Crash of an Avro 748-310-2A LFD in Kasabonika

Date & Time: Aug 6, 1998 at 1600 LT
Type of aircraft:
Operator:
Registration:
C-GTAD
Flight Type:
Survivors:
Yes
Schedule:
Pickle Lake - Kasabonika
MSN:
1750
YOM:
1977
Flight number:
WSG804
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
20600
Captain / Total hours on type:
6000.00
Copilot / Total flying hours:
3000
Copilot / Total hours on type:
500
Aircraft flight hours:
12310
Circumstances:
Wasaya Airways Ltd. Flight 804, a Hawker Siddeley 748-2A, serial number 1750, landed at Kasabonika, Ontario, on a freight flight from Pickle Lake, Ontario. During the landing roll, the aircraft could not be stopped and overran the runway by about 450 feet. The captain, the first officer and one of the freight handlers suffered minor injuries; the other freight handler was not injured. The aircraft was destroyed.
Probable cause:
The aircraft was landed at a point from which it could not be stopped under the prevailing conditions. Contributing to the occurrence were the lack of immediate propeller ground fine pitch and the choice of runway 03 as the landing runway. A possible contributing factor was the inappropriate information in the then-current runway analysis manual.
Final Report:

Crash of an Avro 748-378-2B in Stansted

Date & Time: Mar 30, 1998 at 2331 LT
Type of aircraft:
Operator:
Registration:
G-OJEM
Flight Phase:
Survivors:
Yes
Schedule:
Stansted - Leeds-Bradford
MSN:
1791
YOM:
1982
Location:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
40
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6100
Captain / Total hours on type:
3950.00
Copilot / Total flying hours:
1100
Copilot / Total hours on type:
250
Aircraft flight hours:
18352
Aircraft flight cycles:
19122
Circumstances:
Immediately after take-off from London (Stansted) Airport, on a night flight with 30 passengers and 4 crew on board, an uncontained failure of the right engine occurred. This resulted in sudden power loss and a major engine bay fire. The commander elected to land back on the runway. The aircraft overran the paved surface, and uneven ground in the overrun area caused the nose landing gear to collapse. After the aircraft had come to rest, with the engine bay fire continuing, the crew organized a rapid evacuation and all the occupants escaped, with little or no injury. The engine bay fire was extinguished by the Airport Fire Service (AFS), but fuel release continued for some hours.
Probable cause:
The engine failure was caused by high-cycle fatigue cracking of the High Pressure (HP) turbine disc. Four similar Dart turbine failures had occurred over the previous 26 year period. These had been attributed to a combination of turbine entry flow distortion and turbine blade wear. The following causal factors were identified:
- Significant reduction in the fatigue strength f the HP turbine disc due to surface corrosion,
- Inadequate control of the fit between engine turbine assembly seal members, possibly influenced by inadequate turbine clamping blot fit, causing sufficient reduction in the natural frequency of an HP turbine disc vibratory mode to allow its excitation within the normal operating speed range and consequent excessive stressing of the disc,
- Fuel leakage from the engine bay fuel system, resulting in a major nacelle fire,
- Failure to identify the turbine assembly seal member fit and HP turbine disc corrosion as possible contributors to disc fatigue damage after previous similar failures.
Final Report:

Crash of an Avro C-91 in Navegantes

Date & Time: Feb 9, 1998
Type of aircraft:
Operator:
Registration:
2509
Flight Type:
Survivors:
Yes
Schedule:
Rio de Janeiro - Navegantes
MSN:
1732
YOM:
1975
Country:
Crew on board:
7
Crew fatalities:
Pax on board:
18
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
After landing at Navegantes-Itajaí Airport, the crew encountered unknown difficulties. The aircraft overran, lost its undercarriage and came to rest in a grassy area. All 25 occupants escaped uninjured and the aircraft was damaged beyond repair.

Crash of an Avro 748-106-1A in Pokhara

Date & Time: Nov 6, 1997
Type of aircraft:
Operator:
Registration:
9N-ACM
Survivors:
Yes
Schedule:
Kathmandu - Pokhara
MSN:
1549
YOM:
1963
Location:
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
44
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
After landing at Pokhara Airport, the hydraulic system failed. The crew lost control of the airplane that veered off runway to the right and collided with a parked Nepal Airways Avro 748 registered 9N-ACW. All 48 occupants evacuated safely while the aircraft was damaged beyond repair.

Crash of an Avro 748-401-2B in Yogyakarta

Date & Time: Oct 13, 1997
Type of aircraft:
Operator:
Registration:
PK-IHO
Survivors:
Yes
MSN:
1774
YOM:
1980
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
For unknown reasons, the twin engine airplane landed very hard at Yogyakarta-Adisutjipto Airport. All 10 occupants were uninjured while the aircraft was damaged beyond repair following irreparable structural damages.

Crash of an Avro 748-353-2A in Tambacounda: 23 killed

Date & Time: Feb 1, 1997 at 1438 LT
Type of aircraft:
Operator:
Registration:
6V-AEO
Flight Phase:
Survivors:
Yes
Schedule:
Tambacounda - Dakar
MSN:
1769
YOM:
1979
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
49
Pax fatalities:
Other fatalities:
Total fatalities:
23
Circumstances:
The departure was delayed due to overbooking. Passengers and crew were nervous and few passengers should disembark. Following a normal takeoff roll, the pilot-in-command started the rotation. About 30 seconds later, while climbing to a height of about 100 feet, the left engine failed. The aircraft stalled and crashed less than 100 metres past the runway end, bursting into flames. The aircraft broke in two and most of the survivors were found in the rear part of the cabin while the front one disintegrated on impact. Twenty-nine people survived while 23 others, including all three crew members, were killed.
Probable cause:
The exact cause of the accident could not be determined and the official accident report was not published by the Senegal Government. Nevertheless, The determination of the causes of the accident is therefore based on the expert reports ordered by the French investigating magistrate and the position of the locking pin of the left supply valve observed after the accident. Experts conclude that the left engine has stopped due to the closing of the fuel supply valve. The poor quality of the fuel was also blamed, which, before the accident, led Air Senegal to ask a chemical engineer from Shell-Senegal to test the fuel and the refueling operations. The engineer, while noting the poor quality of the fuel, came to the same conclusions as the experts. In France, operational tests were carried out on a similar aircraft and, moreover, fuel analyzes were carried out by the Accident Investigation Bureau. To these different expertises were added those of the government of the United Kingdom, the country of the manufacturer of the aircraft, and the results of a test carried out by British Aerospace with the same aircraft. The various analyzes carried out on the drums used for refueling showed that water was not present in the drums but in the pump used for refueling. It appears that the pump had been disassembled and the filters removed before filling the aircraft's tanks. As a result, the tiny amount of water that could have been found in the tanks would not have allowed the fuel to be considered contaminated and therefore unfit for consumption. The court, considering itself sufficiently informed by all these expertises, refused to grant the civil parties a further investigation 12 years after the facts. For the magistrates, there is no doubt that the determining cause of the accident was the closure of the left fuel isolation valve. The various investigations finally made it possible to determine that a ground mechanic had carried out a technical intervention under the left wing before the departure, at the level of the engine, but the exact nature of this intervention could not be established with precision. In its judgment, the court recognized that various indirect causes may have played a role in the occurrence of this air disaster: anomalies in the storage and distribution of fuel, nervousness and intense stress generated around the aircraft due to overbooking, irritability of the captain who, impatient to take off, did not consider certain checks useful. However, the magistrates have ruled, the determining cause perfectly defined by the various experts is the closing of the isolation valve of the left engine of the aircraft. On May 14, 2009, more than 12 years after the incident, Senegalese mechanic Moustapha Diagne was sentenced to 30 months' imprisonment with a 15-month suspended sentence. The length of the firm prison sentence is the length of the pre-trial detention that the defendant, after being extradited, had already served.

Crash of an Avro 748-402-2B in Ambon

Date & Time: Jul 11, 1996 at 0900 LT
Type of aircraft:
Operator:
Registration:
PK-IHN
Flight Phase:
Survivors:
Yes
Schedule:
Ambon - Manado
MSN:
1794
YOM:
1983
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
43
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
During the takeoff roll at Ambon-Pattimura Airport, just before Vr, one of the engine failed. The captain abandoned the takeoff procedure and initiated an emergency braking manoeuvre. Unable to stop with the remaining distance (the runway surface was wet), the aircraft overran and came to rest 180 metres further against a dyke. All 48 occupants evacuated safely while the aircraft was damaged beyond repair.

Crash of an Avro 748-352-2B in Meghauli

Date & Time: Apr 25, 1996 at 1158 LT
Type of aircraft:
Operator:
Registration:
9N-ABR
Survivors:
Yes
Schedule:
Kathmandu - Meghauli
MSN:
1771
YOM:
1979
Flight number:
RA155
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
27
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Following an uneventful flight from Kathmandu, the crew started the descent to Meghauli Airfield. On final, the aircraft was too high and landed too far down the runway, about 1,148 feet past the runway threshold (Meghauli Airstrip is 3,500 feet). Unable to stop on a wet grassy runway, the aircraft overran and came to rest in a ravine. All 31 occupants escaped uninjured while the aircraft was damaged beyond repair.
Probable cause:
Wrong approach configuration on part of the crew who landed the aircraft too far down the runway, reducing the landing distance available. Also, it was reported that the braking action was poor as the grassy runway was wet.

Crash of an Avro 748-216-2A near Kaimana: 10 killed

Date & Time: Aug 9, 1995
Type of aircraft:
Operator:
Registration:
PK-KHL
Survivors:
No
Site:
Schedule:
Langgur - Kaimana
MSN:
1735
YOM:
1974
Country:
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
10
Circumstances:
While descending to Kaimana Airport, the twin engine aircraft struck the slope of Mt Kumawa (2,800 metres high) located few km from Kaimana. The wreckage was found five days later and all 10 occupants were killed.
Probable cause:
Controlled flight into terrain.

Crash of an Avro 748-357-2B in Palaly: 52 killed

Date & Time: Apr 29, 1995 at 0845 LT
Type of aircraft:
Operator:
Registration:
4R-HVA
Flight Type:
Survivors:
No
Schedule:
Anuradhapura - Palaly
MSN:
1768
YOM:
1979
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
49
Pax fatalities:
Other fatalities:
Total fatalities:
52
Circumstances:
The aircraft was completing a flight from Anuradhapura to Jaffna-Palaly Airport on behalf of the Sri Lanka Air Force. On final approach, at an altitude of 3,000 feet, the aircraft was shot down by a surface-to-air missile and crashed in a huge explosion. All 52 occupants were killed, among them 44 soldiers, two policemen, three journalists and three crew members.
Probable cause:
Shot down by a surface-to-air missile fired by Tamil separatists.