Crash of a Beechcraft B200 Super King near Coleman: 3 killed

Date & Time: Feb 20, 2020 at 0600 LT
Operator:
Registration:
N860J
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Abilene – Harlingen
MSN:
BB-1067
YOM:
1982
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
5300
Circumstances:
The pilot and two passengers departed on an instrument flight rules cross-country flight in night instrument meteorological conditions (IMC). The pilot was instructed by air traffic control to climb to 12,000 ft, and then cleared to climb to FL230. The pilot reported to the controller that the airplane encountered freezing drizzle and light rime icing during the climb from 6,500 ft to 8,000 ft mean sea level (msl). As the airplane climbed through 11,600 ft msl, the pilot reported that they had an issue with faulty deicing equipment and needed to return to the airport. The controller instructed the pilot to descend and cleared the airplane back to the airport. When asked by the controller if there was an emergency, the pilot stated that they “blew a breaker,” and were unable to reset it. As the controller descended the airplane toward the airport, the pilot reported that they were having issues with faulty instruments. At this time, the airplane was at an altitude of about 4,700 ft. The controller instructed the pilot to maintain 5,000 ft, and the pilot responded that he was “pulling up.” There was no further communication with the pilot. Review of the airplane’s radar track showed the airplane’s departure from the airport and the subsequent turn and southeast track toward its destination. The track appeared as a straight line before a descending, right turn was observed. The turn radius decreased before the flight track ended. The airplane impacted terrain in a right-wing-low attitude. The wreckage was scattered and highly fragmented along a path that continued for about 570 ft. Examination of the wreckage noted various pieces of the flight control surfaces and cables in the wreckage path. Control continuity could not be established due the fragmentation of the wreckage; however, no preimpact anomalies were found. Examination of the left and right engines found rotational signatures and did not identify any pre-impact anomalies. A review of maintenance records noted two discrepancies with the propeller deice and surface deice circuit breakers, which were addressed by maintenance personnel. Impact damage and fragmentation prevented determination of which circuit breaker(s) the pilot was having issues with or an examination of any deicing systems on the airplane. The radio transmissions and transponder returns reflected in the radar data indicate that the airplane’s electrical system was operational before the accident. It is likely that the pilot’s communications with the controller and attempted troubleshooting of the circuit breakers introduced distractions from his primary task of monitoring the flight instruments while in IMC. Such interruptions would make him vulnerable to misleading vestibular cues that could adversely affect his ability to effectively interpret the instruments and maintain control of the airplane. The pilot’s report of “faulty instruments” during a decreasing radius turn and his initial distraction with the circuit breakers and radio communications is consistent with the effects of spatial disorientation.
Probable cause:
The pilot’s loss of airplane control due to spatial disorientation. Contributing to the accident was the pilot’s distraction with a “popped” circuit breaker and communications with air traffic control.
Final Report:

Crash of a Cessna 501 Citation I/SP near Fairmount: 4 killed

Date & Time: Feb 8, 2020 at 1013 LT
Type of aircraft:
Operator:
Registration:
N501RG
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Peachtree City - Nashville
MSN:
501-0260
YOM:
1982
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
805
Copilot / Total flying hours:
5924
Copilot / Total hours on type:
55
Aircraft flight hours:
8078
Circumstances:
While on an instructional flight in icing and instrument meteorological conditions (IMC), the pilots indicated that they were having instrumentation difficulties to air traffic control. They initially reported a problem with the autopilot, then a navigational issue, which they later indicated were resolved, and finally they reported it was a problem with the left side attitude indicator. After air traffic control cleared them to their destination, the airplane entered a descending left turn, which continued into a 360° descending turn. An inflight breakup resulted, with the wreckage being scattered over 7,000 ft of wooded terrain. Examination of the engines revealed there were no anomalies that would have precluded normal operation prior to the accident. Control cable continuity was established from the flight controls in the cockpit to all flight control surfaces through multiple overload failures. The pitot-static system was examined, and no blockages were noted. Since there was rotational scoring noted on the vertical gyro and the directional gyro, it’s likely they were operating at the time of the accident. Furthermore, the left side attitude indicator examination revealed that there were no anomalies with the instrument. Examination of the deice valves for the deicing boots revealed that the left wing deice valve did not operate. Corrosion was visible in all three valves and it could not be determined if the corrosion was a result of postimpact environmental exposure. Furthermore, since the cockpit switch positions were compromised in the accident, it could not be determined if the pilots were operating the deicing system at the time of the accident. However, most of the pilot reports (PIREPs) in the area indicated light icing and the airplane performed a 6,000 ft per minute climb just before the loss of control. Given this information, it is unlikely the icing conditions made the airplane uncontrollable. A review of the pilots’ flight experience revealed that the pilot in the left seat did not hold a type rating for the accident airplane model but was scheduled to attend flight training to obtain such a type rating. The pilot in the right seat, who also held a flight instructor certificate, did hold a type rating for the airplane. Given that the remarks section of the filed flight plan described the flight as a “training flight” and the left-seat pilot’s plan to obtain a type rating for the accident airplane model, it is likely the pilot in the left seat was the flying pilot for the majority of the flight. Although the right-seat pilot's autopsy noted coronary artery disease, the condition was poorly described. The circumstances of the accident are not consistent with sudden physical impairment or incapacitation; therefore, it is unlikely it contributed to the event. Toxicology testing identified diphenhydramine, which can cause significant sedation, in the right-seat pilot’s blood. However, the level present at the time of the accident was too low to quantify. Therefore, it is unlikely effects from diphenhydramine contributed to the accident. Prior to entering the descending right turn, air traffic control noted that the airplane was not following assigned headings and altitudes and the pilots’ reported having autopilot problems. Subsequently, the pilots’ reported they were using the right attitude indicator as they had difficulties with the left-side indicator. Information was insufficient to evaluate whether the reported difficulties were the result of a malfunction of the autopilot or the pilots’ management of the autopilot system. However, the reported difficulties likely increased the pilots’ workload, may have diverted their attention while operating in IMC and icing conditions, resulting in task saturation, and may have increased their susceptibility to spatial disorientation. It is also possible that the onset of spatial disorientation was the beginning of the pilots’ difficulties maintaining the airplane’s flight track and what they perceived to be an instrumentation problem. Regardless, since the left seat pilot was not rated to fly the airplane, the right seat pilot’s workload would have increased by having to diagnose the issue, assess the situation, and maintain positive airplane control. The airplane’s track data are consistent with the known effects of spatial disorientation, leading to an inflight loss of control and subsequent inflight breakup.
Probable cause:
The pilots’ loss of control in flight in freezing instrument meteorological conditions due to spatial disorientation and the cumulative effects of task saturation.
Final Report:

Crash of a Beechcraft B60 Duke in Big Spring

Date & Time: Jan 29, 2020 at 1710 LT
Type of aircraft:
Operator:
Registration:
N50JR
Flight Type:
Survivors:
Yes
Schedule:
Abilene – Midland
MSN:
P-303
YOM:
1974
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
25000
Captain / Total hours on type:
7.00
Circumstances:
The pilot was conducting a cross-country flight at a cruise altitude of 10,500 ft mean sea level when the left engine lost all power. He secured the engine and elected to continue to his destination. Shortly thereafter, the right engine lost all power. After selecting an airport for a forced landing, he overflew the runway and entered the pattern. The pilot stated that on short final, after extending the landing gear, "the plane quit flying and the airspeed went to nothing." The airplane landed 200 to 300 yards short of the runway threshold, resulting in substantial damage to the wings and fuselage. During a postaccident examination, only tablespoons of fuel were drained from the left tank. Due to the position of the airplane, the right tank could not be drained; however, when power was applied to the airplane, both fuel quantity gauges indicated empty fuel tanks. Neither fuel tank was breached during the accident, and there was no discoloration present on either of the wings or engine nacelles to indicate a fuel leak; therefore, the loss of engine power is consistent with fuel exhaustion.
Probable cause:
A total loss of engine power in both engines due to fuel exhaustion, which resulted in a landing short of the runway.
Final Report:

Crash of a Piper PA-61 Aerostar (Ted Smith 601P) in Springfield: 3 killed

Date & Time: Jan 28, 2020 at 1503 LT
Operator:
Registration:
N6071R
Flight Type:
Survivors:
No
Site:
Schedule:
Huntsville – Springfield
MSN:
61P-0686-7963324
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
5500
Aircraft flight hours:
3542
Circumstances:
The pilot was conducting an instrument landing system (ILS) approach in instrument meteorological conditions at the conclusion of a cross-country flight. The airplane had been cleared to land, but the tower controller canceled the landing clearance because the airplane appeared not to be established on the localizer as it approached the locator outer marker. The approach controller asked the pilot if he was having an issue with the airplane’s navigation indicator, and the pilot replied, “yup.” Rather than accept the controller’s suggestion to use approach surveillance radar (ASR) approach instead of the ILS approach, the pilot chose to fly the ILS approach again. The pilot was vectored again for the ILS approach, and the controller issued an approach clearance after he confirmed that the pilot was receiving localizer indications on the airplane’s navigation equipment. The airplane joined the localizer and proceeded toward the runway while descending. The pilot was instructed to contact the tower controller; shortly afterward, the airplane entered a left descending turn away from the localizer centerline. At that time, the airplane was about 3 nautical miles from the locator outer marker. The pilot then told the tower controller, “we’ve got a prob.” The tower controller told the pilot to climb and maintain 3,000 ft msl and to turn left to a heading of 180°. The pilot did not respond. During the final 5 seconds of recorded track data, the airplane’s descent rate increased rapidly from 1,500 to about 5,450 ft per minute. The airplane impacted terrain about 1 nm left of the localizer centerline in a left-wing-down and slightly nose down attitude at a groundspeed of about 90 knots. A postimpact fire ensued. Although the pilot was instrument rated, his recent instrument flight experience could not be determined with the available evidence for this investigation. Most of the fuselage, cockpit, and instrument panel was destroyed during the postimpact fire, but examination of the remaining wreckage revealed no anomalies. Acoustic analysis of audio sampled from doorbell security videos was consistent with the airplane's propellers rotating at a speed of 2,500 rpm before a sudden reduction in propeller speed to about 1,200 rpm about 2 seconds before impact. The airplane’s flightpath was consistent with the airplane’s avionics receiving a valid localizer signal during both instrument approaches. However, about 5 months before the accident, the pilot told the airplane’s current maintainer that the horizontal situation indicator (HSI) displayed erroneous heading indications. The maintainer reported that a replacement HSI was purchased and shipped directly to the pilot to be installed in the airplane; however, the available evidence for the investigation did not show whether the malfunctioning HSI was replaced before the flight. The HSI installed in the airplane at the time of the accident sustained significant thermal and fire damage, which prevented testing. During both ILS approaches, the pilot was cleared to maintain 3,000 ft mean sea level (msl) until the airplane was established on the localizer. During the second ILS approach, the airplane descended immediately, even though the airplane was below the lower limit of the glideslope. Although a descent to the glideslope intercept altitude (2,100 ft msl) would have been acceptable after joining the localizer, such a descent was not consistent with how the pilot flew the previous ILS approach, during which he maintained the assigned altitude of 3,000 ft msl until the airplane intercepted the glideslope. If the HSI provided erroneous heading information during the flight, it could have increased the pilot’s workload during the instrument approach and contributed to a breakdown in his instrument scan and his ability to recognize the airplane’s deviation left of course and descent below the glideslope; however, it is unknown if the pilot had replaced the HSI.
Probable cause:
The pilot’s failure to follow the instrument landing system (ILS) course guidance during the instrument approach.
Final Report:

Crash of a Stinson V-77 Reliant in Auburn: 2 killed

Date & Time: Jan 24, 2020 at 0956 LT
Type of aircraft:
Registration:
N50249
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Auburn - Auburn
MSN:
77-458
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
650
Circumstances:
The pilot departed on a local flight with two passengers. Several witnesses reported that they heard the airplane’s engine backfiring and sputtering and subsequently heard the engine quit. The surviving passenger, who was seated in the front right seat, stated that the engine lost power and there was nowhere to land. The airplane subsequently impacted heavily wooded terrain about 1 mile from the departure airport. Postaccident examination of the engine revealed that the No. 7 cylinder intake valve was stuck open. The No. 2 cylinder front spark plug was defective, and the Nos. 2- and 4-cylinders’ ignition wires were frayed, worn, and displayed arcing, which likely led to erratic operation or a lack of ignition in these two cylinders. The culmination of these issues most likely led to the engine running rough, backfiring, and subsequently losing total power. An annual inspection was accomplished on the airframe and engine about 2 months before the
accident. General maintenance practices and the inspection should have identified the anomalies that were found during the postaccident engine examination.
Probable cause:
A total loss of engine power due to a combination of mechanical engine anomalies. Contributing to the accident was inadequate maintenance that failed to identify the engine anomalies.
Final Report:

Crash of a Beechcraft A100 King Air in Charallave: 9 killed

Date & Time: Dec 19, 2019
Type of aircraft:
Operator:
Registration:
YV1104
Flight Type:
Survivors:
No
Schedule:
Guasipati – Charallave
MSN:
B-231
YOM:
1977
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
9
Circumstances:
On final approach to Charallave-Óscar Machado Zuloaga Airport in marginal weather conditions, the twin engine airplane crashed in unknown circumstances about 8 km from the runway threshold. The aircraft was destroyed and all nine occupants were killed.

Crash of a Piper PA-60-602P Super 700 Aerostar on Gabriola Island: 3 killed

Date & Time: Dec 10, 2019 at 1805 LT
Operator:
Registration:
C-FQYW
Flight Type:
Survivors:
No
Schedule:
Cabo San Lucas – Chino – Bishop – Nanaimo
MSN:
60-8265-020
YOM:
1982
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
320
Aircraft flight hours:
5752
Circumstances:
On 09 December 2019, a private Piper Aerostar PA-60-602P aircraft (registration C-FQYW, serial number 60-8265020), departed Cabo San Lucas International Airport (MMSL), Baja California Sur, Mexico, with 3 people on board, for a 2-day trip to Nanaimo Airport (CYCD), British Columbia (BC). As planned the aircraft stopped for an overnight rest at Chino Airport (KCNO), California, U.S. At 1142, on 10 December 2019, the aircraft departed KCNO on a visual flight rules (VFR) flight plan to Bishop Airport (KBIH), California, U.S., for a planned fuel stop. The aircraft departed KBIH at approximately 1425 on an instrument flight rules (IFR) flight plan to CYCD. On 10 December 2019, night started at 1654. At 1741, the Vancouver area control centre air traffic controller advised the pilot that an aerodrome special meteorological report (SPECI) had been issued for CYCD at 1731. The SPECI reported visibility as 2 ½ statute miles (SM) in light drizzle and mist, with an overcast ceiling of 400 feet above ground level (AGL). The pilot informed the controller that he would be conducting an instrument landing system (ILS) approach for Runway 16. At 1749, when the aircraft was approximately 32 nautical miles (NM) south of CYCD, the pilot contacted the controller to inquire about the weather conditions at Victoria International Airport (CYYJ), BC. The controller informed the pilot that a SPECI was issued for CYYJ at 1709 and it reported the visibility as 5 SM in mist, a broken ceiling at 600 feet AGL, and an overcast layer at 1200 feet AGL. The controller provided the occurrence flight with pilot observations from another aircraft that had landed at CYCD approximately 15 minutes before. That crew had reported being able to see the Runway 16 approach lights at minimums, i.e., at 373 feet AGL. Between 1753 and 1802, the controller provided vectors to the pilot in order to intercept the ILS localizer. At 1803, the controller observed that the aircraft had not intercepted the localizer for Runway 16. The aircraft had continued to the southwest, past the localizer, at an altitude of 2100 feet above sea level (ASL) and a ground speed of 140 knots. The controller queried the pilot to confirm that he was still planning to intercept the ILS for Runway 16. The pilot confirmed that he would be intercepting the ILS as planned. The aircraft made a heading correction and momentarily lined up with the localizer before beginning a turn to the west. At 1804:03, the pilot requested vectors from the controller and informed him that he “just had a fail.” The controller responded with instructions to “turn left heading zero nine zero, tight left turn.” The pilot asked the controller to repeat the heading. The controller responded with instructions to “…turn right heading three six zero.” The pilot acknowledged the heading; however, the aircraft continued turning right beyond the assigned heading while climbing to 2500 feet ASL and slowing to a ground speed of 80 knots. The aircraft then began to descend, picking up speed as it was losing altitude. At 1804:33, the aircraft descended to 1800 feet ASL and reached a ground speed of 160 knots. At 1804:40, the pilot informed the air traffic controller that the aircraft had lost its attitude indicator.Footnote6 At the same time, the aircraft was climbing into a 2nd right turn. At 1804:44, the air traffic controller asked the pilot what he needed from him; the pilot replied he needed a heading. The controller provided the pilot with a heading of three six zero. At 1804:47, the aircraft reached an altitude of 2700 feet ASL and a ground speed of 60 knots. The aircraft continued its right turn and began to lose altitude. The controller instructed the pilot to gain altitude if he was able to; however, the pilot did not acknowledge the instruction. The last encoded radar return for the aircraft was at 1805:26, when the aircraft was at 300 feet ASL and travelling at a ground speed of 120 knotsControl of the aircraft was lost. The aircraft collided with a power pole and trees in a wooded park area on Gabriola Island, BC, and then impacted the ground. The aircraft broke into pieces and caught fire. The 3 occupants on board received fatal injuries. As a result of being damaged in the accident, the emergency locator transmitter (Artex ME406, serial number 188-00293) did not activate.
Probable cause:
The occurrence aircraft was equipped with a BendixKing KI 825 electronic horizontal situation indicator (HSI) that was interfaced to the flight control system and GPS (global positioning system) Garmin GNS530W/430W. The HSI also supplies the autopilot system with heading information. The investigation determined that the HSI had failed briefly during operation on 22 November 2019 and a 2nd time, 3 days later, on 26 November 2019. The KI 825 HSI is electrically driven and therefore is either on and working, or off and dark with no display. The aircraft owner was in contact with an aircraft maintenance organization located at Boundary Bay Airport (CZBB), BC, and an appointment to bring the occurrence aircraft in for troubleshooting of the 2 brief HSI malfunctions had been made for 11 December 2019, i.e., the day after the accident. In total, 13 flights had been conducted after the 1st failure of the HSI. There were no journey log entries for defects with the HSI or evidence of maintenance completed. RegulationsFootnote9 require that defects that become apparent during flight operations be entered in the aircraft journey logbook, and advisory guidance in the regulatory standardsFootnote10 states that all equipment required for a particular flight or type of operation, such as the HSI in this case, be functioning correctly before flight. The HSI was destroyed in the accident and the investigation was unable to determine if it was operational on impact. Similarly, it could not be determined if the HSI was supplying the autopilot with heading information, or if the autopilot was engaged during the approach.
Final Report:

Crash of a Cessna 550 Citation II in Maraú: 5 killed

Date & Time: Nov 14, 2019 at 1417 LT
Type of aircraft:
Registration:
PT-LTJ
Flight Type:
Survivors:
Yes
Schedule:
Jundiaí – Maraú
MSN:
550-0225
YOM:
1981
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
8000
Captain / Total hours on type:
2500.00
Copilot / Total flying hours:
350
Copilot / Total hours on type:
25
Aircraft flight hours:
6978
Aircraft flight cycles:
6769
Circumstances:
The aircraft took off from the Comandante Rolim Adolfo Amaro Aerodrome (SBJD), Jundiaí - SP, to the Barra Grande Aerodrome (SIRI), Maraú - BA, at about 1458 (UTC), in order to carry out a private flight, with two pilots and eight passengers on board. Upon arriving at the destination Aerodrome, at 1717 (UTC), the aircraft made an undershoot landing on runway 11, causing the main and auxiliary landing gear to burst. The airplane moved along the runway, dragging the lower fuselage and the lower wing, leaving the runway by its left side, and stopping with the heading lagged, approximately, 210º in relation to the landing trajectory. Afterwards, there was a fire that consumed most of the aircraft. The aircraft was destroyed. One crewmember and four passengers suffered fatal injuries and the other crewmember and four passengers suffered serious injuries.
Probable cause:
Contributing factors.
- Control skills – a contributor
The inadequate performance of the controls led the aircraft to make a ramp that was lower than the ideal. This condition had the consequence of touching the ground before the runway’s threshold.
- Attention – undetermined
During the approach for landing, the commander divided his attention between the supervision of the copilot's activities and the performance of the aircraft's controls. Such circumstances may have impaired the flight management and limited the reaction time to correct the approach ramp.
- Attitude – undetermined
The report that the commander took two photographs of the runway and of the Aerodrome with his cell phone, during the wind leg, reflected an inadequate and complacent posture in relation to his primary tasks at that stage of the flight, which may have contributed to this occurrence.
- Communication – undetermined
As reported by the commander, the low tone and intensity of voice used by the copilot during the conduct of callouts, associated with the lack of use of the head phones, limited his ability to receive information, which may have affected his performance in management of the flight.
- Crew Resource Management – a contributor
The lack of proper use of CRM techniques, through the management of tasks on board, compromised the use of human resources available for the operation of the aircraft, to the point of preventing the adoption of an attitude (go-around procedure) that would avoid the accident, from the moment when the recommended parameters for a stabilized VFR approach are no longer present.
- Illusions – undetermined
It is possible that the width of the runway, narrower than the normal for the pilots involved in the accident, caused the illusion that the aircraft was higher than expected, for that distance from the thrashold 11 of SIRI, to the point of influence the judgment of the approach ramp. In addition, the fact that the pilot was surprised by the geography of the terrain (existence of dunes) and the coloring of the runway (asphalt and concrete), may have led to a false visual interpretation, which reflected in the evaluation of the parameters related to the approach ramp.
- Piloting judgment – a contributor
The commander's inadequate assessment of the aircraft's position in relation to the final approach ramp and landing runway contributed to the aircraft touching the ground before the thrashold.
- Perception – undetermined
It is possible that a decrease in the crew's situational awareness level resulted in a delayed perception that the approach to landing was destabilized and made it impossible to correct the flight parameters in a timely manner to avoid touching the ground before the runway.
- Flight planning – undetermined
It is possible that, during the preparation work for the flight, the pilots did not take into account the impossibility of using the perception and alarm system of proximity to the ground that equipped the aircraft, and the inexistence of a visual indicator system of approach ramp at the Aerodrome.
- Other / Physical sensory limitations – undetermined
The impairment of the hearing ability of the aircraft commander, coupled with the lack of the use of head phones, may have interfered with the internal communication of the flight cabin, in the critical phase of the flight.
Final Report:

Crash of a Cessna 414A Chancellor in Colonia: 1 killed

Date & Time: Oct 29, 2019 at 1058 LT
Type of aircraft:
Registration:
N959MJ
Flight Type:
Survivors:
No
Site:
Schedule:
Leesburg - Linden
MSN:
414A-0471
YOM:
1980
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
7173
Captain / Total hours on type:
1384.00
Aircraft flight hours:
7712
Circumstances:
The pilot was conducting a GPS circling instrument approach in instrument meteorological conditions to an airport with which he was familiar. During the final minute of the flight, the airplane descended to and leveled off near the minimum descent altitude (MDA) of about 600 ft mean sea level (msl). During this time, the airplane’s groundspeed slowed from about 90 knots to a low of 65 knots. In the few seconds after reaching 65 knots groundspeed, the flight track abruptly turned left off course and the airplane rapidly descended. The final radar point was recorded at 200 ft msl less than 1/10 mile from the accident site. Two home surveillance cameras captured the final few seconds of the flight. The first showed the airplane in a shallow left bank that rapidly increased until the airplane descended in a steep left bank out of camera view below a line of trees. The second video captured the final 4 seconds of the flight; the airplane entered the camera view already in a steep left bank near treetop level, and continued to roll to the left, descending out of view. Both videos showed the airplane flying below an overcast cloud ceiling, and engine noise was audible until the sound of impact. Postaccident examination of the airplane revealed no evidence of preimpact mechanical malfunctions that would have precluded normal operation. The propeller signatures, witness impact marks, audio recordings, and witness statements were all consistent with the engines producing power at the time of impact. The pilot likely encountered restricted visibility of about 2 statute miles with mist and ceilings about 700 ft msl. When the airplane deviated from the final approach course and descended below the MDA, the destination airport remained 3.5 statute miles to the northeast. Although the airplane was observed to be flying below the overcast cloud layer, given the restricted visibility, it is likely that the pilot was unable to visually identify the airport or runway environment at any point during the approach. According to airplane flight manual supplements, the stall speed likely varied from 76 to 67 knots indicated airspeed. The exact weight and balance and configuration of the airplane could not be determined. Based upon surveillance video, witness accounts, and automatic dependent surveillance-broadcast data, it is likely that, as the pilot leveled off the airplane near the MDA, the airspeed decayed below the aerodynamic stall speed, and the airplane entered an aerodynamic stall and spin from which the pilot was unable to recover. Based on a readout of the pilot’s cardiac monitoring device and autopsy findings, while the pilot had a remote history of arrhythmia, sudden incapacitation was not a factor in this accident. Autopsy findings suggested that the pilot’s traumatic injuries were not immediately fatal; soot material in both the upper and lower airways provided evidence that the pilot inhaled smoke. This autopsy evidence supports that the pilot’s elevated carboxyhemoglobin level was from smoke inhalation during the postcrash fire. In addition, there were no distress calls received from the pilot and there was no evidence found that would indicate there was an in-flight fire. Thus, carbon monoxide exposure, as determined by the carboxyhemoglobin level, was not a contributing factor to the accident.
Probable cause:
The pilot’s failure to maintain airspeed during a circling instrument approach procedure, which resulted in an exceedance of the airplane’s critical angle of attack and an aerodynamic stall and spin.
Final Report:

Crash of a Cessna 401A in Las Juntas: 6 killed

Date & Time: Oct 23, 2019 at 1800 LT
Type of aircraft:
Registration:
XB-JZF
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Durango - Acapulco
MSN:
401A-0051
YOM:
1969
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
6
Circumstances:
En route from Durango to Acapulco, the twin engine airplane crashed in unknown circumstances in the Infiernillo River, in the region of Las Juntas. The wreckage was found inverted and partially submerged in water. All six occupants were killed.