Crash of a Shin Meiwa US-1A off Oki Island: 10 killed

Date & Time: Feb 21, 1995
Type of aircraft:
Operator:
Registration:
9080
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
2010
Country:
Region:
Crew on board:
12
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
10
Circumstances:
Crashed in unknown circumstances in the sea few hundred metres off Oki Island while completing a training flight. Two crew members were rescued while 10 others were killed.

Crash of a Mitsubishi MU-2S Marquise off Hamamatsu: 4 killed

Date & Time: Oct 19, 1994
Type of aircraft:
Operator:
Registration:
53-3219
Flight Phase:
Flight Type:
Survivors:
No
MSN:
919
YOM:
1974
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
4
Circumstances:
The crew was engaged in a post maintenance test flight. En route, the copilot informed ATC about technical problems when control was lost. The aircraft entered a dive and crashed in the sea off Hamamatsu. All four crew members were killed.

Crash of an Airbus A300-622R in Nagoya: 264 killed

Date & Time: Apr 26, 1994 at 2015 LT
Type of aircraft:
Operator:
Registration:
B-1816
Survivors:
Yes
Schedule:
Taipei - Nagoya
MSN:
580
YOM:
1990
Flight number:
CI140
Country:
Region:
Crew on board:
15
Crew fatalities:
Pax on board:
256
Pax fatalities:
Other fatalities:
Total fatalities:
264
Captain / Total flying hours:
8340
Captain / Total hours on type:
1350.00
Copilot / Total flying hours:
1624
Copilot / Total hours on type:
1033
Aircraft flight hours:
8550
Aircraft flight cycles:
3910
Circumstances:
China Airlines' Flight 140 (from Taipei International Airport to Nagoya Airport), B-1816, took off from Taipei International Airport at 0853 UTC (1753 JST) on April 26, 1994 (hereinafter all times shown are Coordinated Universal Time, unless otherwise specified), canying a total of 271 persons consisting of 2 flight crew members, 13 cabin crew members and 256 passengers (including 2 infants). The flight plan of the aircraft, which had been filed to the Taiwanese civil aviation authorities, Zhongzheng International Airport Office, was as follows:
Flight rule: IFR, Aerodrome of departure: Taipei International Airport, Destination Aerodrome: Nagoya Airport, Cruising speed: 465 knots, Level: FL330, Route: A1 SUCJAKAL-KE-SIV-XMC, total estimated enroute time: 2 hours and 18 minutes, Alternate Aerodrome: Tokyo International Airport.
DFDR shows that the aircraft reached FL330 about 0914 and continued its course toward Nagoya Airport in accordance with its flight plan.
DFDR and CVR show that its flight history during approximately 30 minutes prior to the accident progressed as follows:
The aircraft which was controlled by the FIO, while cruising at FL330 was cleared at 1047:35 to descend to FL210 by the Tokyo Area Control Center and commenced descent. For about 25 minutes from a few minutes before the aircraft began its descent, the CAP briefed the F/O on approach and landing.
At 1058:18, communication was established with Nagoya Approach Control. The aircraft began to descend and decreased its speed gradually, in accordance with the clearances given by Approach Control.
At 1104:03, the aircraft was instructed by Nagoya Approach control to make a left turn to a heading of 010". Later, at 1107:14, the aircraft was cleared for ILS approach to Runway 34 and was instructed to contact Nagoya Tower. After the aircraft took off from Taipei International Airport, from 0854 when the aircraft had passed 1,000 feet pressure altitude, AP No.2 was engaged during climb, cruise and descent.
At 1107:22, when the aircraft was in the initial phase of approach to Nagoya airport, AP No. 1 was also engaged. Later, at 1111:36, both AP No. 1 and 2 were disengaged by the FIO. The aircraft passed the outer marker at 1112:19, and at 1113:39, received landing clearance from Nagoya Tower. At this time, the aircraft was reported of winds 290 degrees at 6 knots. Under manual control, the aircraft continued normal LS approach.
At 1114:05, however, while crossing approximately 1,070 feet pressure altitude, the F/O inadvertently triggered the GO lever. As a result the aircraft shifted into GO AROUND mode leading to an increase in thrust. The CAP cautioned the FIO that he had triggered the GO lever and instructed him, saying "disengage it". The aircraft leveled off for about 15 seconds at approximately 1,040 feet pressure altitude (at a point some 5.5 km from the Runway). The CAP instructed the F/O to correct the descent path which had become too high. The F/O acknowledged this. Following the instruction, the F/O applied nose down elevator input to adjust its descent path, and consequently the aircraft gradually regained its normal glide path. During this period, the CAP cautioned to the FIO twice that the aircraft was in GO AROUND Mode.
At 1114: 18, both AP No.2 and No. 1 were engaged almost simultaneously when the aircraft was flying at approximately 1,040 feet pressure altitude, a point 1.2 dots above the glide slope. Both APs were used for the next 30 seconds. There is no definite record in the CVR of either the crew expressing their intention or calling out to use the AP. For approximately 18 seconds after the AP was engaged, the THS gradually moved from -5.3" to -12.3", which is close to the maximum nose-up limit. The THS remained at -12.3" until 1115: 1 1. During this period, the elevator was continually moved in the nose-down direction. In this condition, the aircraft continued its approach, and at 1115:02, when it was passing about 510 feet pressure altitude (at a point approximately 1.8 km from the runway), the CAP, who had been informed by the FIO that the THR had been latched, told the FIO that he would take over the controls. Around this time, the THR levers had moved forward greatly, increasing EPR from about 1.0 to more than 1.5. Immediately afterwards, however, the THR levers were retarded, decreasing EPR to 1.3. In addition, the elevator was moved close to its nose-down limit when the CAP took the controls.
At 1115:11, immediately after the CAP called out "Go lever", the THR levers were moved forward greatly once again, increasing EPR to more than 1.6. The aircraft therefore began to climb steeply. The F/O reported to Nagoya Tower that the aircraft would go around, and Nagoya Tower acknowledged this. The aircraft started climbing steeply, AOA increased sharply and CAS decreased rapidly. During this period, the TI-IS decreased from -12.3" to -7.4", and SLATS/FLAPS were retracted from 30/40 to 15/15 after the F/O reported "Go Around to Nagoya Tower.
At 1115:17, the GPWS activated Mode 5 warning "Glide Slope" once, and at 1115:25, the stall warning sounded for approximately 2 seconds.
At 1115:31, after reaching about 1,730 feet pressure altitude (about 1,790 feet radio altitude), the aircraft lowered its nose and began to dive.
At 1115:37, the GPWS activated Mode 2 warning "Terrain, Terrain" once, and the stall warning sounded from 1115:40 to the time of crash.
At about 1115:45, the aircraft crashed into the landing zone close to the El taxiway. The accident occurred within the landing zone approximately 110 meters east-northeast of the center of the Runway 34 end at Nagoya Airport. It occurred at about 1115:45. Seven passengers were seriously injured and all 264 other occupants were killed.
Probable cause:
While the aircraft was making an ILS approach to Runway 34 of Nagoya Airport, under manual control by the F/O, the F/O inadvertently activated the GO lever, which changed the FD (Flight Director) to GO AROUND mode and caused a thrust increase. This made the aircraft deviate above its normal glide path. The APs were subsequently engaged, with GO AROUND mode still engaged. Under these conditions the FIO continued pushing the control wheel in accordance with the CAP'S instructions. As a result of this, the THS (Horizontal Stabilizer) moved to its full nose-up position and caused an abnormal out-of-trim situation. The crew continued approach, unaware of the abnormal situation. The AOA increased. The Alpha Floor function was activated and the pitch angle increased. It is considered that, at this time, the CAP (who had now taken the controls), judged that landing would be difficult and opted for go-around. The aircraft began to climb steeply with a high pitch angle attitude. The CAP and the FIO did not carry out an effective recovery operation, and the aircraft stalled and crashed.
The AAIC determined that the following factors, as a chain or a combination thereof, caused the accident:
1. The F/O inadvertently triggered the Go lever. It is considered that the design of the GO lever contributed to it: normal operation of the thrust lever allows the possibility of an inadvertent triggering of the GO lever.
2. The crew engaged the APs while GO AROUND mode was still engaged, and continued approach.
3. The F/O continued pushing the control wheel in accordance with the CAP'S instructions, despite its strong resistive force, in order to continue the approach.
4. The movement of the THS conflicted with that of the elevators, causing an abnormal out-of-trim situation.
5. There was no warning and recognition function to alert the crew directly and actively to the onset of the abnormal out-of-trim condition.
6. The CAP and FIO did not sufficiently understand the FD mode change and the AP override function. It is considered that unclear descriptions of the AFS (Automatic Flight System) in the FCOM (Flight Crew Operating Manual) prepared by the aircraft manufacturer contributed to this.
7. The CAP'S judgment of the flight situation while continuing approach was inadequate, control take-over was delayed, and appropriate actions were not taken.
8. The Alpha-Floor function was activated; this was incompatible with the abnormal out-of-trim situation, and generated a large pitch-up moment. This narrowed the range of selection for recovery operations and reduced the time allowance for such operations.
9. The CAP'S and F/O's awareness of the flight conditions, after the PIC took over the controls and during their recovery operation, was inadequate respectively.
10. Crew coordination between the CAP and the FiO was inadequate.
11. The modification prescribed in Service Bulletin SB A300-22-6021 had not been incorporated into the aircraft.
12. The aircraft manufacturer did not categorise the SB A300-22-602 1 as "Mandatory", which would have given it the highest priority. The airworthiness authority of the nation of design and manufacture did not issue promptly an airworthiness directive pertaining to implementation of the above SB.
Final Report:

Crash of a Cessna 208B Grand Caravan in Hiroshima: 1 killed

Date & Time: Apr 6, 1994 at 1915 LT
Type of aircraft:
Operator:
Registration:
JA8898
Flight Type:
Survivors:
No
Site:
Schedule:
Okayama - Hiroshima
MSN:
208B-0313
YOM:
1992
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Aircraft flight hours:
200
Circumstances:
While descending to Hiroshima Airport, the pilot encountered marginal weather with dark and limited visibility due to rain falls. On approach, the single engine aircraft struck the slope of Mt Noboru Lu (542 metres high) located about 15 from the airport. The wreckage was found at an altitude of 450 metres and the pilot, sole on board, was killed.
Probable cause:
It was determined that the pilot was not familiarized with night operations and that his capacities were probably reduced due to alcohol consumption.

Crash of a Douglas DC-9-41 in Hanamaki

Date & Time: Apr 18, 1993 at 1244 LT
Type of aircraft:
Operator:
Registration:
JA8448
Survivors:
Yes
Schedule:
Nagoya - Hanamaki
MSN:
47767
YOM:
1978
Flight number:
JD451
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
72
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
16106
Captain / Total hours on type:
8468.00
Copilot / Total flying hours:
615
Copilot / Total hours on type:
380
Aircraft flight hours:
47767
Aircraft flight cycles:
53314
Circumstances:
The approach to Hanamaki Airport was completed by the copilot. On short final, eight seconds prior to landing on runway 02, the aircraft was caught by downdrafts and windshear. Three seconds prior to touchdown, the captain regained control but this was too late. The aircraft landed hard, right main gear first. It rolled for about 1,860 metres before coming to rest on the runway, bursting into flames. All 76 occupants were rescued, among them 20 were injured. A fire erupted under the right wing following a tank rupture.
Probable cause:
It was determined that the aircraft encountered windshear on short final with wind from 240° to 320° gusting 26 to 47 knots. The copilot who was at controls at this time was not sufficiently experienced according to the operator operational procedures. Poor supervision on part of the captain and a too late recovery were considered as contributing factors.
Final Report:

Crash of a Lockheed P-3C-II.5 Orion in Iwo Jima

Date & Time: Mar 31, 1992
Type of aircraft:
Operator:
Registration:
5032
Survivors:
Yes
MSN:
185-5032
YOM:
1963
Country:
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Belly landed at Iwo Jima Airport and was damaged beyond repair. There were no casualties.

Crash of a Learjet U-36A off Shikoku Island: 5 killed

Date & Time: Feb 28, 1991
Type of aircraft:
Operator:
Registration:
9203
Flight Phase:
Flight Type:
Survivors:
No
MSN:
36-058
YOM:
1988
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
5
Circumstances:
The aircraft was engaged in a low level ECM exercice when it crashed in the sea off Shikoku Island. All five crew members were killed. It is understood that the aircraft struck the water surface while cruising at low level and low speed.

Crash of a Mitsubishi LR-1 Marquise in Japan

Date & Time: Feb 17, 1990
Type of aircraft:
Operator:
Registration:
22012
Flight Phase:
Flight Type:
MSN:
812
YOM:
1980
Location:
Country:
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Crashed in unknown circumstances somewhere in Japan. Crew fate unknown. Operated by the Japan Ground Self-Defence Force (JGSDF).

Crash of a NAMC YS-11-109 in Yonago

Date & Time: Jan 10, 1988 at 0936 LT
Type of aircraft:
Operator:
Registration:
JA8662
Flight Phase:
Survivors:
Yes
Schedule:
Yonago - Osaka
MSN:
2022
YOM:
1966
Flight number:
JD670
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
48
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
During the takeoff roll on runway 25, as V2 speed was reached, the copilot (pic) started the rotation but found the elevator control too heavy and decided to reject the takeoff. The crew initiated an emergency braking procedure but unable to stop within the remaining distance, the aircraft overran and plunged in the Nakaumi Lake. All 52 occupants were rescued, among them eight were injured. The aircraft was damaged beyond repair.
Probable cause:
Weather conditions were marginal at the time of the accident with light snow showers. It was determined that the crew failed to proceed to a deicing prior to takeoff. Thus it is believed that the elevator control may have been affected due to an accumulation of ice, frost and/or slush. It was also reported that the captain had been acting as such on YS-11 aircraft less then 6 months and that he was not allowed to leave the controls to the copilot during takeoff.
Final Report:

Crash of a Cessna T303 Crusader near Saga: 4 killed

Date & Time: May 15, 1987 at 0952 LT
Type of aircraft:
Operator:
Registration:
JA5277
Flight Phase:
Flight Type:
Survivors:
No
Site:
MSN:
303-00279
YOM:
1984
Location:
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
4419
Captain / Total hours on type:
1072.00
Copilot / Total flying hours:
3186
Copilot / Total hours on type:
843
Circumstances:
Three student pilots and one instructor were on board this Crusader to complete a training mission. While in cruising altitude under VFR mode over the north part of the Ariake Sea, the pilot-in-command lost control of the aircraft that entered a dive and crashed 3,6 km south of the Suminoe harbor. The aircraft disintegrated on impact and all four occupants were killed.
Probable cause:
It is believed that the loss of control occurred during a VFR training flight while the crew was performing emergency procedures. The crew was unable to recover the aircraft.
Final Report: