Crash of an Avro 748-1-105 in Bahía Blanca

Date & Time: Jul 15, 1969
Type of aircraft:
Operator:
Registration:
LV-IEV
Survivors:
Yes
Schedule:
Buenos Aires - Bahía Blanca
MSN:
1558
YOM:
1963
Country:
Crew on board:
4
Crew fatalities:
Pax on board:
35
Pax fatalities:
Other fatalities:
Total fatalities:
0
Aircraft flight hours:
16137
Aircraft flight cycles:
12930
Circumstances:
The descent to Bahía Blanca-Comandante Espora Airport was started by night. The crew was informed by ATC that the visibility was reduced to 200 meters due to fog which means below minima. The captain decided to attempt an approach to runway 34. After passing the middle marker, he was able to see the runway lights so he decided to continue the approach under visual mode. Shortly later, he lost visual contact when the airplane struck the ground about 25 meters short of runway threshold and 200 meters to the left of the extended centerline. On impact, the right wing was torn off and the airplane lost its undercarriage before coming to rest. All 39 occupants were evacuated safely.
Probable cause:
Wrong approach configuration on part of the captain who decided to land in below-minima weather conditions.

Crash of a Dinfia IA.50 Guaraní II in Córdoba: 3 killed

Date & Time: May 27, 1969
Type of aircraft:
Operator:
Registration:
T-123
Flight Phase:
Flight Type:
Survivors:
No
MSN:
15
YOM:
1968
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
Shortly after takeoff from Córdoba-Pajas Blancas Airport, while in initial climb, the airplane suffered an explosion and crashed. All three crew members were killed.

Crash of a Douglas C-47A-30-DK at Las Higueras AFB: 11 killed

Date & Time: May 5, 1969
Operator:
Registration:
TC-28
Flight Type:
Survivors:
No
Schedule:
Buenos Aires – Río Cuarto
MSN:
13783/25228
YOM:
1944
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
11
Circumstances:
On final approach to Las Higueras Airbase in Río Cuarto, the airplane crashed in unknown circumstances. All 11 occupants were killed.

Crash of a Rockwell Aero Commander 680 in Mendoza: 6 killed

Date & Time: Jan 31, 1969
Operator:
Registration:
LQ-FZC
Flight Phase:
Survivors:
No
MSN:
680-513-183
YOM:
1957
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
6
Circumstances:
Shortly after takeoff from Mendoza-Aeroparque Ciudad Mendoza Airport, while climbing, the airplane went out of control and crashed in the district of Los Horcones, near the airport. All six occupants were killed.

Crash of a De Havilland DHC-2 Beaver in Rosario: 2 killed

Date & Time: Nov 29, 1968 at 1200 LT
Type of aircraft:
Operator:
Registration:
LV-GHX
Flight Phase:
Flight Type:
Survivors:
No
MSN:
1274
YOM:
1959
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The single engine aircraft was engaged in a local post maintenance test flight with one technician and one pilot on board. Shortly after takeoff, the airplane went out of control and crashed near the runway end, killing both occupants.

Crash of a Cessna 411 in Maquinista Savio: 6 killed

Date & Time: Nov 7, 1968 at 0900 LT
Type of aircraft:
Registration:
LV-ISW
Flight Type:
Survivors:
No
Schedule:
Paraná – Buenos Aires
MSN:
411-0206
YOM:
1966
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
6
Circumstances:
While descending to Buenos Aires-Aeroparque-Jorge Newbury Airport, the twin engine airplane went out of control and crashed in a huge explosion near the Maquinista Savio train station. The aircraft was totally destroyed and all six occupants were killed.

Crash of a Douglas DC-6A/B in Mar del Plata

Date & Time: Nov 7, 1968
Type of aircraft:
Operator:
Registration:
TC-55
Survivors:
Yes
Schedule:
Río Gallegos – Mar del Plata – Buenos Aires
MSN:
44114
YOM:
1954
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
21
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The four engine aircraft was returning to Buenos Aires following a reconnaissance mission over Antarctica. The approach to Mar del Plata Airport was initiated in very bad weather conditions when the airplane crashed in flames in a field located some six km short of runway. All 24 occupants escaped while the aircraft was destroyed by a post crash fire.

Crash of a Convair CV-240-6 in Buenos Aires

Date & Time: May 26, 1967 at 1143 LT
Type of aircraft:
Operator:
Registration:
ZP-CDP
Survivors:
Yes
Schedule:
Asunción – Buenos Aires
MSN:
72
YOM:
1948
Country:
Crew on board:
6
Crew fatalities:
Pax on board:
18
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4958
Captain / Total hours on type:
780.00
Copilot / Total flying hours:
1800
Copilot / Total hours on type:
600
Aircraft flight hours:
18502
Circumstances:
The aircraft was on a scheduled international flight and was carrying eighteen passengers. It was coming in to land and was lined up with and about to touchdown on runway 10 when it suddenly underwent an abrupt change of attitude and crashed to the ground. After a series of bounces which commenced on the left wing causing it to break off together with the left power unik, the aircraft slewed round and came to rest upside down on a heading practically opposite to that of landing some 250 metres from the runway end. The pilot stated that during approach and when he was approximately 20 metres above and some 50 metres away from the runway threshold, and had just finished It calling to the co-pilot eighteen inches, reduce to idle", that is to say, when the aircraft was practically touching down, he heard the characteristic sound of propellers reversing (on both engines). At the very same moment, according to his statement, the mechanic reported this occurrence to him, and since the aircraft was nosing down and tilting to the left at the same time. he applied right rudder and tried to correct the attitude by nosing up. The aircraft, however, did not respond in spite of application of power to supplement the control manoeuvres. The aircraft nosed down and struck the runway surface. Both engines and the left wing were torn off, the aircraft went out of control, veered off runway and came to rest upside down in a grassy area. All 24 occupants were injured while the aircraft was destroyed.
Crew:
René Ferreira, pilot,
Pablo Romero, copilot,
Zacarías Soto, flight engineer,
Marcial Quiñónez, radio operator,
Néstor Arrúa, purser,
Elodia González, stewardess.
Photos via http://aeronauticapy.com/
Probable cause:
The conclusion set forth above is based on the fact that the electro-mechanical reverse safety device installed on the landing gear is so designed that whec the left landing gear strut is compressed it closes an electric circuit and frees the throttle lock. Therefore, the aircraft must touch down and roll for some distance in order to lose some lift through decrease in speed, The full weight of the aircraft is then on the landing gear and it is possible to move the levers manually and place the throttles into the proper position to reverse the propellers and then to give more throttle to gain more reverse thrust, All this requires some time and some ground roll distance after touchdown, which may or my not have some effect on the estimated distance for braking the aircraft or discontinuing the landing. The fact that the reverse lock safety system was inoperative was considered a deficiency in maintenance, even in the assumption that it had been intentionally so adjusted by the crew or during overhauls in the aviation workshops. The confirmed abnormality explains why in this particular case the levers could be moved back and the propeller reversing system operated. In accordance with the above findings and conclusions, it was considered that the statements by the crew members should be disregarded because, as brought out by the evidence, the accident was due to premature operation of the reversing system, when the aircraft was on final approach at a height of 20 metres, thereby causing it to go into a stall, This, together with the fact that the reverse safety mechanism was not: operating as it should have been, led to operation of the reversing system before the landing gear had made contact with the runway an essential requirement for operation of the propeller reversing system, barring any irregularities in the operation of the equipment. It is furthermore considered that the pilot-in-command acted incorrectly and imprudently in prematurely operating the propeller reversing system during the final approach instead of following the required procedure of applying reverse propellers during the landing run, when the weight of the aircraft is firmly on the landing gear. Consequently, the accident -- which was classified as serious -- was attributed to sudden loss of lift of the aircraft when it was about to land, which caused it to drop to the ground, slew round and turn over as a result of premature application of the propeller reversing system. An unofficial report stated that a paper cup was placed on the center console by the crew. On final approach, the content of this cup poured on the gear levers, causing an electrical short-circuit that caused the activation of the thrust reversers.
Final Report:

Crash of a Lockheed 18-08-01 LodeStar in La Plata

Date & Time: May 5, 1967
Type of aircraft:
Operator:
Registration:
N65GC
Flight Type:
Survivors:
Yes
MSN:
18-2029
YOM:
1940
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was performing an illegal flight and deliberately belly landed the airplane near La Plata, southeast of Buenos Aires. There were no casualties but the aircraft was written off.