Crash of a Beechcraft 65-A90 King Air in Aurora: 6 killed

Date & Time: Jul 10, 1978 at 1046 LT
Type of aircraft:
Registration:
N278DU
Flight Phase:
Survivors:
No
Site:
Schedule:
Denver - Richfield
MSN:
LJ-243
YOM:
1967
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
2715
Captain / Total hours on type:
810.00
Circumstances:
After takeoff from Denver-Stapleton Airport, while climbing, the left engine failed. The pilot lost control of the airplane that stalled and crashed in flames in the Aurora district. The aircraft was totally destroyed and all six occupants were killed. There were no injuries on the ground.
Probable cause:
Stall during initial climb due to engine failure for undetermined reasons. The following contributing factors were reported:
- Failure of the fuel pump system,
- Inadequate preflight preparation,
- Improperly loaded aircraft,
- Left engine boost pump inoperative, switched off,
- Crossfeed off,
- Approximately 700 lbs over max gross weight.
Final Report:

Crash of a Piper PA-31T Cheyenne II in Lamar: 4 killed

Date & Time: Jun 5, 1978 at 2140 LT
Type of aircraft:
Registration:
N176CC
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Lamar - Fort Collins
MSN:
31-7620024
YOM:
1976
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
3000
Captain / Total hours on type:
100.00
Circumstances:
After takeoff from Lamar Municipal Airport, while climbing, the twin engine airplane entered a controlled descent then crashed in a field located three miles south of the airport. The aircraft was destroyed and all four occupants were killed.
Probable cause:
Controlled collision with ground during climb to cruise due to inadequate preflight preparation. The following contributing factors were reported:
- Diverted attention from operation of aircraft,
- Pilot fatigue,
- Two large dogs and a cat in aircraft unrestrained,
- The pilot flew approximately 6 hours and performed 2 operations on the day of the accident.
Final Report:

Crash of a De Havilland DHC-6 Twin Otter 300 in Pueblo: 3 killed

Date & Time: Jan 18, 1978 at 1503 LT
Operator:
Registration:
N982FL
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Pueblo - Pueblo
MSN:
465
YOM:
1975
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
15284
Captain / Total hours on type:
307.00
Circumstances:
The crew was engaged in a local training flight at Pueblo-Memorial Airport. Following an approach to runway 27, the crew completed a circuit then a second approach to runway 17. After the airplane made a complete stop, the crew initiated a takeoff from runway 17. During initial climb, at a height of 100-150 feet, the airplane nosed over, stall and crashed near the runway end. The aircraft was destroyed upon impact and all three occupants were killed.
Probable cause:
Stall during initial climb after the crew failed to maintain flying speed. The following contributing factors were reported:
- Failed to follow approved procedures,
- Misused or failed to use flaps,
- Flaps found in fully extended 30° position,
- Flap setting for normal takeoff is 10°.
Final Report:

Crash of a Cessna 414 Chancellor near Aspen: 1 killed

Date & Time: Nov 27, 1977 at 1730 LT
Type of aircraft:
Registration:
N1682T
Flight Phase:
Flight Type:
Survivors:
Yes
Site:
Schedule:
Aspen - Pueblo
MSN:
414-0475
YOM:
1974
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1820
Captain / Total hours on type:
220.00
Circumstances:
The pilot initiated the takeoff from a snow covered runway at Aspen-Pitkin County-Sardy Field and with an aircraft covered with ice and snow on wings. At liftoff, the twin engine airplane struck a fence located past the runway end and despite the situation, the pilot continued departure. Few minutes later, at an altitude of 11,800 feet, the pilot encountered downdrafts/updrafts and lost control of the airplane that crashed in a canyon located few miles from the airport. The wreckage was found two days later. A passenger was killed while six other occupants were seriously injured.
Probable cause:
Controlled collision with fence during initial climb then controlled flight into terrain due to inadequate preflight preparation. The following contributing factors were reported:
- Failed to abort takeoff,
- Airframe ice,
- Improper in-flight decisions or planning,
- Snow on runway,
- Icing conditions including sleet, freezing rain,
- Downdrafts, updrafts,
- Ice and snow on wings,
- Hit fence at liftoff,
- Continued departure.
Final Report:

Crash of a Dassault Falcon 10 in Denver: 4 killed

Date & Time: Apr 3, 1977 at 0452 LT
Type of aircraft:
Operator:
Registration:
N60MB
Flight Phase:
Survivors:
Yes
Schedule:
Denver - Cheyenne
MSN:
15
YOM:
1974
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
16122
Captain / Total hours on type:
800.00
Aircraft flight hours:
1425
Circumstances:
Few minutes after takeoff from Denver-Stapleton Airport, while climbing to an altitude of 12,000 feet, the crew reported hydraulic problems and was cleared to return. Shortly later, the airplane entered an uncontrolled descent and crashed in a field located 10 miles northeast of Stapleton Airport. A passenger was seriously injured while four other occupants were killed.
Probable cause:
Uncontrolled descent for undetermined reasons.
Final Report:

Crash of a Douglas DC-9-14 in Denver

Date & Time: Nov 16, 1976 at 1729 LT
Type of aircraft:
Operator:
Registration:
N9104
Flight Phase:
Survivors:
Yes
Schedule:
Salt Lake City - Denver - Houston
MSN:
47081/155
YOM:
1967
Flight number:
TI987
Crew on board:
5
Crew fatalities:
Pax on board:
81
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
15000
Captain / Total hours on type:
651.00
Copilot / Total flying hours:
8400
Copilot / Total hours on type:
4000
Aircraft flight hours:
24333
Circumstances:
On November 16, 1976, Texas International Flight 987, a McDonnell Douglas DC-9-14, N9104, operated as a scheduled passenger flight from Salt Lake City, Utah, to Houston, Texas, with an intermediate stop at Denver, Colorado. The flight was routine to Stapleton International Airport, Denver, Colorado. The flight left the gate at Stapleton International Airport with 81 passengers and 5 crew members aboard. When Flight 987 was cleared to taxi to runway 8R for takeoff, the weather was clear, the wind was from 130° at 7 kns, and the temperature was 40° F. At 1726:33, the tower cleared the flight to take the runway and to hold while two light: aircraft took off from a nearby intersection. At 1729:13, Flight 987 was cleared for takeoff, and at 1729: 15 the flight reported "rolling." The first officer was making the takeoff and, upon receipt of the clearance, he advanced the throttles to a position commanding 1.4 EPR and released the brakes. After the engines stabilized at 1.4 EPR, the first officer advanced the throttles to the takeoff thrust position. Upon reaching this position, he relinquished control of the throttles and placed his left hand on the control yoke. The captain guarded the throttles until rotation speed (VR) was reached. The pilots described the takeoff roll to rotation as "normal." The captain monitored the engine instruments and noted no abnormal readings. He said he called out 100 KIAS, 130 KIAS, V1, VR, V2; the cockpit voice recorder (CVR) readout corroborated his statement. The first officer stated that when the captain called VR, he checked his airspeed indicator before he moved his control column aft and saw 149 or 150 KIAS either at, or just before, he began to rotate the aircraft. He stated that he rotated the aircraft at a normal rate to a target pitch angle of 10° which he determined from his attitude indicator; he estimated that this took about 3 to 4 seconds. About halfway through the rotation--about a 5° pitch angle--the stall warning system's stickshaker activated. The first officer stated that once it began it was continuous. He said he continued the rotation to what he believed to be about 10° and the stickshaker continued to operate. He saw that although the airspeed was beyond 150 KIAS, the aircraft did not lift off. Since it had accelerated to a speed greater than V1, the first officer said that he tried to get it airborne. He could not recall how long he maintained the pitch angle, but he believed it was adequate to get the aircraft off the runway. When he concluded that the aircraft was not going to fly, he rejected the takeoff. The captain stated that rotation was normal and that as rotation was begun there were a couple of "clacks" from the stickshaker. As the rotation continued, the stickshaker began to operate continuously. He saw about 10° pitch angle on his attitude indicator and 152 KIAS on the airspeed indicator. All other instrument indications were normal. The stickshaker continued to operate and he believed that the aircraft would not lift off. At this point, with the airspeed well past V2, he decided to reject the takeoff. His actions to reject the takeoff were simultaneous with those of the first officer. When the first officer began to abort the takeoff, he reached over and, in what he described as one continuous motion, pulled the throttles to idle and applied full reverse thrust. Almost simultaneous with his initiation of the power reduction, he felt the captain's hand on top of his. He said that he had already started to apply forward pressure on the yoke to lower the nose. on his, he realized that the captain was assuming control of the aircraft and he removed his own hand from the thrust levers and placed it on the yoke. He described the lowering of the nosewheel to the runway as rapid, and once it was on the ground he pushed the yoke forward to hold the nosewheel there and applied brakes. The stickshaker had stopped, but neither pilot could recall exactly when. When he felt the captain's hand When the nose was lowered, full reverse thrust and maximum wheel braking were applied; however, the ground spoilers were not deployed. The captain estimated that there was 2,500 to 3,000 ft of runway remaining when the takeoff was rejected. He later noted that they were in the amber lighted area of the runway when the abort began. The first officer said that all he could see were the amber runway edge lights when the nose was lowered. The amber coded runway edge lights on 8R begin 2,000 feet from the eastern threshold of the runway. The captain stated that he steered the aircraft toward the right side of the runway to avoid the approach light stanchions for runway 26L. The aircraft left the runway, continued another 1,050 ft, traversed two drainage ditches, struck approach light stanchions, turned left, and stopped headed in a northerly direction. After the aircraft stopped, the captain ordered the first officer to proceed into the cabin and assist the flight attendants with the passenger evacuation. The captain then cleaned up the cockpit and carried out the emergency engine shutdown procedures. The engines were shut down, the fuel shutoff valves were closed, the engine fire handles were pulled, the fire extinguishing agent was discharged, and battery and ignition switches were turned off. All 86 occupants were evacuated safely and the aircraft was damaged beyond repair.
Probable cause:
A malfunction of the stall warning system, for undetermined reasons, which resulted in a false stall warning and an unsuccessful attempt to reject the take-off after the aircraft had accelerated beyond refusal and rotation speed. The decision to reject the take-off although not consistent with standard operating procedures and training, was reasonable in this instant case, based upon the unusual circumstances in which the crew found themselves, the minimal time available for decision, and the crew's judgment concerning a potentially catastrophic situation.
Final Report:

Crash of a Douglas A-26C Invader in Grand Junction: 1 killed

Date & Time: Aug 8, 1976 at 1618 LT
Type of aircraft:
Registration:
N3427G
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Grand Junction - Grand Junction
MSN:
28704
YOM:
1944
Flight number:
Tanker 59
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
4100
Captain / Total hours on type:
500.00
Circumstances:
While completing a fire fighting mission, the pilot made a steep turn when the airplane stalled and crashed in flames. The pilot, sole on board, was killed.
Probable cause:
Stall during a low pass following improper in-flight decisions. The following contributing factors were reported:
- Flew into blind canyon,
- Failed to maintain flying speed,
- High obstructions,
- High density altitude at 9,700 feet,
- Wind gusting to 25 knots,
- Stall during steep bank.
Final Report:

Crash of a Douglas A-26B Invader near Grand Junction: 1 killed

Date & Time: Jul 16, 1976 at 0850 LT
Type of aircraft:
Operator:
Registration:
N5426E
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Grand Junction - Grand Junction
MSN:
27425
YOM:
1944
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
7000
Captain / Total hours on type:
200.00
Circumstances:
The pilot, sole on board, departed Grand Junction Airport on a fire fighting mission. While turning to final approach for slurry drop, the twin engine airplane flew into a mountain slope and crashed. The aircraft was destroyed and the pilot was killed.
Probable cause:
Controlled flight into terrain after the pilot failed to follow approved procedures. The following contributing factors were reported:
- Misjudged altitude and clearance,
- Jettisoned load.
Final Report:

Crash of a Rockwell Grand Commander 680 in Pagosa Springs: 4 killed

Date & Time: Dec 28, 1975 at 1200 LT
Registration:
N6221D
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Pagosa Springs - Burbank
MSN:
680-489-159
YOM:
1957
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
1600
Circumstances:
Just after liftoff from Pagosa Springs Airfield, while climbing, the right engine failed. The pilot was able to feather the propeller but the airplane lost height and crashed in flames in a canyon. The aircraft was totally destroyed and all four occupants were killed.
Probable cause:
Powerplant failure for undetermined reasons. The following contributing factors were reported:
- Improper emergency procedures,
- Airport conditions,
- High density altitude,
- Flew into blind canyon,
- Right engine quit, propeller feathered,
- Aircraft hit canyon wall,
- High obstructions at end of runway,
- Density altitude 7,400 feet.
Final Report:

Crash of a Mitsubishi MU-2B-30 near Rollinsville: 9 killed

Date & Time: Dec 26, 1975 at 1449 LT
Type of aircraft:
Operator:
Registration:
N133MA
Flight Phase:
Survivors:
No
Site:
Schedule:
Denver - Granby
MSN:
506
YOM:
1970
Crew on board:
1
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
9
Captain / Total flying hours:
3885
Captain / Total hours on type:
307.00
Circumstances:
The airplane was completing a charter flight from Denver to Granby on behalf of Conquest Aero Resources. While cruising in poor weather conditions (low clouds and snow falls), the pilot failed to realize his altitude was insufficient when the airplane struck a mountain located near Rollinsville. The wreckage was found two days later, on December 28, and all nine occupants have been killed.
Probable cause:
Controlled flight into terrain after the pilot continued VFR flight into adverse weather conditions. The following contributing factors were reported:
- Improper in-flight decisions,
- Disregard of good operating practice,
- High obstructions,
- Low ceiling,
- Snow,
- Fog.
Final Report: