperature areas on the right engine after the Aircraft stopped in its assigned spot, and the Aircraft burned out after several explosions. With regard to the cause of the puncture in the track can, it is certain that the downstop assembly having detached from the aft end of the above-mentioned inboard main track fell off into the track can, and when the slat was retracted, the assembly was pressed by the track against the track can and punctured it. With regard to the cause of the detachment of the downstop assembly, it is considered highly probable that during the maintenance works for preventing the nut from loosening, which the Company carried out on the downstop assembly about one and a half months prior to the accident based on the Service Letter from the manufacturer of the Aircraft, the washer on the nut side of the assembly fell off, following which the downstop on the nut side of the assembly fell off and then the downstop assembly eventually fell off the track. It is considered highly probable that a factor contributing to the detachment of the downstop assembly was the design of the downstop assembly, which was unable to prevent the assembly from falling off if the washer is not installed. With regard to the detachment of the washer, it is considered probable that the following factors contributed to this: Despite the fact that the nut was in a location difficult to access during the maintenance works, neither the manufacturer of the Aircraft nor the Company had paid sufficient attention to this when preparing the Service Letter and Engineering Order job card, respectively. Also, neither the maintenance operator nor the job supervisor reported the difficulty of the job to the one who had ordered the job.
Final Report:

Crash of a De Havilland Dash-8-Q402 in Busan

Date & Time: Aug 12, 2007 at 0938 LT
Operator:
Registration:
HL5256
Survivors:
Yes
Schedule:
Jeju - Busan
MSN:
4141
YOM:
2006
Flight number:
JJA502
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
74
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8655
Copilot / Total flying hours:
1213
Aircraft flight hours:
1645
Aircraft flight cycles:
1876
Circumstances:
On 12 August 2007, about 05:20, the flight crew showed up and prepared for the flight of Gimpo/Jeju/Gimhae/Gimpo at the crew lounge of the Gimpo Airport. For a flight duty of the flight 103 (Gimpo to Jeju section), the flight crew departed from the Gimpo Airport at about 06:50 and arrived at the Jeju Airport at about 08:15. For the flight 502 (Jeju to Gimhae section), they departed the Jeju Airport at 08:49. While the aircraft passing through an altitude of 9,500 feet), RUD CTRL caution lights and #2 RUD HYD caution lights illuminated. Accordingly, the pilots followed and carried out the procedures) of QRH (Quick Reference Handbook). Referring to the pilots’ statements, #2 RUD HYD caution lights illuminated constantly during the flight; however, RUD CTRL caution lights illuminated intermittently. As it reached a cruising altitude of 15,000 feet, the pilots notified the condition of malfunctions and actions taken according to the QRH to a mechanic stationed at the Gimhae Airport. The pilots received a clearance from the Gimhae Approach Control for ILS RWY 36L then circling approach to RWY 18R. At the final approach course of ILS DME RWY 36L, after visually identifying the runway, the captain received a clearance for conducting a circling approach on initial contact with the Gimhae Control Tower. Referring to the pilots’ statements and the data of Flight Data Recorder (hereinafter referred to as "FDR"), from 09:33:57 until 09:34:03 (for the time of turning from the final approach course of ILS to enter a downwind for circling approach), the caution lights of Elevator Feel, RUD CTRL, Pitch Trim and other warning lights illuminated on the caution and warning lights panel. However, the pilots stated that they couldn’t recall all the caution lights illuminated at the time, and did not take any measures considering the illuminating lights as "nuisance.") The first officer who was a pilot flying continued the circling approach, and aligned his aircraft with the runway 18R on the final approach course. After aligned with runway 18R, the aircraft heading was at 178 degrees magnetic. At that time, according to the ATIS information, the wind direction/speed was 130 degrees at 13 knots gusting to 18 knots, ceiling 4,000 feet, and it was mostly cloudy. According to FDR record, at 09:38:08, about 2 feet above the runway, the rudder started to be applied to the right side. Concurrently, the pilot moved the control wheel to the right. At that time, the aircraft heading changed from 174 degrees to 175 degrees. At 09:38:09, the main landing gear of the aircraft touched down on the runway, and the aircraft heading was at 174 degrees. From the point where the main landing gear touched down, the aircraft continued to drift left into the wind. Initially the pilots applied right rudder in an attempt to maintain runway center-line. Rather then apply left wing down, the control wheel input was toward the right. According to the Cockpit Voice Recorder (hereinafter referred to as "CVR"), at 09:38:11, as the captain kicked onto the rudder pedal and said, "Why, why, Ah?" and the first officer replied, "it doesn’t respond.") At 09:38:13, the nose landing gear touched down, and the pilots started to apply brakes. At 09:38:15, all of sudden, the deceleration rate dropped. According to the tire marks, the aircraft departed the left edge of the runway at 3,500 feet from the end of runway. At 09:38:19, the groaning sound of one of the pilots, "Uh. Uh" was recorded on CVR. After 09:38:15, the heading direction of the aircraft was increasing to the left. According to CVR, at 09:38:25, there was a recorded voice of the captain, "Oh, no, Gosh,"and then at 09:38:27, with a sound of crash, the captain’s screaming sound, "Ah!" was recorded. The aircraft collided into a concrete drainage ditch, which is located 340 feet away from the centerline of the runway 18R and 4,600 feet away from the end of runway, and then it came to rest. When the aircraft stopped in the concrete drainage ditch, the pilots shut off the right engine, declared emergency to the air traffic control tower, and instructed the passengers to perform emergency evacuation.
Probable cause:
The Aviation and Railway Accident Investigation Board determines that the cause of the runway excursion of the Flight 502 was that the rudder failure was not recognized by the pilots during flight and as well as during landing roll. Contributing to this accident was that:
1) the rudder was failing to respond to the pilots' rudder pedal input and
2) After departing from the runway, no appropriate alternative measure was taken to control the aircraft direction.
Final Report:

