Crash of a Fairchild C-82A Packet near Beaver

Date & Time: Jan 16, 1965 at 1705 LT
Type of aircraft:
Operator:
Registration:
N208M
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
10163
YOM:
1945
Location:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
While on a positioning flight to Fairbanks, both engines failed simultaneously. Unable to maintain the prescribed altitude, the crew decided to attempt an emergency landing. The airplane crash landed in a snow covered area located about 100 miles north of Fairbanks, near Beaver. All three crew members were rescued while the aircraft was damaged beyond repair.
Probable cause:
Both engines failed en route due to icing. It was determined that weather conditions were conducive to carburetor icing in flight. For unknown reason, the crew failed to use the deicing-anti-icing equipment in flight. The crew received a report of enroute sky conditions from the airline but did not receive any weather briefing.
Final Report:

Crash of a Boeing KC-135A-BN Stratotanker in Wichita: 30 killed

Date & Time: Jan 16, 1965 at 1030 LT
Type of aircraft:
Operator:
Registration:
57-1442
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
McConnell - McConnell
MSN:
17513
YOM:
1958
Flight number:
501
Location:
Crew on board:
7
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
30
Circumstances:
Shortly after takeoff from McConnell AFB, while climbing to a height of 500-700 feet, the captain sent a first distress call while the aircraft experienced a large amount of yaw. The crew elected to return for a safe landing and began to dump large quantities of fuel from the aircraft's refueling tanks. Shortly after this, the aircraft made a hard bank to the left, and began to enter a roll. Out of control, the airplane dove into the ground and crashed at the intersection of Piatt and 20th Street, just three minutes after takeoff, some 7 miles north-northwest of the airbase. The aerial refueling aircraft was loaded with 31,000 US gallons of jet fuel and the crash resulted in a large explosion and subsequent fire, which engulfed dozens of homes. The accident killed all seven crew members on board the aircraft and 23 people on the ground. In addition, 27 other people on the ground sustained injuries, three of which were serious. It was reported that the crew entry door was jettisoned and a B-52 Stratofortress bomber, which took off prior to the KC-135, may have blown a detached drag chute from an F-105 Thunderchief against the departing aircraft.
Probable cause:
Ten months after the accident, the U.S. Air Force issued an official accident report which stated that the crash was caused by "a rudder control system malfunction" which was impossible for the crew to overcome.

Crash of a Lockheed 18 LearStar I in Detroit: 2 killed

Date & Time: Jan 14, 1965 at 1208 LT
Type of aircraft:
Operator:
Registration:
N512V
Flight Type:
Survivors:
No
Schedule:
Detroit - Detroit
MSN:
2580
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
11008
Captain / Total hours on type:
3870.00
Aircraft flight hours:
7877
Circumstances:
The crew was completing a local training flight at Detroit-Willow Run (Ypsilanti) Airport. On final approach to runway 05R, the instructor decided to make a go around. The crew increased engine power, raised the landing gear and deployed the flaps when the airplane stalled and crashed in a field and burst into flames. Both pilots were killed.
Probable cause:
Loss of control caused by the failure of a flap cable.
Final Report:

Crash of a Beechcraft C18S in Quitman

Date & Time: Jan 11, 1965 at 1630 LT
Type of aircraft:
Registration:
N5881C
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
8704
YOM:
1945
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
18000
Captain / Total hours on type:
145.00
Circumstances:
While in cruising altitude, both engines failed simultaneously. The pilot informed ATC about his situation and reduced his altitude in an attempt to make an emergency landing. The airplane belly landed in a field located in Quitman and slid for several yards before coming to rest. The pilot was slightly injured and the aircraft was damaged beyond repair.
Probable cause:
In-flight failure of both engines for undetermined reason.
Final Report:

Crash of a De Havilland DHC-2 Beaver in Pile Bay: 2 killed

Date & Time: Jan 11, 1965 at 1409 LT
Type of aircraft:
Operator:
Registration:
N4799C
Flight Phase:
Survivors:
No
Site:
MSN:
1292
YOM:
1959
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
253
Captain / Total hours on type:
31.00
Circumstances:
En route, weather conditions deteriorated and while cruising in rain falls, the pilot lost his sens of orientation when the single engine airplane struck the slope of a mountain located near Pile Bay. The aircraft was destroyed by impact forces and a post crash fire and both occupants were killed. The wreckage was found a day later.
Probable cause:
The pilot continued under VFR mode into adverse weather conditions. It is reported the pilot exercised poor judgment and that the weather forecast was incorrect.
Final Report:

Crash of a Douglas C-133A-5-DL Cargomaster off Wake Island: 6 killed

Date & Time: Jan 11, 1965
Type of aircraft:
Operator:
Registration:
54-0140
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Wake Island - Kadena
MSN:
44710
YOM:
1954
Crew on board:
6
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
6
Circumstances:
Shortly after a night takeoff from Wake Island, while climbing to a height of 500 feet, the airplane went out of control and crashed into the sea some 4,5 km off shore. All six crew members were killed.

Crash of a Boeing KC-135A-BN Stratotanker at Loring AFB: 4 killed

Date & Time: Jan 4, 1965 at 0900 LT
Type of aircraft:
Operator:
Registration:
61-0265
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Loring - Loring
MSN:
18172
YOM:
1961
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
The aircraft departed Loring AFB at 0900LT for a six hour training mission. Shortly after takeoff, while in initial climb, the airplane suffered severe turbulences and the number three engine drag brace failed due to a missing nut. The engine swung up in front of the wing, causing a severe roll to the left. The aggressive control inputs in an attempt to level the aircraft resulted in both the #3 and #4 engines separating from the wing. The aircraft then entered a 90° right bank, plunges into the earth and crashed in a wooded area located 2,4 miles north of the runway. The aircraft was destroyed and all four crew members were killed.
Crew:
Cpt Kenneth Gomes, pilot,
Cpt Matthew Ramstsch, copilot,
1st Lt John McCarron, navigator,
S/Sgt Jimmy Tardie, boom operator.
Probable cause:
Loss of control after the number three engine drag brace failed due to a missing nut.

Crash of a Beechcraft E18S near Henderson: 4 killed

Date & Time: Jan 3, 1965 at 1445 LT
Type of aircraft:
Registration:
N208UB
Flight Phase:
Flight Type:
Survivors:
No
MSN:
BA-331
YOM:
1958
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
4341
Captain / Total hours on type:
174.00
Circumstances:
While in cruising altitude, the propeller blades on the left engine detached. Control was lost and the airplane dove into the ground and crashed in a lake located near Henderson. The aircraft was destroyed and all four occupants were killed.
Probable cause:
The left engine tearaway following the in-flight separation of the propeller blade due to fatigue fracture.
Final Report:

Crash of an Aero Commander 520 off Miami Beach

Date & Time: Dec 30, 1964 at 1700 LT
Operator:
Registration:
N4120B
Flight Type:
Survivors:
Yes
Schedule:
Miami - Miami
MSN:
520-99
YOM:
1953
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
9535
Captain / Total hours on type:
50.00
Circumstances:
The pilot, sole occupant, was completing a local test flight out from Miami. Following an uneventful flight, the pilot was returning to Miami when both engines stopped simultaneously. Unable to maintain the requested altitude, he attempted to ditch the aircraft off Miami Beach. The airplane crashed into the sea at 1700LT and sank by a depth of few dozen feet. The pilot was rescued.
Probable cause:
As the airplane was not recovered, investigations were unable to determine with certainty the cause of the double engine failure.
Final Report:

Crash of a Curtiss C-46A-45-CU Commando in Detroit: 4 killed

Date & Time: Dec 30, 1964 at 0214 LT
Type of aircraft:
Operator:
Registration:
N608Z
Flight Type:
Survivors:
No
Schedule:
Cleveland – Detroit – Denver
MSN:
30328
YOM:
1944
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
21400
Captain / Total hours on type:
7520.00
Aircraft flight hours:
7385
Circumstances:
The C-46 Commando had been cleared for a runway 03L ILS approach at Detroit in poor weather (sky obscured, visibility 1 mile, light drizzle). During the approach, at 1,5 miles right of the ILS course and 1 mile NE of the Outer Marker, the aircraft suddenly entered a 45° bank left turn. The bank angle exceeded 60° as the plane crossed the localizer course from left to right. The aircraft struck several 84 feet tall trees in an 8° nose down and 30° right bank attitude, struck the ground and disintegrated. In the investigation an incapacitation of the captain was considered, but not supported by postmortem examination.
Probable cause:
Loss of control during night instrument approach in adverse weather for an undetermined reason.
Final Report: