Ground fire of a Boeing 737-809 in Naha

Date & Time: Aug 20, 2007 at 1033 LT
Type of aircraft:
Operator:
Registration:
B-18616
Flight Phase:
Survivors:
Yes
Schedule:
Taipei - Naha
MSN:
30175/1182
YOM:
2002
Flight number:
CI120
Location:
Country:
Region:
Crew on board:
8
Crew fatalities:
Pax on board:
157
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7941
Captain / Total hours on type:
3823.00
Copilot / Total flying hours:
890
Copilot / Total hours on type:
182
Aircraft flight hours:
13664
Circumstances:
The aircraft departed Taipei-Taoyuan Airport at 0814LT on a schedule service to Naha with 157 passengers and a crew of 8. Following an uneventful flight, the crew was cleared to land on runway 18 and vacated via taxiway E6 then A5. After being stopped at spot 41, engines were shot down when a fire broke out somewhere in an area aft of the right engine and spread to the right wing leading edge near the n°5 slat and the apron surface below the right engine. All 165 occupants evacuated safely while the aircraft was totally destroyed by fire.
Probable cause:
It is considered highly probable that this accident occurred through the following causal chain: When the Aircraft retracted the slats after landing at Naha Airport, the track can that housed the inboard main track of the No. 5 slat on the right wing was punctured, creating a hole. Fuel leaked out through the hole, reaching the outside of the wing. A fire started when the leaked fuel came into contact with high-temperature areas on the right engine after the Aircraft stopped in its assigned spot, and the Aircraft burned out after several explosions. With regard to the cause of the puncture in the track can, it is certain that the downstop assembly having detached from the aft end of the above-mentioned inboard main track fell off into the track can, and when the slat was retracted, the assembly was pressed by the track against the track can and punctured it. With regard to the cause of the detachment of the downstop assembly, it is considered highly probable that during the maintenance works for preventing the nut from loosening, which the Company carried out on the downstop assembly about one and a half months prior to the accident based on the Service Letter from the manufacturer of the Aircraft, the washer on the nut side of the assembly fell off, following which the downstop on the nut side of the assembly fell off and then the downstop assembly eventually fell off the track. It is considered highly probable that a factor contributing to the detachment of the downstop assembly was the design of the downstop assembly, which was unable to prevent the assembly from falling off if the washer is not installed. With regard to the detachment of the washer, it is considered probable that the following factors contributed to this: Despite the fact that the nut was in a location difficult to access during the maintenance works, neither the manufacturer of the Aircraft nor the Company had paid sufficient attention to this when preparing the Service Letter and Engineering Order job card, respectively. Also, neither the maintenance operator nor the job supervisor reported the difficulty of the job to the one who had ordered the job.
Final Report:

Crash of a Mitsubishi MU-2S Marquise on Mt Mikagura: 4 killed

Date & Time: Apr 14, 2005 at 1350 LT
Type of aircraft:
Operator:
Registration:
73-3229
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Niigata - Niigata
MSN:
929
YOM:
1974
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
Few minutes after takeoff from Niigata Airport, while flying in good weather conditions, the twin engine aircraft crashed on Mt Mikagura located about 55 km southeast of Niigata. All four crew members were killed. They were engaged in a local training mission.

Crash of a Learjet U-36A at Iwakuni AFB: 4 killed

Date & Time: May 21, 2003 at 1125 LT
Type of aircraft:
Operator:
Registration:
9202
Flight Type:
Survivors:
No
Schedule:
Iwakuni - Iwakuni
MSN:
36-056
YOM:
1988
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
The crew departed Iwakuni AFB at 0900LT on a training mission over the Sea of Japan. At 1045LT, the aircraft returned to Iwakuni and the crew completed several touch-and-go manoeuvres on runway 02. During one of these procedures, the aircraft went out of control upon touchdown and crashed beside the runway, bursting into flames. All four crew members were killed.

Crash of a Rockwell Gulfstream 695 Jetprop 980 in Ogawa: 2 killed

Date & Time: Mar 24, 2003 at 1052 LT
Operator:
Registration:
JA8604
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Tokyo-Chōfu - Tokyo-Chōfu
MSN:
695-95044
YOM:
1980
Location:
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
11473
Captain / Total hours on type:
300.00
Aircraft flight hours:
6029
Circumstances:
The aircraft departed Chofu Aerodrome at 10:26 (JST) with the captain and a mechanic on board for a company test flight prior to an airworthiness certification inspection. During the flight at around 10:52, the aircraft crashed into woods at Nishine, Kamiose, Ogawa, Naka County, Ibaraki Prefecture. The two persons on board the aircraft, the captain and the mechanic, both sustained fatal injuries. A fire broke out and the aircraft was destroyed.
Probable cause:
It is estimated that in this accident, while the aircraft was on a company test flight prior to an airworthiness certification inspection, it entered spin and because it was unable to recover, it crashed, destroying the fuselage and killing the captain and the passenger. Because the left engine’s oil tank cap had not been normally locked, abnormal engine oil temperature and pressure occurred, and it is estimated that the aircraft’s airspeed decreased to near the stall speed. The captain increased power on the right engine to regain airspeed, which induced a yawing moment. It is considered possible that the aircraft then entered a spin because either it was uncontrollable due to being below the minimum control speed and safe one engine inoperative speed, or the captain had been incapacitated by hypoxia and was unable to cope with the loss of airspeed.
The following are considered possible reasons as to why the aircraft did not recover from the spin; however, the precise cause could not be clarified.
① Because the aircraft type is prohibited from spins, the captain could not have been practiced in spin recovery for the aircraft.
② The spin developed without being arrested in the early stages, until flight conditions exceeding the aircraft’s design limits so that the aircraft could not be recovered by normal control forces.
③ The aircraft was in a state of spinning without a reduction of engine power, which made recovery difficult.
④ The captain had been incapacitated.
Final Report:

Crash of a Boeing 767-281 in Shimoji-shima

Date & Time: Jun 26, 2002 at 1254 LT
Type of aircraft:
Operator:
Registration:
JA8254
Flight Type:
Survivors:
Yes
Schedule:
Shimoji-shima - Shimoji-shima
MSN:
23433
YOM:
1987
Flight number:
NH8254
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
10375
Captain / Total hours on type:
6654.00
Copilot / Total flying hours:
259
Copilot / Total hours on type:
5
Aircraft flight hours:
35347
Circumstances:
On June 26, 2002, a Boeing 767-200 of All Nippon Airways, registration JA8254, took off from Shimoji-Shima Airport at around 11:32 on a flight for takeoff and landing training. The flight plan of the aircraft submitted to the Shimoji-Shima Airport Office of the Japan Civil Aviation Bureau (CAB) was as follows: FLIGHT RULES: VFR, AERODROME of DEPARTURE: Shimoji-Shima Airport, TIME: 11:20, CRUISING SPEED: 250kt, LEVEL: VFR, ROUTE: Traffic Pattern, DESTINATION AERODROME: Shimoji-Shima Airport, FLIGHT PURPOSE: Training Flight, TOTAL EET: 1 hour 40 minutes, ENDURANCE: 6 hrs 32 minutes, PERSONS ON BOARD: 3. The three persons on board were in the cockpit at the time of the accident: A pilot undergoing training for promotion to First Officer (Trainee Pilot-A) occupying the left pilot’s seat, the Captain acting as instructor occupying the right pilot’s seat, and another pilot undergoing training for promotion to First Officer (Trainee Pilot-B) occupying the left observer’s seat. First, Trainee Pilot-B made seven landings on runway 17 from the left pilot’s seat, including two landings with one engine simulated inoperative, and a go-around with both engines operative. He then changed places with Trainee Pilot-A. At around that time, the wind direction changed from the south to the west, and the aerodrome control tower instructed a change to runway 35. Trainee Pilot-A then made two landings on runway 35 with both engines operative, and training then switched to landing with one engine simulated inoperative. The first landing was made with the left engine simulated inoperative. After that, during a landing with the right engine simulated inoperative, the touchdown was late and Trainee Pilot-A attempted to go-around with go-around thrust on the left engine only. A few seconds later the instructor increased power on the right engine to go-around thrust, but at that time even though the left engine thrust had started to increase the right engine was still at minimum idle thrust. As a result, a thrust imbalance occurred between the left and right engines while right rudder was
being applied, and the aircraft rolled and yawed to the right (East). Although Trainee Pilot-A and the instructor attempted to correct the attitude changes, the aircraft veered off the runway into a grass field on east side of the runway and came to a stop around 1,990m from the point it had first touched down. The accident occurred at runway 35 of Shimoji-Shima Airport at around 12:54.
Probable cause:
It is estimated that the accident was caused as follows:
The aircraft was being operated on a training flight at Shimoji-Shima Airport, and was making a one-engine-out touch-and-go landing with the right engine simulated inoperative. The touchdown was late and beyond the normal aim point, and on the direction of the instructor, the trainee pilot attempted to go around on only the left engine. However, the trainee mishandled the aircraft, and then, seeing the instructor advance the right engine’s thrust lever, he applied right rudder pedal mechanically. This coincided with an increase in the rotation speed of the left engine, and the aircraft’s attitude suddenly changed towards the right. Because the trainee pilot could not fully correct this and the instructor was late in taking over control, the aircraft veered off the east side of the runway into a grass area and was damaged. Moreover, it is estimated that the following causal factors contributed to the accident:
1) The instructor did not take over when he directed the trainee to go around, or at an earlier stage, because he thought to allow the trainee pilot to handle the aircraft as much as possible, and because he did not sufficiently recognize that a go-around with one-engine simulated inoperative is a difficult maneuver for an inexperienced pilot.
2) Regarding the instructor’s intent to allow the trainee pilot to handle the aircraft as much as possible, the company’s instructional guidelines contained statements meaning that a judgment to go around should be made by the trainee pilot, and that during simulated one-engine-out touch-and-go training landings, the go-around after landing should continue with one engine simulated inoperative.
3) Regarding the instructor’s insufficient recognition of the difficulty of a go-around with one engine simulated inoperative for an inexperienced pilot, the instructor had not been trained to deal with the situation encountered in the accident, and the company’s regulations and manuals did not describe considerations on the difficulty of executing a go-around with one-engine simulated inoperative for an inexperienced pilot or on the effects of the wind on such maneuvers.
4) Regarding the delay in the instructor taking over control of the aircraft, the instructor was not following with his hands on the control wheel and was not in a position to take over immediately if necessary, and when the instructor had changed from being a simulator instructor to a flight instructor, he had not received sufficient training on cautionary matters regarding training in actual aircraft.
Final Report:

Crash of a Kawasaki C-1A off Shimano: 8 killed

Date & Time: Jun 27, 2000
Type of aircraft:
Operator:
Registration:
88-1027
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Yonago AFB - Yonago AFB
MSN:
8027
Location:
Country:
Region:
Crew on board:
8
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
8
Circumstances:
The crew (four pilots and four technicians) departed Yonago-Miho AFB on a post maintenance local flight. After several circuits, while in cruising altitude, the aircraft entered an uncontrolled descent and crashed in the sea off Shimano. All eight occupants were killed.

Crash of a NAMC YS-11A-213 in Sapporo

Date & Time: Feb 16, 2000 at 1243 LT
Type of aircraft:
Operator:
Registration:
JA8727
Survivors:
Yes
Schedule:
Hakodate - Sapporo
MSN:
2095
YOM:
1969
Flight number:
EL354
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
37
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On approach to Sapporo-Okadama, the aircraft was too high on the glide and approached at an excessive speed. It landed too far down a snow covered runway and was unable to stop within the remaining distance. It overran, collided with snow bank and came to rest. All 41 occupants escaped uninjured while the aircraft was damaged beyond repair.
Probable cause:
Wrong approach configuration on part of the crew who completed the approach at an excessive speed and above the glide, causing the aircraft to land too far down the runway. The following findings were identified:
- The aircraft speed was 23 knots higher than the reference speed above threshold,
- Excessive speed upon touchdown,
- The braking action was reduced because the runway surface was contaminated with snow,
- The aircraft was unable to stop within the remaining distance,
- The crew failed to initiate a go-around procedure while the landing was obviously missed,
- Marginal weather conditions,
- Poor crew coordination,
- Poor airspeed monitoring on part of the flying crew.

Crash of a Douglas DC-10-30 in Fukuoka: 3 killed

Date & Time: Jun 13, 1996 at 1208 LT
Type of aircraft:
Operator:
Registration:
PK-GIE
Flight Phase:
Survivors:
Yes
Schedule:
Fukuoka – Denpasar – Jakarta
MSN:
46685
YOM:
1979
Flight number:
GA865
Country:
Region:
Crew on board:
15
Crew fatalities:
Pax on board:
260
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
10263
Captain / Total hours on type:
2641.00
Copilot / Total flying hours:
3910
Copilot / Total hours on type:
1437
Aircraft flight hours:
46325
Circumstances:
During the takeoff roll at Fukuoka-Itazuke Airport runway 16, at a speed of 158 knots, the captain started the rotation. During initial climb, at a height of about 3 metres, the right engine suffered a loss of power after a fan blade located on the 1st stage of the high pressure compressor disk separated. The N1 dropped to 23,7% and five seconds later, the flight engineer informed the crew about the failure of the engine n°1. The captain decided to abort the takeoff and landed back on runway. The aircraft contacted ground with a vertical acceleration of 2,1 g then thrust reversers were deployed and ground spoilers were extended. Unable to stop within the remaining distance, the aircraft overran, crossed a road, skidded for about 620 metres before coming to rest in an open field, bursting into flames. Three passengers were killed.
Probable cause:
Although the CAS was well in excess of V1 and the aircraft had already lifted off from the runway, the takeoff was aborted. Consequently the aircraft departed the end of the runway, came to rest and caught fire. It is estimated that contributing to the rejection of the takeoff under this circumstance was the fact that the CAP's judgement in the event of the engine failure was inadequate. Investigation revealed that the turbine blade that failed, had operated for 30913 hours and 6182 cycles. General Electric had advised customers to discard blades after about 6000 cycles.
Final Report:

Crash of a Socata TBM-700 in Kushiro: 6 killed

Date & Time: Apr 26, 1996 at 1108 LT
Type of aircraft:
Operator:
Registration:
JA8896
Survivors:
No
Schedule:
Sapporo - Kushiro
MSN:
68
YOM:
1993
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
6
Circumstances:
The pilot encountered poor visibility on approach to Kushiro Airport due to foggy conditions. Too low on final, the single engine aircraft collided with elements of the ILS systems and crashed 200 metres short of runway 17, bursting into flames. The aircraft was destroyed by a post crash fire and all six occupants were killed.

Crash of a Britten-Norman BN-2B-20 Islander near Kawatana

Date & Time: Feb 9, 1996 at 1322 LT
Type of aircraft:
Operator:
Registration:
JA5322
Flight Phase:
Flight Type:
Survivors:
Yes
Site:
Schedule:
Fukuoka - Nagasaki
MSN:
2285
YOM:
1990
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
While cruising at a relative low altitude under VFR mode in IMC conditions (snow falls), the crew saw a mountain. To avoid a collision, the pilot increased engine power but the aircraft struck trees and crashed in a wooded area located on the Takami Peak, near Kawatana. Both pilots were injured and the aircraft was destroyed.