Crash of a Noorduyn Norseman near Mendi: 1 killed

Date & Time: Jul 8, 1958
Type of aircraft:
Operator:
Registration:
VH-GSA
Flight Type:
Survivors:
No
Site:
Schedule:
Minj – Mendi
MSN:
250
YOM:
1943
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The pilot, sole on board, was performing a cargo flight from Minj to Mendi, carrying a load of cement bags. While approaching Mendi, weather conditions deteriorated. The single engine aircraft went through a valley in thunderstorm activity when it struck the slope of a mountain and disintegrated on impact. The pilot was killed.

Crash of a Lockheed L-414-56 Hudson IIIA off Lae: 3 killed

Date & Time: Jun 8, 1958
Type of aircraft:
Operator:
Registration:
VH-AGG
Flight Type:
Survivors:
No
Schedule:
Lae - Wewak - Lae
MSN:
414-6486
YOM:
1942
Location:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
Carrying one pilot, a navigator and a photographer, the aircraft departed Lae on a photographic survey flight over the Wewak area, but conditions proved unfavourable for photography and it was decided to return to Lae. Lae tower was called five minutes before arrival and landing instructions were passed, in which it was advised that Runway 32 was to be used, the wind velocity being 300 degrees at 15 knots with gusts to 20 knots. Just before turning on to base leg the aircraft was cleared to do a practice asymmetric landing, but was warned to expect turbulence on the final approach. This was acknowledged by the aircraft. Witnesses agree that the aircraft was very low at the time of entering the final approach from a right-hand base leg with the left-hand propeller feathered. They also agreed that, following what sounded to be a marked increase in the power setting when 300 yards from the end of the strip, the aircraft rolled to the left and dived into the water in a partly inverted attitude. All three occupants perished.
Crew:
Allen Motteram, pilot,
Patrick Murphy, navigator,
Passenger:
Gordon Murrell, photographer.

Crash of a Consolidated PBY-5A Catalina in the Kikori River

Date & Time: Jun 16, 1957
Type of aircraft:
Registration:
VH-WWB
Flight Type:
Survivors:
Yes
MSN:
1830
YOM:
1944
Location:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Struck a submerged obstacle while landing on Kikori River. The aircraft quickly sank and was lost. Both crew members were rescued.

Crash of a Junkers JU.52/3mg in Wau

Date & Time: Mar 21, 1957
Type of aircraft:
Operator:
Registration:
VH-BUW
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Wau – Lae
MSN:
641375
YOM:
1943
Location:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
GSA pilot Peter Manser was making a down-hill takeoff on the sloping strip, carrying a heavy load of sawn timber. Just before becoming airborne the port engine suddenly lost all power, causing the aircraft to swing violently to the left and roll towards the Qantas terminal building and freight shed. The Qantas agent Mrs. Ivy Crawford saw it approaching and ran through the passenger room out on to the airfield and jumped over an embankment as the aircraft struck the building. The port wing sliced through the wooden structure, the roof collapsing as the Junkers kept rolling on to a road, tearing off its rear fuselage before Manser could bring it to a stop. The fuselage was broken into three sections and 12 feet was smashed off the port wing.
Source:
http://www.goodall.com.au/australian-aviation/junkers ju52/junkersju52.html
Probable cause:
The accident was probably caused by a loss of power, for reasons undetermined, at a critical stage of the takeoff.

Crash of a De Havilland DH.84 Dragon off Madang

Date & Time: Oct 29, 1955
Type of aircraft:
Registration:
VH-AOE
Flight Phase:
Survivors:
Yes
MSN:
2058
YOM:
1943
Location:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The twin engine aircraft was engaged in a local sightseeing flight, carrying two European tourists and one pilot. Shortly after takeoff, while climbing, both engines encountered problems. The aircraft stalled and crashed in the harbor of Madang and came to rest upside down. All three occupants were quickly rescued and uninjured. An attempt to recover the airplane was made on November 8 but it broke in two when it went out of water.
Probable cause:
It was determined that fuel was contaminated by water, causing both engine to malfunction.

Crash of a Noorduyn Norseman in Minj

Date & Time: Aug 23, 1955
Type of aircraft:
Operator:
Registration:
VH-BNT
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Minj – Mendi
MSN:
181
YOM:
1943
Location:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Shortly after takeoff from Minj Airstrip, while in initial climb, the engine failed. The aircraft stalled and crashed in a field. The pilot was injured and the aircraft was destroyed.
Probable cause:
Engine failure caused by fuel exhaustion.

Crash of an Avro 652A Anson I in Bereina

Date & Time: Dec 22, 1954
Type of aircraft:
Operator:
Registration:
VH-BMN
Survivors:
Yes
Schedule:
Port Moresby – Bereina
Location:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
13
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The twin engine aircraft landed hard, causing a wing to touch the ground and to be sheared off. Out of control, the airplane veered off runway and came to rest. All 15 occupants were injured while the aircraft was damaged beyond repair.

Crash of an Avro 652A Anson I in Wabag

Date & Time: Dec 18, 1954
Type of aircraft:
Operator:
Registration:
VH-BMD
Survivors:
Yes
Schedule:
Port Moresby – Wabag
Location:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
13
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
A undercarriage collapsed on landing at Wabag Airstrip. The twin engine aircraft went out of control, veered off runway and came to rest. There were no casualties but the aircraft was damaged beyond repair.
Probable cause:
Undercarriage collapsed on landing.

Crash of a De Havilland DH.84 Dragon in Heyfield

Date & Time: Aug 9, 1954
Type of aircraft:
Operator:
Registration:
VH-AOP
Flight Phase:
Survivors:
Yes
MSN:
2010
YOM:
1943
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Apparently, the pilot encountered technical problems with the brakes and decided to abandon the takeoff procedure. Unable to stop within the remaining distance, the twin engine aircraft overran and crashed in flames in a deep ravine. All eight occupants were injured and the aircraft was destroyed by fire.

Crash of a De Havilland DH.83 Fox Moth in Kokoda

Date & Time: Nov 17, 1953
Operator:
Registration:
VH-UTY
Flight Type:
Survivors:
Yes
Schedule:
Port Moresby – Kokoda
MSN:
4041
YOM:
1933
Location:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The single engine airplane was performing a cargo flight from Port Moresby to Kokoda, carrying mail, freezer meat, bread, Christmas parcels and general cargo. The pilot Frank Goosens remembers: "I had to circle and circle to climb over the Gap. I jumped over the ridge to get over Lake Myola, and had to tackle one more ridge. Instead of getting an updraft, I was in a downdraft, tried to turn back and in doing so, dodging around the hills, I fell into a spin, caught not get out and wrapped the Fox Moth around a tree. The plane was a wreck but apart from a bleeding forehead I was unscratched. Everything in front of the pilot's cabin was crushed. The engine was pushed right back and must have just missed my head." Frank Goosens attempted to walk out of the jungle on the Kokoda Trail, but after being seen by a searching DC-3, returned to the wreck and slept in the cockpit for two nights while waiting the arrival of the ground search party.
Probable cause:
Caught by downdraft on approach.