Crash of a Cessna 421B Golden Eagle II in Nashville

Date & Time: Jul 8, 1977 at 0802 LT
Registration:
N1504G
Survivors:
Yes
Schedule:
McMinnville - Nashville
MSN:
421B-0601
YOM:
1974
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5571
Circumstances:
On approach to Nashville Airport, the pilot reported smoke in the cockpit and attempted an emergency landing. The aircraft crash landed few miles from the airport and was destroyed b a post impact fire. The pilot, sole on board, was seriously injured.
Probable cause:
Fire in cabin for undetermined reasons. The following findings were reported:
- Fire in cabin, cockpit, baggage compartment,
- Fire in engine,
- Smoke in cockpit,
- Forced landing off airport on land,
- Suspected or known aircraft damage.
Final Report:

Crash of a Beechcraft E18S in Covington: 2 killed

Date & Time: Sep 1, 1976 at 2239 LT
Type of aircraft:
Operator:
Registration:
N1052N
Flight Type:
Survivors:
No
Schedule:
Wakeman - Memphis
MSN:
BA-265
YOM:
1957
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
22950
Circumstances:
While approaching by night to Memphis Airport on a cargo flight from Wakeman, the airplane entered an uncontrolled descent and crashed in a field located in Covington, about 40 miles northeast of Memphis Airport. The aircraft was totally destroyed by impact forces and a post crash fire and both occupants were killed.
Probable cause:
The exact cause of the accident could not be determined as the aircraft was totally destroyed.
Final Report:

Crash of a Mitsubishi MU-2B-25 Marquise in Jefferson City: 5 killed

Date & Time: Nov 13, 1975 at 1345 LT
Type of aircraft:
Registration:
N69QJ
Survivors:
No
Schedule:
Memphis - Jefferson City
MSN:
254
YOM:
1973
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
3180
Captain / Total hours on type:
169.00
Circumstances:
On final approach to Jefferson City-Moore-Murrell Airport, the left engine failed. The airplane banked left the stalled and crashed in flames few miles from the airfield. The aircraft was destroyed and all five occupants have been killed.
Probable cause:
Powerplant failure for undetermined reasons. The following contributing factors were reported:
- Diverted attention from operation of aircraft,
- Failed to maintain flying speed,
- Improper operation of powerplan controls,
- Wreckage pattern indicative of aircraft in left rotation at impact,
- Left propeller 11-15°, right propeller 30° position.
Final Report:

Crash of a Lockheed 18 LodeStar in Rockwood: 2 killed

Date & Time: May 29, 1975 at 0150 LT
Type of aircraft:
Operator:
Registration:
N75G
Flight Type:
Survivors:
No
Schedule:
Gainesville - Rockwood
MSN:
2482
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
10685
Circumstances:
The airplane was engaged in an illegal flight from Gainesville to Rockwood, carrying a load of marijuana. On final approach to Rockwood Municipal Airport by night, in a gear up and flaps down configuration, the crew apparently attempted a low pass when the airplane struck trees located about a quarter mile short of runway and crashed in flames. The aircraft was destroyed and both pilots were killed.
Probable cause:
The accident was caused after the pilot-in-command failed to maintain flying speed and diverted attention from operation of the aircraft while completing a low pass by night.
Final Report:

Crash of a Cessna 411 in Memphis

Date & Time: May 15, 1975 at 1000 LT
Type of aircraft:
Operator:
Registration:
N617JC
Flight Phase:
Survivors:
Yes
Schedule:
Memphis - Baton Rouge
MSN:
411-0096
YOM:
1965
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4070
Captain / Total hours on type:
800.00
Circumstances:
After takeoff from Memphi Airport, while climbing, the right engine malfunctioned. The pilot elected to return but as he was unable to feather the propeller, he attempted an emergency landing in an open field located few miles from the airport. The aircraft belly landed and slid for dozen yards before coming to rest. All six occupants were injured, three of them seriously. The aircraft was written off.
Probable cause:
Engine malfunction after a failure of the propeller governor control system. The following contributing factors were reported:
- Material failure,
- Propeller control P/N 5000009-10 broken at swaged on fitting, pilot secured the engine but was unable to return to the airport due to windmilling propeller.
Final Report:

Crash of a Rockwell 1121 Jet Commander in Tullahoma

Date & Time: Mar 13, 1975 at 1440 LT
Operator:
Registration:
N711JT
Survivors:
Yes
Schedule:
Oklahoma City - Tullahoma
MSN:
1121-091
YOM:
1967
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4300
Captain / Total hours on type:
70.00
Circumstances:
Following an uneventful flight from Oklahoma City, the twin engine airplane landed on runway 36 at Tullahoma-Northern Regional Airport. After touchdown, it was unable to stop within the remaining distance and overran the wet runway before colliding with trees. All seven occupants escaped with various injuries and the aircraft was damaged beyond repair.
Probable cause:
Overshoot runway and collided with trees after the crew delayed in initiating go-around. The following contributing factors were reported:
- Wet runway,
- Hydroplaning on wet runway,
- Touchdown on runway 36 near intersection with runway 24, approximately 2,000 feet remaining.
Final Report:

Crash of a Beechcraft 65-90 King Air in Knoxville: 1 killed

Date & Time: Jul 16, 1974 at 1048 LT
Type of aircraft:
Registration:
N113TC
Survivors:
No
Schedule:
Oneida - Haleyville
MSN:
LJ-22
YOM:
1965
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
5397
Captain / Total hours on type:
36.00
Circumstances:
En route from Oneida to Haileyville, the pilot informed ATC about the failure of the right engine and was cleared to divert to Knoxville-Downtown Island Airport for an emergency landing. On short final, the pilot realized he was not properly aligned with the runway centerline and decided to initiate a go-around when he lost control of the airplane that crashed in flames. The aircraft was destroyed and the pilot, sole on board, was killed.
Probable cause:
Engine failure on approach due to inadequate maintenance and inspection. The following contributing factors were reported:
- Failure of the lubricating system: lines, hoses, fitting,
- Failed to maintain flying speed,
- Incorrect trim setting,
- Right engine oil line to cooler fitting disconnected,
- Full right trim.
Final Report:

Crash of a Beechcraft D18S in Tullahoma

Date & Time: Feb 14, 1974 at 0235 LT
Type of aircraft:
Operator:
Registration:
N313A
Flight Type:
Survivors:
Yes
Schedule:
Nashville - Chattanooga
MSN:
A-257
YOM:
1946
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1244
Captain / Total hours on type:
385.00
Circumstances:
While on a night approach to Tullahoma Airport, the left engine caught fire. The crew was able to extinguish the fire and the propeller was feathered. Unfortunately, the pilot missed the runway and the captain decided to initiate a go-around manoeuvre when the airplane stalled and crashed. Both occupants were injured and the aircraft was destroyed.
Probable cause:
Fire on left engine after a fuel line failed on approach. The following factors were reported:
- Loose parts,
- Failed to maintain flying speed,
- Fire in engine,
- Low ceiling,
- Obstructions to vision,
- Suspected or known aircraft damage,
- Loose fuel line.
Final Report:

Crash of a Douglas DC-9-32 in Chattanooga

Date & Time: Nov 27, 1973 at 1851 LT
Type of aircraft:
Operator:
Registration:
N3323L
Survivors:
Yes
Schedule:
Atlanta - Chattanooga
MSN:
47032/204
YOM:
1967
Flight number:
DL516
Crew on board:
5
Crew fatalities:
Pax on board:
74
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
15949
Captain / Total hours on type:
3218.00
Copilot / Total flying hours:
6301
Copilot / Total hours on type:
4000
Aircraft flight hours:
18233
Circumstances:
Following an uneventful flight from Atlanta, the crew started the approach to Chattanooga Airport in poor weather conditions with limited visibility due to heavy rain falls. On short final, the crew failed to realize his altitude was insufficient when the airplane struck approach light located 1,600 feet short of runway 20 threshold. The airplane then struck the ground, lost its left wing and skidded for another 1,200 feet before coming to rest 250 feet to the left of the runway centerline. All 79 occupants evacuated safely and only seven passengers were slightly injured.
Probable cause:
The pilot did not recognize the need to correct an excessive rate of descent after the aircraft had passed decision height. This occurred despite two verbal reports of increasing sink rate by the first officer. The captain disregarded the reports by the first officer, possibly because of the influence of a visual illusion caused by the refraction of light through the heavy rain on the windshield. The excessive rate of descent was initiated by a wind shear condition which extended in the lower levels of the approach path and a glide slope that tended toward the lower signal limit.
Final Report:

Crash of a Rockwell Aero Commander 500B in Alcoa: 2 killed

Date & Time: Feb 8, 1973 at 1255 LT
Operator:
Registration:
N6166X
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Knoxville - Knoxville
MSN:
500B-996-27
YOM:
1960
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
2871
Captain / Total hours on type:
82.00
Circumstances:
After takeoff from Knoxville-McGee Tyson Airport, while on a local flight, the pilot lost control of the airplane that dove into the ground and crashed in an open field located in Alcoa, south of the airport. The aircraft was destroyed and both occupants were killed. It was determined that the pilot was intoxicated.
Probable cause:
Uncontrolled descent after the pilot failed to maintain flying speed due to physical impairment. The following factors were reported:
- Alcoholic impairment of efficiency and judgment,
- Icing conditions including sleet and freezing rain,
- Stolen aircraft or unauthorized flight,
- Fog,
- Missed visual approach to airport under ravec,
- Blood alcohol 2,52‰,
- Unauthorized use of aircraft,
Final Report: