Crash of a Cessna 402B in Saint-Barthélemy

Date & Time: Aug 5, 1996 at 1335 LT
Type of aircraft:
Operator:
Registration:
N403N
Flight Phase:
Survivors:
Yes
Schedule:
Saint-Barthélemy – Charlotte Amalie
MSN:
402B-0900
YOM:
1975
Crew on board:
1
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On August 5, 1996, about 1335 Atlantic standard time, a Cessna 402B, N403N, registered to Virgin Air, Inc. dba Air St. Thomas, as flight 105, 14 CFR Part 135 scheduled international passenger service, from St. Barthelemy Island to St. Thomas, overran the runway during an aborted takeoff at St. Barthelemy Island. Visual meteorological conditions prevailed at the time and an instrument flight plan was filed. The aircraft received substantial damage and the airline transport-rated pilot and 6 passengers were not injured. One passenger received minor injuries. The flight was originating at the time of the accident. The pilot stated the elevator control jammed during the takeoff roll. He aborted the takeoff, but could not stop prior to over running the runway. The aircraft came to rest in about 3 feet of water.

Crash of a Canadair CL-215-1A10 in Lake Fanaco: 1 killed

Date & Time: Jul 30, 1996
Type of aircraft:
Operator:
Registration:
I-CFSU
Flight Type:
Survivors:
Yes
MSN:
1074
YOM:
1985
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The crew was engaged in a fire fighting mission and was supposed to land on Lake Fanaco to proceed to a scooping manoeuvre. For unknown reasons, the aircraft landed hard, causing the hull to rupture. The aircraft sank and was lost. A pilot was killed and the second was injured.

Crash of a Boeing 747-131 off East Moriches: 230 killed

Date & Time: Jul 17, 1996 at 2031 LT
Type of aircraft:
Operator:
Registration:
N93119
Flight Phase:
Survivors:
No
Schedule:
New York – Paris
MSN:
20083
YOM:
1971
Flight number:
TW800
Crew on board:
18
Crew fatalities:
Pax on board:
212
Pax fatalities:
Other fatalities:
Total fatalities:
230
Captain / Total flying hours:
18800
Captain / Total hours on type:
5490.00
Copilot / Total flying hours:
17000
Copilot / Total hours on type:
4700
Aircraft flight hours:
93303
Aircraft flight cycles:
16869
Circumstances:
On July 17, 1996, about 2031 eastern daylight time, Trans World Airlines, Inc. (TWA) flight 800, a Boeing 747-131, N93119, crashed in the Atlantic Ocean near East Moriches, New York. TWA flight 800 was operating under the provisions of 14 Code of Federal Regulations Part 121 as a scheduled international passenger flight from John F. Kennedy International Airport (JFK), New York, New York, to Charles De Gaulle International Airport, Paris, France. The flight departed JFK about 2019, with 2 pilots, 2 flight engineers, 14 flight attendants, and 212 passengers on board. All 230 people on board were killed, and the airplane was destroyed. Visual meteorological conditions prevailed for the flight, which operated on an instrument flight rules flight plan. The investigation revealed that the crash occurred as the result of a fuel/air explosion in the airplane's center wing fuel tank (CWT) and the subsequent in-flight breakup of the airplane. The investigation further revealed that the ignition energy for the CWT explosion most likely entered the CWT through the fuel quantity indication system wiring; neither the ignition energy release mechanism nor the location of the ignition inside the CWT could be determined from the available evidence. There was no evidence of a missile or bomb detonation.
Probable cause:
An explosion of the center wing fuel tank (CWT), resulting from ignition of the flammable fuel/air mixture in the tank. The source of ignition energy for the explosion could not be determined with certainty, but, of the sources evaluated by the investigation, the most likely was a short circuit outside of the CWT that allowed excessive voltage to enter it through electrical wiring associated with the fuel quantity indication system. Contributing factors to the accident were the design and certification concept that fuel tank explosions could be prevented solely by precluding all ignition sources and the design and certification of the Boeing 747 with heat sources located beneath the CWT with no means to reduce the heat transferred into the CWT or to render the fuel vapor in the tank non flammable.
Final Report:

Crash of a Piper PA-46-310P Malibu in Hartford

Date & Time: Jul 12, 1996 at 1115 LT
Registration:
N234DM
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Hartford – Block Island
MSN:
46-8408043
YOM:
1984
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4918
Captain / Total hours on type:
488.00
Circumstances:
The pilot reported that he performed a rolling takeoff from the 2315 ft runway. He said that as soon as the airplane broke ground on the takeoff roll, he experienced a loss of engine power. The pilot said that he retracted the gear to help clear a 42 ft dike at the departure end of the runway. Also, he reported that after clearing the dike, he turned gradually to the left, and the left wing stalled. Two witnesses reported hearing loud, steady sounds from the airplane's engine and propeller. They said they saw the airplane in a high nose-up attitude, and watched the airplane descend behind the dike. The engine could be heard until the airplane contacted the river. During an operational check after the accident, the engine performed at recommended levels. According to performance data provided by the FAA, at the given takeoff weight, with a zero degree flap setting, the airplane required 2850 feet of runway to clear a 50 ft obstacle. The charts were based on full power before brake release.
Probable cause:
The pilot's inadequate preflight planning/preparation, and his failure to attain the proper liftoff airspeed, which resulted in a stall and collision with the terrain (river).
Final Report:

Crash of a De Havilland DHC-3 Otter near Cochenour

Date & Time: Jun 16, 1996 at 1914 LT
Type of aircraft:
Registration:
C-FMEL
Flight Phase:
Survivors:
Yes
Schedule:
Cochenour - Thunder Bay
MSN:
222
YOM:
1957
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The float-equipped DHC-3 (Otter), carrying the pilot and six passengers, departed the company's water base at Cochenour, Ontario, on a charter flight to Sandy Beach Lodge, located on Trout Lake approximately 25 miles to the east. The pilot levelled the aircraft and configured it for cruise flight at approximately 2,500 feet above sea level (asl). Shortly after level-off, the pilot heard a popping sound and noted a slight loss of engine power, and wisps of whitish-grey smoke entered the cabin. The aircraft instruments indicated normal engine operation, and the fire warning system did not activate. The pilot suspected that the engine had suffered a cylinder failure and turned to return to Cochenour. A passenger seated in the right front crew seat reported flames near the floor at the front, right corner of the cockpit. The pilot radioed the Thunder Bay Flight Service Station to advise of the emergency, had the passenger vacate the crew seat, and attempted to suppress the fire with a hand-held extinguisher. Thick, black smoke billowed into the cabin, restricting visibility and causing respiratory distress for all of the occupants. The pilot opened the left crew door in order to see ahead and landed the aircraft, still on fire, on McNeely Bay, the first available landing site. The aircraft landed hard but remained upright on the floats. The occupants left by the main door, with their life jackets, and were picked up almost immediately by nearby boats. The aircraft was consumed by fire within minutes after landing. The pilot suffered second degree burns to his face and right forearm, and the passenger in the right crew seat suffered burns to his right leg. The remaining five passengers escaped serious injury.
Probable cause:
Continued operation of the engine following an exhaust valve failure on the n°2 cylinder resulted in a flaming gas path near the right side of the firewall, an exhaust system overheat, and a subsequent cabin fire.
Final Report:

Crash of a Piper PA-31-310 Navajo off Stevensville

Date & Time: May 24, 1996 at 1055 LT
Type of aircraft:
Registration:
N103RW
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Stevensville - Laconia
MSN:
31-223
YOM:
1968
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2000
Captain / Total hours on type:
600.00
Aircraft flight hours:
3812
Circumstances:
The pilot reported that he ran the engines to full power before releasing the brakes. Immediately after lift-off, when he retracted the landing gear, he noticed a dramatic loss of airspeed. The airplane began to rock back and forth, and the pilot's efforts to increase the airspeed including lowering the nose and adding full power was unsuccessful. According to the Piper Information Manual for a short field takeoff, a lift-off speed of 85 mph and 15 degree of flaps is required. The reported winds were 010 degrees at 7 knots. The pilot departed runway 29 which is 2910 feet long. A witness who was refueling an airplane on the ramp stated that the airplane was still on the runway at the 500 foot mark from the end of runway 29.
Probable cause:
The pilot's improper short field takeoff/procedure and selection of the wrong runway for takeoff.
Final Report:

Crash of a Douglas DC-3C in Kenty Lake

Date & Time: May 5, 1996 at 1400 LT
Type of aircraft:
Operator:
Registration:
C-GCZG
Flight Type:
Survivors:
Yes
MSN:
17118/34385
YOM:
1945
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Upon landing on the icy Kenty Lake, the right ski struck a snowbank, causing the gear to collapse. All three occupants were evacuated safely while the aircraft was damaged beyond repair.

Crash of a Rockwell Aero Commander 500B in the Caribbean Sea: 3 killed

Date & Time: May 2, 1996
Registration:
N50GV
Flight Phase:
Survivors:
No
Schedule:
Christiansted - Roseau
MSN:
500-1308-120
YOM:
1963
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
11200
Circumstances:
The pilot departed on a VFR flight behind another company airplane. About 5 minutes after takeoff, the pilot informed the pilot in the lead airplane that he was having a generator problem, and that he would monitor them. The lead airplane landed at a different airport, and waited for the other pilot to join him after dropping off his passengers at another airport. The pilot did not arrive at either airport. All shipping vessels along the airplane's expected course were requested to report any sightings. No contact was reported and the search was terminated. Aircraft damage and injuries are presumed.
Probable cause:
The exact cause of the accident could not be determined.
Final Report:

Crash of an Antonov AN-2TP off Anadyr

Date & Time: Apr 20, 1996
Type of aircraft:
Registration:
RA-33631
Flight Phase:
Survivors:
Yes
MSN:
1G233-15
YOM:
1989
Country:
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Crashed in unknown circumstances in the sea (Anadyrsky Liman) off Anadyr. There were no casualties.

Crash of a Dornier DO228-212 off Matsu Nangan

Date & Time: Apr 5, 1996 at 1625 LT
Type of aircraft:
Operator:
Registration:
B-12257
Survivors:
Yes
Schedule:
Taipei - Matsu Nangan
MSN:
8223
YOM:
1993
Flight number:
VY7613
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
15
Pax fatalities:
Other fatalities:
Total fatalities:
6
Circumstances:
On approach to Matsu Nangan Airport, the crew encountered poor weather conditions with reduced visibility due to fog. The descent was completed under VFR mode in IMC conditions. On final, the copilot who was the pilot-in-command continued the approach despite he did not establish any visual contact with the runway, and failed to monitor the instruments. Eventually, the crew attempted to make a go-around but this decision was taken too late. The aircraft struck the water surface and crashed in the sea about 1,600 metres offshore. Six passengers were killed while 11 other occupants were injured.
Probable cause:
Wrong approach configuration on part of the crew who continued the descent under VFR mode in IMC conditions, below the MDA until the aircraft struck the water surface. Poor supervision on part of the captain. Poor crew coordination and poor approach and landing planning.