Crash of a De Havilland DHC-6 Twin Otter 300 off Moorea: 20 killed

Date & Time: Aug 9, 2007 at 1201 LT
Operator:
Registration:
F-OIQI
Flight Phase:
Survivors:
No
Schedule:
Moorea – Papeete
MSN:
608
YOM:
1979
Flight number:
QE1121
Location:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
19
Pax fatalities:
Other fatalities:
Total fatalities:
20
Captain / Total flying hours:
3514
Captain / Total hours on type:
298.00
Aircraft flight hours:
30833
Aircraft flight cycles:
55044
Circumstances:
On Thursday 9 August 2007, the DHC-6 aeroplane registered F-OIQI was scheduled to fly a public transport flight (QE1121) between Moorea and Tahiti Faa’a with a pilot and 19 passengers on board. The flight, with an average duration of 7 minutes, is performed under VFR at a planned cruise altitude of 600 feet. The following information is derived from the on-board audio recording and witness statements. At 21 h 53 min 22, startup was authorised. The pilot made the safety announcement in English and in French: “Ladies and Gentlemen, hello and welcome on board. Please fasten your seatbelts”. At 21 h 57 min 19, the air traffic controller cleared the aeroplane to taxi towards holding point Bravo on runway 12. At 21 h 58 min 10, the aeroplane was cleared to line up. It taxied up the runway and lined up at the level of the second taxiway. At 22 h 00 min 06, the aeroplane was cleared for takeoff. Six seconds later the engines were powered up. At 22 h 00 min 58, the pilot retracted the flaps. At 22 h 01 min 07, propeller speed was reduced. At 22 h 01 min 09 the pilot uttered an expression of surprise. Two GPWS warnings sounded, propeller speed increased and four further GPWS warnings sounded. The aeroplane struck the surface of the sea at 22 h 01 min 20. One minute and eight seconds elapsed between engine power-up and the end of the audio recording. Fourteen bodies were recovered during the rescue operations. Some aeroplane debris, including parts of the right main gear and seat cushions were recovered by fishermen and the rescue team. Some days later, at a depth of seven hundred metres, a fifteenth body was recovered during operations to recover the flight recorder, both engines, the instrument panel, the front part of the cockpit including engine and flaps controls, the flaps jackscrews and the tail section. It was noted that the rudder and elevator control cables were broken off in their forward parts and that the elevator pitch-up control cable had, in its aft part, a second failure whose appearance was different from that observed on the other failures that were examined.
Probable cause:
The accident was caused by the loss of airplane pitch control following the failure, at a low height, of the elevator pitch-up control cable at the time the flaps were retracted. This failure was due to the following series of phenomena:
- Significant wear on the cable in line with a cable guide;
- An external phenomenon, most likely jet blast, which caused the failure of several strands;
- The failure of the last strand or strands under in-flight loads on the elevator control system.
The following factors may have contributed to the accident:
- The absence of information and training for pilots on a loss of pitch control;
- The operator’s failure to carry out some special inspections;
- The failure by the manufacturer and the airworthiness authority to fully take into account the wear phenomenon;
- The failure by the airworthiness authorities, airport authorities and operators to fully take into account the risks associated with jet blast;
- The rules for replacement of stainless steel cables on a calendar basis, without taking into account the activity of the airplane in relation to its type of operation.
Final Report:

Crash of a Let L-410UVP in Bandundu

Date & Time: Jul 18, 2007
Type of aircraft:
Registration:
9Q-CIM
Flight Phase:
Survivors:
Yes
MSN:
83 09 35
YOM:
1983
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Shortly after takeoff from Bandundu Airport, while in initial climb, the twin engine aircraft collided with a flock of birds, stalled and crashed. There were no casualties but the aircraft was destroyed.
Probable cause:
Loss of control and subsequent crash on takeoff following a bird strike.

Crash of an Airbus A320-233 in São Paulo: 199 killed

Date & Time: Jul 17, 2007 at 1854 LT
Type of aircraft:
Operator:
Registration:
PR-MBK
Survivors:
No
Site:
Schedule:
Porto Alegre – São Paulo
MSN:
789
YOM:
1998
Flight number:
JJ3054
Country:
Crew on board:
6
Crew fatalities:
Pax on board:
181
Pax fatalities:
Other fatalities:
Total fatalities:
199
Captain / Total flying hours:
13654
Captain / Total hours on type:
2236.00
Copilot / Total flying hours:
14760
Copilot / Total hours on type:
237
Aircraft flight hours:
20000
Aircraft flight cycles:
9300
Circumstances:
On 17 July 2007, at 17:19 local time (20:19 UTC), the Airbus aircraft, model A320, registration PR-MBK, operating as flight JJ3054, departed from Porto Alegre (SBPA) destined to Congonhas Airport (SBSP) in São Paulo city, São Paulo State. There were a total of 187 souls on board the aircraft, being six active crew members and 181 passengers, including 2 infants and 5 extra crew members (not on duty). The weather prevailing along the route and at the destination was adverse, and the crew had to make a few deviations. Up to the moment of the landing, the flight occurred within the expected routine. The aircraft was operating with the number 2 engine reverser de-activated, in accordance with the Minimum Equipment List (MEL). According to information provided to the TWR by crews that had landed earlier, the active runway at Congonhas (35L) was wet and slippery. During the landing, at 18:54 local time (21:54 UTC), the crew noticed that the ground spoilers had not deflected, and the aircraft, which was not slowing down as expected, veered to the left, overran the left edge of the runway near the departure end, crossed over the Washington Luís Avenue, and collided with a building in which the cargo express service of the very operator (TAM Express) functioned, and with a fuel service station. All the persons on board perished. The accident also caused 12 fatalities on the ground among the people that were in the TAM Express building. The aircraft was completely destroyed as a result of the impact and of the raging fire, which lasted for several hours. The accident caused severe damage to the convenience shop area of the service station and to some vehicles that were parked there. The TAM Express building sustained structural damages that determined its demolition. The aircraft was completely destroyed.
Probable cause:
Human factors
1.1 Medical aspect
a. Pain - Undetermined
At a certain moment, during the approach, the PIC reported having a mild headache. Although it was not possible to verify which type of headache it was, or even to evaluate its intensity, it is possible that this trouble may have influenced his cognitive and psychomotor capabilities during the final moments of the flight, when the unpredictability of the situation demanded a higher effectiveness of performance. This factor was considered undetermined due to the impossibility of confirming its contribution in factual terms.

1.2 Operational aspect
a. Training - A contributor
The theoretical qualification of their pilots was founded on the exclusive use of computer interactive courses (CBT), which allowed a massive training, but did not ensure the quality of the training received. In addition, the formation of the SIC was restricted to the “Right Seat Certification”, something that proved insufficient for him to deal with the critical situation experienced after the landing. Lastly, there was a perception among the crews interviewed that the training through the years and on account of the high demand resulting from the company’s growth was being abbreviated.

b. Application of the commands - Undetermined
One of the hypotheses considered in this investigation was that the pilot may have attempted to perform a procedure no longer in force at the time of the accident for the landing with a pinned reverser. This procedure consisted in the receding of both levers to the “IDLE” position during the flare at about a 10-foot altitude, and, after touching down, in activating the only reverser available, maintaining the thrust lever of the other engine in the “IDLE” position.
This procedure, though being more efficient from a braking perspective, could induce the crew to making mistakes, as there were several reports of occurrences in which there was a wrong setting of the levers, motivating the manufacturer to establish a new procedure, months before the accident. Thus, there is a high probability that the PIC inadvertently left one of the thrust levers in the “CL” position, placing the other one first in “IDLE” and later in the “REV” position. This factor was considered undetermined due to the impossibility of confirming its contribution in factual terms.

c. Cockpit coordination - A contributor
Independently of the hypothesis considered, the monitoring of the flight at the landing was not appropriate, since the crew did not have perception of what was happening in the moments that preceded the impact. This loss of situational awareness hindered the adoption of an efficient and timely corrective action.

d. Forgetfulness by the pilot - Undetermined
It is possible that the pilot has inadvertently left one of the levers at the “CL” position, while trying to perform a procedure no longer in force for the operation with a pinned reverser. This factor was considered undetermined due to the impossibility of confirming its contribution in factual terms.

e. Flight indiscipline - Undetermined
The procedure prescribed for the operation with a pinned reverser had been modified by the manufacturer and, according to the FDR recordings, the procedure in force was known to the crew and executed by them on the leg that preceded the accident. However, as this procedure imposed an increase of up to 55 meters in the calculations of runway distance required for landing, it is possible that the PIC deliberately tried to perform adoption of a procedure no longer in force would characterize flight indiscipline. This factor was considered undetermined due to the impossibility of confirming its contribution in factual terms.

f. Influence from the environment - Undetermined
The operating conditions of the Congonhas runway, may have affected the crew’s performance from a psychological perspective, considering the state of anxiety that was present in the cockpit.
In addition, the lack of luminosity resulting from the operation at night time, associated with the size and color of the thrust levers may have hindered the verification of a contingent inappropriate positioning of those controls during the landing. This factor was considered undetermined due to the impossibility of confirming, in factual terms, the psychological influence of the runway operating conditions and/or lack of luminosity on the performance of the crew.

g. Judgment of pilotage - Undetermined
In view of all the operation scenario - the 55 meters added on account of the reverser procedure, the 2.4 extra tons of fuel on account of the tankering, the crowded aircraft, the pressure to proceed to Congonhas, the PIC’s physiological condition (headache), a SIC with little experience in the A-320 and in its autothrust system, the wet and slippery runway, the occurrences of the preceding days - there is a high probability that the PIC deliberately tried to perform the procedure no longer in force for the operation with a pinned reverser, in order to increase the braking efficiency, inadvertently leaving the number 2 engine thrust lever in the “CL” position. Considering this hypothesis, the diversion to an alternate airport would be desirable, instead of trying to perform a procedure that was not prescribed. This factor was considered undetermined due to the impossibility of confirming its contribution in factual terms.

h. Management planning - A contributor
At the time of the accident, the operator had a disproportional number of captains in comparison with the number of co-pilots, a fact that obliged the scheduling sector to form crews with 2 captains. Thus, although complying with the minimum requirements of the regulation in force, such a practice may have contributed to the creation of a climate of complacency in the cockpit of the JJ3054. Besides, the long experience of the SIC as a captain was not a guarantee of his competence in the co-pilot function - for which he had done only the “Right Seat Certification” training - and, added to his little experience in that aircraft, it contributed to the loss of situational awareness in the most critical moments of the flight.

i. Flight planning - Undetermined
Thus, considering the hypothesis that the PIC deliberately tried to perform the old procedure for a landing with a pinned reverser to increase the braking efficiency, it is possible that the use of that procedure was not appropriately prepared, something that could have favored the wrong positioning of the levers (according to the hypothesis mentioned above, it is possible that the PIC inadvertently left the nº2 engine thrust lever in the “CL” position.). The lack of a briefing for the descent in the CVR recording hindered the confirmation of a possible intention of applying the old procedure, no longer in force at the time. This factor was considered undetermined due to the impossibility of confirming its contribution in factual terms.

j. Little experience of the pilot - A contributor
Despite his long experience in commercial jets, the SIC possessed only about 200 flight hours in aircraft of the A320 type. Besides, his experience in the function of co-pilot was restricted to the “Right Seat Certification” training, which proved insufficient to deal with the emergency situation.

k. Management oversight - A contributor
The operator allowed the crew to be composed of two captains, with the occupant of the right-hand seat having done only the “Right Seat Certification” training. Besides, the lack of coordination between the several sectors of the company, especially between the sectors of operation and training, determined the lack of an appropriate monitoring of the processes and of the quality of the pilots’ professional formation.

Psychological aspect
a. Anxiety - Undetermined
The CVR recording allows to perceive that the PIC was showing anxiety in relation to the runway conditions for landing, and on two different occasions he asked the SIC to request from the TWR-SP the rain and runway conditions, and on one of them specifically, whether the runway was slippery. It is possible that the state of anxiety present in the PIC may have influenced the performance of the crew to some extent. This factor was considered undetermined due to the impossibility to confirm that this anxiety has effectively influenced the performance of the crew.

b. Perception error - A contributor
Although perceiving that the ground spoilers had not deflected, the pilots were not able to associate the non-deflection with the positioning of the thrust levers. In addition, there is a high probability that the pilots were led to believe that the lack of the expected deceleration after landing was a result of the conditions of operation with a wet runway, the influence of which, from a psychological aspect perspective in the field of individual variables, was perceived along the investigation.

c. Stress - Undetermined
The stress has effect on the cognitive level (diminution of the concentration, diminution of the response speed, degradation of the memory, etc.), emotional level (alteration of the characteristics of personality, weakening of the emotional control, lowering of the self-esteem, etc.), behavioral level (alterations of the sleep pattern, diminution of interests, verbal articulation problems, etc.), and physiological level (sudoresis, tachycardia, sleep pattern alterations, gastric and dermatologic symptoms, etc.). The presence of stress triggering stimuli was perceived, such as the state of anxiety on the part of the pilots, especially regarding the runway conditions, the cephalalgia of the PIC, the issues concerning the operation in Congonhas with a wet runway, the crowded aircraft and the inoperative reverser. However, it was not possible to determine whether those stimuli effectively led any of the two pilots to a high level of stress. This factor was considered undetermined due to the impossibility to confirm its contribution in factual terms.

d. Lack of perception - A contributor
Considering the hypothesis of a failure in the thrust control system, the contingent stimulus generated from the loss of resistance to the movement of the thrust levers may not have been perceived by the pilot(s), according to the CVR recordings. On the other hand, if one considers the hypothesis that the nº 2 engine thrust lever was inadvertently left in the “CL” position, while the pilots were trying to perform a procedure no longer in force, the characteristics of the autothrust system, which keep the levers motionless during the variations of thrust, in addition to the size and color of those control levers, hard to be observed on a night flight, were not sufficiently evident to be perceived by the pilots. This situation was aggravated by the lack of a warning device relative to the conflicting positioning of the thrust levers.

e. Loss of situational awareness - A contributor
Thus, no matter which hypothesis is considered, the loss of the situational awareness emerged as a result of the very lack of perception on the part of the pilots. In this sense, the automation of the aircraft, however complex, was not capable of providing the pilots with sufficiently clear and accurate stimuli, to the point of favoring their understanding of what was happening in the moments just after the landing in Congonhas.

f. Organizational climate - Undetermined
In relation to the crews of the company, the investigation identified the perception that there was a pressure on the part of the management against diversions, on account of the inconvenience they could arise for the passengers and for the company itself. If the pilots of the JJ3054 shared that perception, it is possible that this factor could have some influence on the pilot’s decision to proceed for the landing in Congonhas, in spite of his concern with the runway operating conditions. This factor was considered undetermined due to the impossibility to confirm its contribution in factual terms.

g. Regulation - A contributor
The regulatory organization, although having already considered the availability of the reversers as a requirement for the operation in Congonhas, at least since April 2006, such a requirement was only formalized as a norm in May 2008. The opportune regulation of this requisite would have prevented the aircraft from operating in Congonhas with a wet runway condition.

h. Training - Undetermined
In relation to the training, the investigation identified in the crews a perception that the company seemed to have reduced the contact hours applied to it, although in formal terms those contact hours had remained unaltered. In relation to crew professional formation, the investigation identified a tendency on the part of the company to reduce the number of hours assigned to training, which remained unaltered in formal terms. Moreover, the FDR recordings showed that, during the period in which the aircraft operated with the pinned reverser, 5 different types of landing procedures were performed by the various crews who operated it. This factor was considered undetermined due to the impossibility to confirm, in factual terms, that the crews’ perception of a shortening in the training processes being applied was consistent with reality and/or whether such alleged shortening effectively influenced the performance of the crew, contributing to the accident.

2 Material factors
a. Design - A contributor
It was verified that, for an A320 airplane proceeding to land, it is possible to place one of the thrust levers at the “REV” position and the other at “CL”, and no alerting device will advise the pilots in an efficient way. This situation may put the aircraft in a critical condition and, depending on the time it takes the crew to identify this configuration, and on the runway parameters, a catastrophic situation may occur. In the specific case of this accident, even with the aircraft on the ground (Weight on Wheels - WOW), with the number 1 engine thrust lever at the “REV” position, with the ground spoilers armed, with the autobrake selected, and with application of maximum braking pressure on the pedals, the power control system gave priority to the information that one of the levers was at “CL”, and this lever did not have any safety devices regarding a possible inadvertent setting.
Final Report:

Crash of an Embraer ERJ-190-100 IGW in Santa Marta

Date & Time: Jul 17, 2007 at 1519 LT
Type of aircraft:
Operator:
Registration:
HK-4455
Survivors:
Yes
Schedule:
Cali - Santa Marta
MSN:
190-00076
YOM:
2007
Flight number:
RPB7330
Country:
Crew on board:
6
Crew fatalities:
Pax on board:
54
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
13737
Captain / Total hours on type:
238.00
Copilot / Total flying hours:
2148
Copilot / Total hours on type:
233
Aircraft flight hours:
998
Circumstances:
Following an uneventful flight from Cali, the crew started the approach to Santa Marta-Simón Bolívar Airport runway 01. On final approach, the crew encountered poor weather conditions with heavy rain falls, turbulences and windshear. As the aircraft was unstable, the captain decided to abandon the approach and initiated a go-around procedure. Few minutes later, the crew started a second approach. Still unstable, the aircraft landed too far down the wet runway 01 at an excessive speed, about 490 metres from the runway end. Unable to stop within the remaining distance, the aircraft overran, went through a fence, collided with pylons, went down a concrete embankment and came to rest with the cockpit in the sea. All 60 occupants evacuated safely while the aircraft was damaged beyond repair.
Probable cause:
 Continuation of the approach and landing without being stabilized on finals with an excessive speed caused the aircraft to cross the threshold of the runway with an additional 41 knots during a low angle approach, which caused the aircraft wheels to touch down positively when there were only 490 meters of runway available, an insufficient distance to stop the aircraft within the runway.
The following contributing factors were identified:
- Lack of situational awareness regarding the approach and landing speed, after having disconnected the automated systems of the aircraft.
- Omission of call outs by the Pilot Monitoring to warn the pilot in control of speeding in order to persuade him to execute a missed approach.
- The delay in initiating a missed approach procedure / interrupted landing in circumstances that indicated the desirability to take such a measure during a destabilized approach.
- Misperception to believe that the aircraft could be stopped within the limited remaining available runway without analyzing the status and distance without having positive contact due to speeding.
Final Report: