Crash of a Cessna 421C Golden Eagle III in Charlevoix: 6 killed

Date & Time: Aug 3, 1994 at 1950 LT
Registration:
C-GVPB
Flight Phase:
Survivors:
No
Schedule:
Charlevoix - Trois-Rivières
MSN:
421C-0484
YOM:
1973
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
5261
Captain / Total hours on type:
1215.00
Aircraft flight hours:
3190
Circumstances:
Around 1950 eastern daylight saving time (EDT), the Cessna 421C aircraft, registration C-GVPB, operated by les Ailes de Charlevoix inc., took off on a visual flight rules (VFR) charter flight from Charlevoix Airport, Quebec, to Trois-Rivières, Quebec, with one pilot and five passengers on board. Shortly after take-off, witnesses saw greyish smoke emanating from the left engine. The aircraft entered a steep left turn followed by a descent. It then continued in the new direction. Shortly after, the aircraft yawed and entered an uncontrolled roll, nosed down, and crashed. The aircraft caught fire on impact. All six occupants were fatally injured during the impact. The aircraft was destroyed.
Probable cause:
It is probable that a loss of oil pressure in the left engine caused a loss of power just after take-off. The pilot was unable to maintain the minimum control speed (VMC) of the aircraft.
Final Report:

Crash of a Cessna 421C Golden Eagle III in Carlsbad: 2 killed

Date & Time: Jun 15, 1994 at 1434 LT
Registration:
N421AG
Flight Phase:
Survivors:
Yes
Schedule:
Carlsbad - Las Vegas
MSN:
421C-0843
YOM:
1980
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
3340
Captain / Total hours on type:
1240.00
Aircraft flight hours:
2943
Circumstances:
About 2 minutes after takeoff, the pilot declared an emergency, stating that he had lost an engine and needed to return to the airport. The airplane descended into rough, brush-covered terrain and then struck a large dirt berm, about 1-1/2 miles northeast of the departure airport. Examination of the engines did not reveal any obvious mechanical malfunction. The fuel was correct. Combustion chamber signatures indicated that the engines were operated at a lean or mild detonation condition. The flaps were extended about 30 degrees and the landing gear was retracted. The surviving passenger could not recall any dramatic engine problems, only that the airplane could not maintain altitude. The pilot and front seat passenger were not wearing shoulder harnesses.
Probable cause:
A loss of engine power for undetermined reasons. The pilot's failure to raise the flaps and maintain altitude were factors in the accident.
Final Report:

Crash of a Cessna 421C Golden Eagle III in San Antonio: 2 killed

Date & Time: Feb 10, 1994 at 0713 LT
Operator:
Registration:
N741CA
Flight Type:
Survivors:
Yes
Schedule:
San Antonio - Eagle Pass
MSN:
421C-0899
YOM:
1980
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
5100
Captain / Total hours on type:
400.00
Aircraft flight hours:
2916
Circumstances:
Shortly after takeoff, the pilot reported he had 'a problem' and needed to return immediately. Witnesses observed dark black smoke coming from both engines. The airplane collided with a tree 1/2-mile northeast of the runway threshold. Analysis of fuel samples revealed the presence of approximately 50% jet fuel. The right propeller was found feathered and engine disassembly revealed a hole burned in the right engine number 5 piston. Left engine disassembly revealed piston edges eroded down to the first compression ring. Fuel filler restrictors had been installed in the airplane's fuel tanks, but the fuel truck did not have the restrictive mating nozzle. The fuel truck was owned by the fuel vender and leased to the FBO.
Probable cause:
Improper servicing of the airplane with jet fuel, which resulted in preignition and/or detonation and subsequent failure of pistons in both engines. A factor related to the accident was: the lack of a restrictive mating nozzle on the refueling truck.
Final Report:

Crash of a Cessna 421C Golden Eagle III in McCook: 2 killed

Date & Time: Jan 26, 1994 at 1515 LT
Registration:
N5468G
Survivors:
Yes
Schedule:
Denver - Columbus
MSN:
421C-0215
YOM:
1976
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
2550
Captain / Total hours on type:
66.00
Aircraft flight hours:
5837
Circumstances:
The part 135 on-demand air taxi flight departed Denver, Colorado, with a destination of Columbus, Nebraska. Weather forecasts were for icing conditions along the entire route of flight. While en route, ATC advised the pilot of reported icing ahead. The pilot was cleared to climb to 19,000 feet to get on top of the clouds. The pilot reported 'some alternator problems,' and requested to divert to North Platte, Nebraska. He then elected to divert to McCook, Nebraska, due to the weather at North Platte. ATC lost communication with the pilot during the diversion. Witnesses reported the airplane circled the McCook Airport twice. According to them, the airplane entered a bank of about 45°, then stalled. Subsequently, it traveled about 190 feet through a stand of trees before coming to rest. Witnesses reported the airplane was covered with ice. One-half inch of mixed ice was found on a piece of windshield. Both alternators had one phase in the stator winding shorted.
Probable cause:
Improper in-flight planning/decision by the pilot, and the accumulation of airframe ice, which resulted in an inadvertent stall. Factors associated with the accident were: partial failure of both alternators, which resulted in a subsequent electrical system failure and an inoperative anti-ice/de-ice system, adverse weather (icing) conditions, and airframe (wing) ice.
Final Report:

Crash of a Cessna 421C Golden Eagle III in Titusville: 3 killed

Date & Time: Jan 21, 1994 at 1445 LT
Registration:
N777BE
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Titusville - Titusville
MSN:
421C-0134
YOM:
1976
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
20000
Circumstances:
Witnesses on the ground reported that the engines sounded normal while the airplane was taxiing to takeoff. After takeoff witnesses reported seeing white smoke trailing the left engine. The airplane was observed to bank to the left with a bank angle of about 90°. The airplane then pitched nose down, descended, and collided with trees and the ground. Examination of the left engine oil separator from the turbocharger assembly revealed that a section of pipe near a flange which is connected to the turbocharger oil outlet failed due to fatigue. There was no other failure or malfunction noted with the left or right engines and propellers. The mixture control arm on the left engine fuel control unit was found in the 'off' position. Additionally, the fuel selectors and magneto switches were also found in the 'off' position. A pilot-rated passenger occupied the left forward seat.
Probable cause:
Failure of the pilot-in-command to maintain vmc resulting in the inflight loss of control. Contributing to the accident was the fatigue failure of a section of pipe adjacent to a flange which connects to the turbocharger oil outlet of the left engine assembly.
Final Report:

Crash of a Cessna 421C Golden Eagle III in Budapest

Date & Time: Mar 25, 1993
Registration:
HA-ACA
Flight Type:
Survivors:
Yes
Schedule:
Budapest - Budapest
MSN:
421C-0615
YOM:
1979
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was engaged in a local training flight at Budapest-Ferihegy Airport. In unknown circumstances, the crew was forced to attempt an emergency landing when the aircraft crashed near the control tower, bursting into flames. Both occupants were injured.

Crash of a Cessna 421C Golden Eagle III in Eagle Mountain: 3 killed

Date & Time: Mar 11, 1993 at 2020 LT
Operator:
Registration:
N2656N
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Bermuda Dunes - Parker
MSN:
421C-0714
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
3250
Captain / Total hours on type:
500.00
Aircraft flight hours:
4869
Circumstances:
A Cessna 421 crashed after an inflight breakup. Investigation disclosed that the left outboard portion of the elevator assembly (including the balance weight) separated first, resulting in empennage flutter and subsequent in-flight breakup of the empennage. The left elevator outboard hinge and support structure exhibited evidence of hinge overtravel. The left horizontal stabilizer front spar had failed downward; rivets that attached the left outboard hinge to the rear spar of the left stabilizer had sheared; and the left elevator center hinge had been pulled off the rear spar. About 100 flight hours before the accident, maintenance was performed to repair the left elevator balance weight (which was loose) and to repair a damaged stiffener in the center structure of the horizontal stabilizer. However, when examined after the accident, the balance weight was tight and the repair to the stiffener was intact. All three occupants were killed.
Probable cause:
Failure of the left elevator for undetermined reason(s), which resulted in flutter and failure of the empennage, and subsequent uncontrolled collision with the terrain.
Final Report:

Crash of a Cessna 421C Golden Eagle III in Hamburg: 1 killed

Date & Time: Dec 17, 1992 at 2340 LT
Registration:
D-IDAK
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Hamburg - Cologne
MSN:
421C-0146
YOM:
1976
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
After takeoff from Hamburg-Fuhlsbüttel Airport runway 23, while climbing by night to a height of about 1,000 feet, the twin engine aircraft entered an uncontrolled descent and crashed. The pilot, sole on board, was killed.

Crash of a Cessna 421C Golden Eagle III in Wilsonville: 2 killed

Date & Time: Dec 12, 1992 at 1605 LT
Registration:
N98489
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Portland - Aurora
MSN:
421C-0067
YOM:
1968
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
4138
Captain / Total hours on type:
727.00
Aircraft flight hours:
2474
Circumstances:
Witnesses reported seeing the airplane flying in a normal cruise attitude when it rolled inverted and the nose dropped near vertical to the terrain. The airplane descended in a near vertical dive. The nose of the airplane started to come up horizontal to the terrain when it struck a 75-ft tree. During the post crash investigation, no evidence of a mechanical failure or malfunction was found. Both occupants were killed.
Probable cause:
The pilot-in-command's failure to maintain control of the aircraft.
Final Report:

Crash of a Cessna 421C Golden Eagle III in Santa Maria

Date & Time: Nov 22, 1992 at 1321 LT
Registration:
N52AK
Survivors:
Yes
Schedule:
Lake Tahoe - Santa Maria
MSN:
421C-0204
YOM:
1976
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4512
Captain / Total hours on type:
503.00
Aircraft flight hours:
4384
Circumstances:
Twelve minutes after departure, the left engine began to run rough and vibrate. The pilot said he could not correct the problem and shut the left engine down. No emergency was declared and the pilot told ATC that he would continue to his destination, 210 nm and 1.5 hours away. The pilot overflew 5 airports with runways over 5,000 feet long and a mountain range. The pilot executed a VOR approach and entered an extended downwind pattern. On short final the pilot executed a go around because he did not get any gear down indications. He then maneuvered for a downwind landing on runway 12. The aircraft hit the ground 100 yards short of the runway, then collided with a ditch and the airport fence. An FAA inspector said there were three clear tire tracks from the point of touchdown to the ditch, where the gear was sheared off. He found no problems with the gear system. Exam of the left engine revealed a left magneto internal failure due to lack of lubrication and wear, which caused cylinder cross firing.
Probable cause:
1) The internal failure of the left engine, left magneto due to inadequate maintenance and non compliance with the manufacturers service bulletins and recommendations, and
2) The failure of the pilot to attain the proper touchdown point during the landing attempt.
Factors in the accident were the inability of the pilot to shut off the left magneto and the false landing gear indications, both for undetermined reasons.
Final Report: