Crash of a Piper PA-31P Pressurized Navajo in Charleston: 1 killed

Date & Time: Jul 10, 1980 at 0858 LT
Type of aircraft:
Registration:
N776SW
Survivors:
Yes
Schedule:
Charleston - Paducah
MSN:
31-7730009
YOM:
1977
Crew on board:
2
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
12400
Captain / Total hours on type:
705.00
Circumstances:
After takeoff from Charleston-Intl Airport, while climbing, the right engine failed. The crew contacted ATC and was cleared to return for an emergency landing. The crew made a 180 turn to reach the approach path when the airplane lost height and crashed in a wooded area. A pilot was killed while five other occupants were injured.
Probable cause:
Powerplant failure for undetermined reasons. The following contributing factors were reported:
- The pilot-in-command failed to follow approved procedures,
- Improper emergency procedures,
- Complete engine failure one engine,
- Right engine not feathered.
Final Report:

Crash of a Douglas RC-54V Skymaster in McCormick: 2 killed

Date & Time: Nov 19, 1979 at 0610 LT
Type of aircraft:
Registration:
N8060C
Flight Type:
Survivors:
No
MSN:
10563
YOM:
1945
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
24200
Circumstances:
By night, the crew was flying at low altitude in the region of McCormick to find a suitable area to land while completing an illegal smuggling flight. In limited visibility due to fog, the airplane struck trees and crashed in flames in a prairie. The aircraft was destroyed and both occupants were killed. The aircraft was carrying a load of 15,000 lbs of marijuana.
Probable cause:
Collision with trees and subsequent crash while in traffic pattern-circling after the crew misjudged distance, speed, altitude and clearance. The following contributing factors were reported:
- Fog,
- Ground fog,
- Visibility below minimums,
- Collided with trees on rising terrain near sod strip at daybreak.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in Greenville: 5 killed

Date & Time: Nov 2, 1979 at 1112 LT
Operator:
Registration:
N66893
Flight Phase:
Survivors:
Yes
Schedule:
Greenville - Columbia
MSN:
31-7405192
YOM:
1974
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
18000
Captain / Total hours on type:
4.00
Circumstances:
After takeoff, while in initial climb, the right engine lost power. The pilot attempted an emergency landing and turned back when the airplane struck a power line and crashed in flames near the airport. The pilot and four passengers were killed while two other passengers were seriously injured.
Probable cause:
Powerplant failure for undetermined reasons. The following contributing factors were reported:
- Inadequate maintenance and inspection,
- High obstructions,
- Forced landing off airport on land,
- Engine malfunction before best climb speed.
Final Report:

Crash of a Lockheed C-141A-20-LM Starlifter in Charleston

Date & Time: Sep 18, 1979
Type of aircraft:
Operator:
Registration:
64-0647
Flight Type:
Survivors:
Yes
Schedule:
Charleston - Charleston
MSN:
300-6060
YOM:
1960
Crew on board:
6
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Aircraft flight hours:
18547
Circumstances:
The crew was completing a local training mission at Charleston Airport. Upon landing, the crew noticed the lack of a 'brakes released' light. After touchdown, thrust reversers failed to deploy because they were locked out by the touchdown relay, still in the Flight Mode. However, due to a malfunction, the n°4 thrust reverser did deploy. Normal brakes were inoperative. The copilot selected emergency brakes and then continued to make multiple attempts to deploy the spoilers. This caused the n°3 hydraulic system to lose pressure due to which in turn the emergency brakes failed. Then an electrical malfunction within the gear handle caused the nose gear to retract. The airplane came to rest in flames on its belly. All six crew members escaped with minor injuries while the aircraft was damaged beyond repair.

Crash of a Lockheed C-130E Hercules in Cottageville: 6 killed

Date & Time: Nov 30, 1978
Type of aircraft:
Operator:
Registration:
68-10936
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Pope - Charleston
MSN:
4316
YOM:
1969
Crew on board:
6
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
6
Circumstances:
En route from Pope AFB to Charleston, while flying in stormy weather, the four engine airplane went out of control, spiraled to the ground and crashed in a field. All six crew members were killed.
Probable cause:
Loss of control after being struck by lightning.

Crash of a Douglas DC-7CF in South Carolina

Date & Time: Dec 31, 1977
Type of aircraft:
Registration:
N73675
Flight Type:
Survivors:
Yes
MSN:
44878/681
YOM:
1956
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Suffered an accident somewhere in South Carolina in 1977 (exact date remains unknown). No casualties.

Crash of a Beechcraft 65-A90 King Air off Charleston

Date & Time: Nov 26, 1977 at 1705 LT
Type of aircraft:
Registration:
N55MG
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Cockburn Harbour - Wilmington
MSN:
LJ-303
YOM:
1967
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6630
Captain / Total hours on type:
175.00
Circumstances:
En route from South Caicos to Wilmington, the pilot encountered technical problems with both engines that failed in flight. He reduced his altitude and ditched the airplane into the sea off Charleston, South Carolina. Both occupants were quickly rescued while the aircraft was lost.
Probable cause:
Engine failure in normal cruise due to inadequate preflight preparation on part of the pilot. The following contributing factors were reported:
- Attempted operation with known deficiencies in equipment,
- Improper in-flight decisions or planning,
- Mismanagement of fuel,
- Fuel exhaustion,
- Miscalculated fuel consumption,
- Failure of both engines,
- Aircraft came to rest in water,
- Forced landing off airport on water.
Final Report:

Crash of a Boeing B-52G-85-BW Stratofortress near Aiken: 3 killed

Date & Time: Sep 3, 1975
Type of aircraft:
Operator:
Registration:
57-6493
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Seymour Johnson - Seymour Johnson
MSN:
464198
YOM:
1957
Crew on board:
7
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
The crew departed Seymour Johnson for a routine training mission. While cruising at an altitude of 28,000 feet, a structural failure occurred in the right wing that partially detached and struck the horizontal stabilizer. Out of control, the airplane entered a dive and four of the seven crew members were able to eject and were later found alive. The aircraft crashed between Aiken and Williston and disintegrated. Debris scattered on a wide area and three crew members were killed.
Crew:
Cpt James A. Perry,
Cpt Donald Exum,
Cpt Gregory A. Watts,
2nd Lt Hector M. Marquez,
Sgt Ricky K. Griffith, †
1st Lt Melvin M. Bewley, †
1st Lt Grady E. Rudolph. †
Probable cause:
A major fuel leak caused a structural failure of the right wing that separated between the third & fourth engine nacelles. The wing then shearing off the horizontal stabilizer, causing the aircraft to be uncontrollable.

Crash of a Beechcraft A100 King Air in Hilton Head: 6 killed

Date & Time: Apr 26, 1975 at 2055 LT
Type of aircraft:
Registration:
N700SP
Flight Phase:
Survivors:
Yes
Schedule:
Savannah - Hilton Head - Jackson
MSN:
B-92
YOM:
1972
Crew on board:
1
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
15657
Captain / Total hours on type:
549.00
Circumstances:
The aircraft was ferried from Savannah, Georgia, to Hilton Head Island, South Carolina, for a corporate flight to Jackson, Mississippi. The aircraft was owned and operated by Stribling-Puckett, Inc. The flight to Hilton Head Island was completed without incident. The pilot of N700SP loaded the passenger baggage; a witness to the loading indicated that the pilot loaded the baggage carefully in the baggage compartment in the aft end of the cabin. At 21:45, the eight passengers boarded the aircraft with one passenger seated in the copilot's seat. The engines were started and the aircraft was taxied to runway 3 for takeoff. The aircraft was taxied onto the 300-foot overrun on the south end of the runway, turned 180° on the runway, and made a "running" takeoff. Two pilots, one inside the terminal and another outside, stated that they did not believe the engines were developing full power during the takeoff. However, there were no unusual sounds, and the engines were operating "smoothly." Both of these pilots believed that the takeoff run was excessively long. The aircraft used about 3,900 feet of pavement to takeoff including most of the 300-foot overrun where the takeoff began. After takeoff, the aircraft was leveled off and was flown straight and level for about 1,200 feet. There it struck the top of a tree which was 40 to 50 feet above the ground. After impact with the trees, the aircraft continued 1,200 to 1,300 feet and struck several other trees before it came to rest right side up. Fire erupted some distance behind the aircraft, but progressed toward the aircraft slowly. The slow progression of the fire allowed the three survivors time to escape through a hole in the left front side of the fuselage. Roger W. Stribling, Jr., Vice President of the Stribling-Puckett, Inc, was killed in the crash. Company President Ben Puckett suffered a broken back in the accident.
Those killed were:
Roger Stribling Jr.,
Max Williams,
Henry Clements,
Clark Boyce Sr.,
Eddie Stanton,
Gordon Ellison.
Probable cause:
The failure of the pilot to maintain a positive rate of climb after a takeoff toward an unlighted area in night, visual meteorological conditions. The failure to maintain a positive rate of climb resulted in a collision with trees in the departure path. An overweight condition of the aircraft may have contributed to the pilot's actions. Investigation showed that the aircraft would have been 436 lbs over the maximum gross takeoff weight, with the center of gravity near the aft limit.
Final Report:

Crash of a Gulfstream GII near Kline: 3 killed

Date & Time: Jun 24, 1974 at 1645 LT
Type of aircraft:
Operator:
Registration:
N720Q
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Savannah - Savannah
MSN:
58
YOM:
1969
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
14500
Captain / Total hours on type:
4000.00
Aircraft flight hours:
3224
Circumstances:
The crew departed Savannah-Intl Airport on a training flight. While in cruising altitude over South Carolina, the airplane went out of control and entered a dive. It completed a 360 turn then crashed in a marshy field. All three crew members were killed.
Probable cause:
Uncontrolled descent following the failure of the wing spoiler system. The following contributing factors were reported:
- Unwanted extension of ground and flight spoilers, possibly due to short circuit in the extended control kit,
- Left ground spoiler actuator failed in flight.
Final Report: