Crash of a Douglas DC-10-30C in New York

Date & Time: Nov 12, 1975 at 1310 LT
Type of aircraft:
Operator:
Registration:
N1032F
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
New York - Frankfurt - Jeddah
MSN:
46826
YOM:
1974
Flight number:
OV032
Crew on board:
11
Crew fatalities:
Pax on board:
128
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
25000
Captain / Total hours on type:
2000.00
Copilot / Total flying hours:
14500
Copilot / Total hours on type:
450
Aircraft flight hours:
8193
Circumstances:
The airplane was engaged in a positioning flight from New York to Jeddah via Frankfurt, carrying ONA employees only. The aircraft taxied to runway 13R and commenced takeoff at 13:10. Shortly after accelerating through 100 knots, but before reaching the V1 speed, a flock of birds were seen to rise from the runway. The aircraft struck many birds and the takeoff was rejected. Bird strikes had damaged the no. 3 engine's fan blades, causing rotor imbalance. Fan-booster stage blades began rubbing on the epoxy micro balloon shroud material; pulverized material then entered into the engine's HPC area, ignited and caused the compressor case to separate. A fire erupted in the right wing and no. 3 engine pylon. The aircraft couldn't be stopped on the runway. The pilot-in-command steered the aircraft off the runway onto taxiway Z at a 40 knots speed. The main undercarriage collapsed and the aircraft came to rest against the shoulder of the taxiway. The successful evacuation may be partially attributed to the fact that nearly all passengers were trained crew members.
Probable cause:
The disintegration and subsequent fire in the No.3 engine when it ingested a large number of seagulls. Following the disintegration of the engine, the aircraft failed to decelerate effectively because:
- The n°3 hydraulic system was inoperative, which caused the loss of the n°2 brake system and braking torque to be reduced 50%,
- The n°3 engine thrust reversers were inoperative,
- At least three tyres disintegrated,
- The n°3 system spoiler panels on each wing could not deploy,
- The runway surface was wet.
The following factors contributed to the accident:
- The bird-control program at John F. Kennedy airport did not effectively control the bird hazard on the airport,
- The FAA and the General Electric Company failed to consider the effects of rotor imbalance on the abradable epoxy shroud material when the engine was tested for certification.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in Blackbushe: 1 killed

Date & Time: Oct 19, 1975 at 0811 LT
Operator:
Registration:
G-BBPV
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Blackbushe - Stansted
MSN:
31-7305097
YOM:
1973
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
5391
Captain / Total hours on type:
122.00
Aircraft flight hours:
771
Circumstances:
The aircraft was en route from Blackbushe to Stansted when about three minutes after takeoff it descended to aerodrome level and flew into some trees which were obscured by fog and low cloud. The aircraft caught fire and the pilot, the sole occupant, was killed.
Probable cause:
The accident was caused by the aircraft descending into fog covered ground. No reason for this loss of height could be positively established but there is a strong possibility that the pilot's ability to fly the aircraft became impaired by the onset of symptoms associated with coronary artery disease.
Final Report:

Crash of a De Havilland DH.104 Dove off Chicago: 1 killed

Date & Time: May 20, 1975 at 1139 LT
Type of aircraft:
Operator:
Registration:
N1536V
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Chicago - Chicago
MSN:
04355
YOM:
1952
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
6650
Captain / Total hours on type:
22.00
Circumstances:
After takeoff from Chicago-Merrill C. Meigs, while climbing, both engines failed simultaneously. The pilot lost control of the airplane that stalled and crashed into Lake Michigan. The aircraft was lost and the pilot, sole on board, was killed.
Probable cause:
Complete failure of both engines due to fuel exhaustion. The following contributing factors were reported:
- Inadequate preflight preparation,
- Mismanagement of fuel,
- Fuel exhaustion,
- Failure of both engines,
- Improper operations of flight controls,
- Fuel drained total less than two gallons from each wing,
- Right wing hit first and aircraft cartwheeled.
Final Report:

Crash of a PZL-Mielec AN-2TP in Ogaryovka: 2 killed

Date & Time: Apr 28, 1975 at 0837 LT
Type of aircraft:
Operator:
Registration:
CCCP-50512
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Tula – Novomoskovsk – Moscow-Bykovo
MSN:
1G88-39
YOM:
1967
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Aircraft flight hours:
6772
Aircraft flight cycles:
12175
Circumstances:
On the leg from Tula to Novomoskovsk of a positioning flight from Tula to Moscow-Bykovo, the crew encountered an unexpected situation and attempted an emergency landing in a field near Ogaryovka (Uzlovaya district of the Tula region) when control was lost. At a speed of 140 km/h, the single engine airplane dove into the ground from a height of some 50-70 metres and was destroyed. Both pilots were killed.
Probable cause:
The cause of the accident could not be determined.

Crash of a Fairchild F27 in Baguio

Date & Time: Mar 29, 1975
Type of aircraft:
Operator:
Registration:
RP-C874
Flight Type:
Survivors:
Yes
MSN:
17
YOM:
1958
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Upon touchdown at Baguio-Loakan Airport, the right main gear collapsed. The airplane slid on runway for few meters before coming to rest. All five crew members who were completing a positioning flight were uninjured while the aircraft was damaged beyond repair.
Probable cause:
Failure of the lower lug of the oleo strut due to corrosion.

Crash of a Rockwell Grand Commander 680 into the Pacific Ocean

Date & Time: Mar 23, 1975
Operator:
Registration:
ZK-DHF
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Pago Pago - Honolulu
MSN:
680-1429-71
YOM:
1964
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was performing a positioning flight from Pago Pago to Honolulu. While approaching Honolulu from the south, the crew informed ATC about the failure of both engines and reduced his altitude in an attempt to ditch the aircraft about 100 km south of Honolulu. Both pilots were quickly rescued while the airplane sank and was lost.
Probable cause:
Double engine failure caused by a fuel exhaustion. It is believed that the fuel quantity was insufficient to cover the distance or that the crew encountered strong headwinds, increasing the fuel consumption.

Crash of a Cessna 411 in Buenos Aires: 2 killed

Date & Time: Feb 5, 1975 at 1200 LT
Type of aircraft:
Registration:
LV-LXW
Flight Phase:
Flight Type:
Survivors:
No
Site:
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
Shortly after takeoff from Buenos Aires-Ezeiza-Ministro Pistarini Airport, the twin engine airplane went out of control and crashed in a residential area located in González Catán, about 8 km northwest of the airfield. The airplane was destroyed and both occupants were killed. There were no injuries on the ground.
Probable cause:
Loss of control following an engine failure.

Crash of a Dornier DO.28A-1 in Vernier: 2 killed

Date & Time: Jan 11, 1975 at 0905 LT
Type of aircraft:
Registration:
EC-BNH
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Geneva - Sion
MSN:
3030
YOM:
1962
Location:
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
3381
Captain / Total hours on type:
1.00
Copilot / Total flying hours:
2990
Copilot / Total hours on type:
1400
Aircraft flight hours:
2530
Circumstances:
The twin engine airplane departed runway 23 at Geneva-Cointrin Airport at 0903LT. During initial climb in limited visibility due to foggy conditions, the crew encountered technical problems with instruments and the airplane completed several turns at a height between 10 and 40 meters. The crew spotted a building of nine floors and elected to make an evasive manoeuvre when the airplane stalled and crashed on a railway track located in Vernier, about three km from the airport. The accident occurred about two minutes after takeoff. At the time of the accident, the horizontal visibility was 500 meters, the vertical visibility 65 meters with a runway visual range of 750 meters for runway 23.
Probable cause:
Investigations determined that after departure, the pilots were confronted with various technical issues on several instruments. Indeed, the crew had started the flight under instrument flight rules but was forced to continue under VFR mode, which was impossible due to the lack of visibility caused by the presence of fog. The aircraft maintenance did not comply with the published requirements due to corrosion detected on the bearings of the electrical turn indicator that led to the assumption that this instrument was not working at takeoff, and probably for a long time. In addition, the artificial horizon was blocked at the time of impact and investigators believe that this instrument was partially deficient at the time of departure. The pilot-in-command accumulated 3,381 flight hours in total but had only 45 minutes of experience on this type of aircraft. The copilot had a total of 2,990 flying hours including 1,400 on type. Given the presence of fog, the pilot's lack of experience and the malfunctioning of two vital instruments, the crew should not have started the flight, especially since neither pilot had a valid license under IFR mode.
Final Report:

Crash of a Douglas C-54P Skymaster at Davis Monthan AFB

Date & Time: Jan 2, 1975 at 1358 LT
Type of aircraft:
Registration:
N39AP
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Davis-Monthan - Barstow-Daggett
MSN:
10430
YOM:
1944
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6409
Captain / Total hours on type:
20.00
Circumstances:
After takeoff from Davis Monthan AFB, the four engine airplane encountered difficulties to gain height. It struck power cables, stalled and crashed in flames. All three occupants were injured while the aircraft was destroyed.
Probable cause:
Inadequate preflight preparation on part of the crew. The following contributing factors were reported:
- Collision with wires,
- Lack of familiarity with aircraft,
- Failed to abort takeoff,
- Gust locks engaged,
- Operational supervisory personnel: inadequate supervision of flight crew,
- Unqualified person operated aircraft,
- Airport conditions,
- Checklist: failed to use,
- Downwind,
- Mechanic acting as copilot,
- 3,060 feet soft dirt strip.
Final Report:

Crash of a Boeing 727-251 near Thiells: 3 killed

Date & Time: Dec 1, 1974 at 1926 LT
Type of aircraft:
Operator:
Registration:
N274US
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
New York - Buffalo
MSN:
20296/777
YOM:
1969
Flight number:
NW6231
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
7434
Captain / Total hours on type:
1973.00
Copilot / Total flying hours:
1938
Copilot / Total hours on type:
1611
Aircraft flight hours:
10289
Circumstances:
Flight NW6231 departed New York-JFK at 19:14 for a ferry flight to Buffalo and was cleared by departure control to climb to FL140. At 19:21 the flight was cleared to climb to FL310. The aircraft began to climb 2,500 fpm at an airspeed of 305 knots. As the aircraft climbed through FL160, both the airspeed and the rate of climb began to increase. Reaching FL230, the airspeed had reached 405 knots and the rate of climb had exceeded 6,500 fpm. The overspeed warning horn sounded a little later, followed 10 seconds later by a stick shaker stall warning. The aircraft then leveled at 24800 feet with a speed of 420 knots until it turned rapidly to the right, 13 seconds later. The airplane started to descend out of control, reaching a vertical acceleration of +5g until it struck the ground in a slightly nose down and right wing-down attitude. The aircraft had descended from 24000 feet to 1090 feet in 83 seconds.
Probable cause:
The loss of control of the aircraft because the flight crew failed to recognize and correct the aircraft's high-angle-of-attack, low-speed stall and its descending spiral. The stall was precipitated by the flight crew's improper reaction to erroneous airspeed and Mach indications which had resulted from a blockage of the pitot heads by atmospheric icing. Contrary to standard operational procedures, the flight crew had not activated the pitot head heaters.
Final Report: