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Crash of a Piper PA-60 Aerostar (Ted Smith 602P) in Fortingall: 1 killed

Date & Time: Nov 30, 2000 at 1635 LT
Operator:
Registration:
N64719
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Linz – Newcastle – Keflavik – Narsarsuaq – Goose Bay – New York
MSN:
60-8365-006
YOM:
1983
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1860
Circumstances:
Start-up, taxi and take-off were apparently normal with an IFR clearance for a noise abatement right turn-out on track towards the Talla VOR beacon. Soon afterwards the pilot was given clearance to join controlled airspace on track towards Talla at FL 140 and to expect the flight planned level of FL 200 when cleared by Scottish Radar. As the aircraft was climbing through FL 120 the Talla sector controller first cleared the pilot to climb to FL140 and then almost immediately re-cleared him to climb to FL 200. The pilot replied "ER NEGATIVE I WOULD LIKE TO MAINTAIN ONE FOUR ZERO FOR THE TIME BEING" and the controller granted his request. At 16:21 hrs the pilot transmitted "SCOTTISH NOVEMBER SIX FOUR SEVEN ONE NINE ER REQUESTING HIGHER TO GET OUT OF SOME ICING". Initially the controller offered FL 160 but the pilot replied "IF POSSIBLE TWO ZERO ZERO". Immediately he was given clearance to climb to FL 205, the correct quadrantal cruising altitude. Recorded radar data showed that for the next six minutes, the aircraft's rate of climb and airspeed were erratic. The pilot made one brief transmission of "SCOTTISH" at about 16:30 hrs but nothing more was said by him or the controller for another 20 seconds. Then the controller said "NOVEMBER SIX FOUR SEVEN ONE NINE ER I SEE YOU'RE IN THE TURN DO YOU HAVE A PROBLEM". There was no reply and so the controller repeated his message, eventually receiving the reply "YES I HAVE ER AN EMERGENCY". The controller asked the pilot to "SQUAWK SEVEN SEVEN ZERO ZERO" but the pilot replied "HANG ON". By this time the aircraft was descending rapidly in a gentle right turn. The controller twice asked the pilot for the nature of his problem but the pilot asked the controller to 'HANG ON FOR A MOMENT". The controller could see the aircraft was near high ground and losing altitude rapidly. He twice passed messages to this effect to the pilot but he did not receive an immediate reply. At 16:33 hrs the pilot transmitted "CAN YOU GET ME ER SOMEWHERE WHERE I CAN LAND I CAN'T MAINTAIN ALTITUDE AT ALL". Immediately the controller instructed the pilot to take up an easterly heading and gave him the aircraft's position relative to the airport at Perth. The controller then asked the pilot for his flight conditions (twice) to which the pilot eventually replied "I'M COMING OUT OF ER THE CLOUDS NOW" followed by "JUST BREAKING OUT". The controller then said "ROGER DO YOU HAVE ANY POWER AT ALL OR HAVE YOU LOST THE ENGINE". The pilot replied "I GOT POWER AGAIN BUT I HAVE NO CONTROL". That was his last recorded RTF transmission made at 16:34:40 hrs. The final radar return placed the aircraft at an altitude of 3,150 feet overhead Drummond Hill which is on the north bank of Loch Tay, near the village of Fortingall, and rises to 1,500 feet amsl.
Probable cause:
On vacating FL140, the aircraft's climb rate was so erratic at 140 KIAS that it seems likely that by then, the aircraft had already gathered sufficient ice to seriously affect its performance. If all the
turbocharger inlets had become partially blocked, then manually selecting both engines to alternate air induction should have introduced warmer air into the turbochargers and restored power. The description of engine operation in the Superstar manual states:
'If manifold pressure continues to decrease after opening the manual alternate air, it is an indication that turbocharger inlets are still restricted and the engine may become normally aspirated through the automatic alternate air door located below the induction air filter'.
Normal aspiration reduces the manifold pressure to ambient or less and at FL140 the ambient pressure is about 17.6 inches which is less than half the climb rated manifold pressure. That might explain the inability to climb above FL 160 but it would also have deprived the pilot of pressurisation. There was no change in his voice consistent with donning an oxygen mask so he may not have lost pressurisation completely. Nevertheless, since he lost control at around FL160 and 110 KIAS, and because the aircraft initially turned to the right, a combination of airframe icing and asymmetric power loss seem the most likely explanation for the sustained loss of control. The split in the EDP diaphragm which almost certainly occurred during this flight may have contributed to an asymmetric power problem. Alternatively, the pilot might have become mildly hypoxic and decided to begin an emergency descent. If so, he did not declare an emergency at the time he started to descend, although he did utter the word "SCOTTISH" after control was lost, so he was conscious even if his mental abilities had been impaired by hypoxia. On balance, the tone of his voice and his initial failure to respond to ATC messages suggested that the descent was begun through loss of control rather than a deliberate act followed by loss of control. At the time of the accident the aircraft had been flying below the freezing level (8,000 feet) for about five minutes and much of the airframe and induction system ice may have melted. The would-be rescuers would have taken at least five minutes to reach the crash site and so the fact that none of them reported seeing or treading on any ice was not surprising. Witness and propeller evidence indicated that power had been restored on at least one engine but there seemed to be insufficient power to climb out of Glen Lyon. The aircraft was out of control when it crashed at low speed from a sharp turning manoeuvre. Before this manoeuvre the pilot may have had partial control, albeit with a power problem which prevented him from climbing, and he finally lost control totally when he attempted to turn around within the confines of the Glen. He had no choice but to attempt the turn since, had he not turned, he would have flown into the side of the hill above the crash site.
Final Report:

Crash of a De Havilland DH.106 Comet 4 in Newcastle

Date & Time: Oct 7, 1970
Type of aircraft:
Operator:
Registration:
G-APDL
Flight Type:
Survivors:
Yes
Schedule:
Newcastle - Newcastle
MSN:
6413
YOM:
1959
Region:
Crew on board:
11
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew (pilots and engineers) was engaged in a local training flight at Newcastle Airport. On approach, the crew forgot to lower the gear and the airplane belly landed. It slid for several yards before coming to rest. All 11 occupants escaped uninjured while the aircraft was damaged beyond repair.
Probable cause:
The crew omitted to carry out the pre-landing checks while practicing a flapless landing.

Crash of a Hawker-Siddeley HS-125-3B in Edinburgh: 1 killed

Date & Time: Jul 20, 1970 at 1829 LT
Type of aircraft:
Operator:
Registration:
G-AXPS
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Edinburgh - Newcastle
MSN:
25135
YOM:
1967
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
5192
Captain / Total hours on type:
429.00
Copilot / Total flying hours:
4594
Copilot / Total hours on type:
144
Aircraft flight hours:
1874
Circumstances:
On the day of the accident the aircraft left Bristol under the command of the company's chief pilot for a flight to Edinburgh via East Midlands Airport. After conveying passengers to Edinburgh it was scheduled to position empty at Newcastle Airport to collect passengers for Bristol. Weather briefing had been obtained and a thorough flight plan covering the outward and return flights had been filed before the aircraft left Bristol in the morning. As there were no passengers on the flight from Edinburgh to Newcastle, the captain decided to make use of this sector to continue the other pilot's training for command of the HS-125. Accordingly, the trainee captain was flying the aircraft from the left hand seat. Prior to takeoff he was briefed that a failure of one of the engines (he was not told which one), would be simulated on takeoff and for the purpose of the exercise the rudder bias system would be switched 'OFF'. The pilots decided that no flap would be used for the takeoff which was started from the end of runway 13. The point where the aircraft became airborne was approximately 2,700 feet from the start of the roll, which was normal for the aircraft's weight and configuration, with both engines operating. The training captain called 'rotate' at approximately 120 knots, which was slightly faster than the calculated figure and when the aircraft had reached a height of approximately 12 feet and had accelerated to about 130 knots, he pulled back the thrust lever of the port engine to simulate a failure. He considered that the trainee pilot's reaction to the emergency was slow and was just about to apply right rudder to counteract the yaw when the trainee pilot applied considerable force to the left rudder and locked his leg in position. The captain immediately applied full right aileron and opened the port thrust lever but he was unable to prevent a high rate of roll developing to the left. Approximately 700 feet after the point where the aircraft became airborne the port wing tip struck the runway, fracturing the port fuel tank and spilling out fuel. The aircraft left the runway at an angle of approximately 30 degrees to the left and travelled across the grass, becoming partially inverted before settling back sideways on the ground on its undercarriage. The sideways movement of the aircraft pulled off the nose gear and the aircraft then gyrated across the airfield sustaining further structural damage before coming to rest on its main wheels and tail facing approximately in the opposite direction to the direction of takeoff. During the aircraft's gyrations on the ground, fuel, which was centrifuged out of the fractured port tank, ignited and a flash fire occurred. When the aircraft finally came to rest there was a small residual fire in the port wing which was very quickly extinguished by the airport fire service.
Probable cause:
The application of incorrect rudder following a simulated engine failure on take-off. The reason for this application of incorrect rudder has not been determined.
Final Report:

Crash of a De Havilland DH.89A Dragon Rapide in Simonburn

Date & Time: Feb 19, 1954
Registration:
G-AFMF
Flight Phase:
Survivors:
Yes
Schedule:
Newcastle – Dublin
MSN:
6432
YOM:
1938
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Ten minutes after his departure from Newcastle Airport, the pilot encountered severe icing conditions and the leading edge were contaminated with ice. At an altitude of 3,200 feet and while in a flat attitude, the twin engine aircraft hit the ground and crashed in fire. All eight occupants were seriously injured while the aircraft was destroyed.
Probable cause:
It was determined that the pilot failed to prepare the flight according to procedures as he started the mission without any information about weather conditions along the route. Thus, he was unaware of the icing conditions. It was also reported that the aircraft was not equipped with deice/anti-ice systems, which was against the regulations and considered as a contributory factor.
Final Report:

Crash of a Martin B-26B Marauder near Newcastle: 5 killed

Date & Time: Apr 10, 1944
Type of aircraft:
Registration:
41-18150
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Toome - Toome
Location:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
5
Circumstances:
The crew was engaged in a training exercise with other Marauder, and left that day the RAF Toome. En route, while cruising in low visibility due to mist, the aircraft hit the Mt Chimney Rock located south of Newcastle, County Down. The wreckage was found in the Spencer Valley, in the Mourne Mountains. All five crew members were killed.

Crash of a De Havilland DH.89A Dragon Rapide in Forest-in-Teesdale: 3 killed

Date & Time: Jun 20, 1939 at 1240 LT
Registration:
G-AERE
Flight Phase:
Survivors:
No
Site:
Schedule:
Heston – Newcastle
MSN:
6355
YOM:
1937
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
While cruising in bad weather conditions on a taxi flight from Heston to Newcastle-upon-Tyne, the crew failed to realize he was flying too low. The twin engine aircraft impacted the slope of Mt Dora's Seat located near Middleton. The aircraft was destroyed by impact forces and a post crash fire and all three occupants were killed. At the time of the accident, the visibility was poor due to mist.
Crew:
Ferruccio Silvani Appi, pilot,
James Elmslie, wireless operator.
Passenger:
John Lionel Crouch, famous British Jockey.
Probable cause:
Controlled flight into terrain.

Crash of an Avro 652 Anson I in Mt Misty Law

Date & Time: Sep 19, 1938
Type of aircraft:
Operator:
Registration:
L7949
Flight Phase:
Flight Type:
Survivors:
Yes
Site:
Schedule:
Ayr – Newcastle
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew lost his orientation while cruising in foggy conditions and failed to realize he was flying at a too low altitude. The twin engine aircraft crashed on a hilly terrain in the Misty Law Mountains, Renfrewshire. All four occupants were injured and the aircraft was destroyed.
Crew:
Lt John Charsley,
Hubert Jordon,
Percival Davidson,
William Nicol.
Probable cause:
Controlled flight into terrain.

Crash of a De Havilland DH.34B in Carrville

Date & Time: Jul 3, 1925
Type of aircraft:
Operator:
Registration:
G-EBBY
Flight Phase:
Survivors:
Yes
Schedule:
Croydon - Newcastle
MSN:
36
YOM:
1922
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The aircraft was performing a special flight from Croydon to Newcastle to follow the 'King's Cup Air Race'. En route, while cruising over Durham County, the crew encountered poor weather conditions and low visibility due to fog. As the pilot was unable to localize the destination, he decided to attempt an emergency landing in an open field when the aircraft impacted a ditch and came to rest against trees. While all seven occupants were uninjured, the aircraft was damaged beyond repair.

Crash of a De Havilland DH.4A in Newcastle: 1 killed

Date & Time: Oct 2, 1919 at 0845 LT
Type of aircraft:
Operator:
Registration:
G-EAEW
Survivors:
Yes
Schedule:
Croydon – Newcastle
MSN:
G7/67
YOM:
1919
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
On final approach to Newcastle, the engine lost power. The aircraft stalled and crashed few km from the airport. The passenger was injured and the pilot was killed.
Probable cause:
Engine failure caused by a fuel exhaustion.