Crash of a Douglas DC-8-61F in Miami: 5 killed

Date & Time: Aug 7, 1997 at 1236 LT
Type of aircraft:
Operator:
Registration:
N27UA
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Miami - Santo Domingo
MSN:
45942
YOM:
1968
Flight number:
FB101A
Crew on board:
3
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
12154
Captain / Total hours on type:
2522.00
Copilot / Total flying hours:
2641
Copilot / Total hours on type:
1592
Aircraft flight hours:
46825
Aircraft flight cycles:
41688
Circumstances:
Fine Air Flight 101 was originally scheduled to depart Miami for Santo Domingo at 09:15 using another DC-8 airplane, N30UA, to carry cargo for Aeromar. Due to a delay of the inbound aircraft, Fine Air substituted N27UA for N30UA and rescheduled the departure for 12:00. N27UA arrived at Miami at 09:31 from San Juan, Puerto Rico, and was parked at the Fine Air hangar ramp. The security guard was not aware of the airplane change, and he instructed Aeromar loaders to load the airplane in accordance with the weight distribution form he possessed for N30UA. The first cargo pallet for flight 101 was loaded onto N27UA at 10:30 and the last pallet was loaded at 12:06. The resulting center of gravity (CG) of the accident airplane was near or even aft of the airplane’s aft CG limit. After the three crew members and the security guard had boarded the plane, the cabin door `was closed at 12:22. Eleven minutes later the flight obtained taxi clearance for runway 27R. The Miami tower controller cleared flight 101 for takeoff at 12:34. Takeoff power was selected and the DC-8 moved down the runway. The flightcrew performed an elevator check at 80 knots. Fourteen seconds later the sound of a thump was heard. Just after calling V1 a second thump was heard. Two seconds later the airplane rotated. Immediately after takeoff the airplane pitched nose-up and entered a stall. The DC-8 recovered briefly from the stall, and stalled again. The airplane impacted terrain in a tail first, right wing down attitude. it slid west across a road (72nd Avenue) and into the International Airport Center at 28th Street and burst into flames. Investigation showed that the center of gravity resulted in the airplane’s trim being mis-set by at least 1.5 units airplane nose up, which presented the flightcrew with a pitch control problem on takeoff.
Probable cause:
The probable cause of the accident, which resulted from the airplane being misloaded to produce a more aft center of gravity and a correspondingly incorrect stabilizer trim setting that precipitated an extreme pitch-up at rotation, was
1) The failure of Fine Air to exercise operational control over the cargo loading process; and
2) The failure of Aeromar to load the airplane as specified by Fine Air.
Contributing to the accident was the failure of the FAA to adequately monitor Fine Airs operational control responsibilities for cargo loading and the failure of the FAA to ensure that known cargo-related deficiencies were corrected at Fine Air.
Final Report:

Crash of a Cessna 207A Skywagon in Belize City: 1 killed

Date & Time: Jul 23, 1997 at 0724 LT
Operator:
Registration:
V3-HFD
Survivors:
No
Site:
Schedule:
San Pedro – Belize City-International – Belize City-Municipal
MSN:
207-0676
YOM:
1981
Flight number:
9N010
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1789
Captain / Total hours on type:
672.00
Aircraft flight hours:
11656
Circumstances:
The single engine aircraft landed at the Philip S. W. Goldson International Airport from San Pedro Airport, Ambergris Caye, with two passengers. The pilot remained in the aircraft on the apron while the two passengers disembarked. After receiving clearance from the Air Traffic Control Tower, V3-HFD, with no passengers, took off at 0720LT for the Belize City Municipal Airport. At 0722LT, the pilot reported by the Haulover Bridge and was instructed by ATC to change to frequency 122.8 MHz, which is the common broadcast frequency where pilots transmit their positions and intentions to each other. No further radio transmissions or distress calls were made to ATC after the pilot reported to Haulover Bridge. While approaching Belize City Municipal Airport at a very low altitude, the aircraft struck power cables and crashed onto a house located in the district Belama Phase 2, bursting into flames. The wreckage was found about 3 km southwest of runway 12 threshold. The pilot was killed and one people on the ground was injured. The aircraft was destroyed by impact forces and a post crash fire.
Probable cause:
There is no evidence which permits the investigation to determine with certainty the actual cause of the accident. It is considered a reasonable deduction that the probable cause of the accident was that the aircraft became uncontrollable after hitting high voltage transmission lines due to the aircraft being flown at a low altitude.
Final Report:

Crash of a Fokker F27 Friendship in Bandung: 28 killed

Date & Time: Jul 17, 1997 at 1155 LT
Type of aircraft:
Operator:
Registration:
PK-YPM
Survivors:
Yes
Site:
Schedule:
Bandung - Jakarta
MSN:
10415
YOM:
1969
Flight number:
TGN304
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
45
Pax fatalities:
Other fatalities:
Total fatalities:
28
Circumstances:
The aircraft departed Bandung-Husein Sastranegara Airport on a regular schedule flight to Jakarta, carrying 45 passengers and 5 crew members. Shortly after takeoff, the captain informed ATC that the left engine lost power and elected to diver to the Bandung-Sulaiman AFB for an emergency landing. On final approach to runway 13, the crew was unable to maintain a safe altitude when the aircraft struck roofs and crashed. Twenty occupants were rescued while 28 others were killed, including all five crew members. All occupants were Indonesian citizens except for one passenger from Singapore.
Probable cause:
Failure of the left engine for unknown reasons.

Crash of a Cessna 414A Chancellor in Zurich: 1 killed

Date & Time: Apr 10, 1997 at 2101 LT
Type of aircraft:
Operator:
Registration:
HB-LPN
Flight Type:
Survivors:
Yes
Site:
Schedule:
Colmar – Basel – Zurich
MSN:
414A-0842
YOM:
1982
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1006
Captain / Total hours on type:
350.00
Copilot / Total flying hours:
251
Copilot / Total hours on type:
2
Aircraft flight hours:
2318
Circumstances:
The crew was completing a flight from Colmar to Zurich with an intermediate stop in Basel. While on a night approach to runway 28 at Zurich-Kloten Airport, both engines lost power simultaneously. The aircraft lost height, struck a three-floor building and crashed on a second one located few dozen metres further. The captain was seriously injured while the copilot was killed.
Probable cause:
The accident was the consequence of the following factors:
- Insufficient flight preparation;
- Insufficient fuel supply;
- An emergency landing at night in a densely populated area following a double engine failure as a result of an inappropriate operation of the fuel selector switch.
Final Report:

Crash of a Basler BT-67 in Newton: 2 killed

Date & Time: Mar 15, 1997 at 1528 LT
Type of aircraft:
Operator:
Registration:
TZ-389
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Oshkosh - Newton
MSN:
26002
YOM:
1943
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
5350
Captain / Total hours on type:
3775.00
Aircraft flight hours:
17616
Circumstances:
At 1400 cst, modified Douglas DC-3C/BT-67R, TZ-389, and Beech A36, N3657A, began formation flight to get DC-3 flying time and for the 2nd occupant of the A36 to get aerial photos of the DC-3. A witness saw the airplanes at 500 feet to 700 feet agl, "flying close together heading north." He said "the big plane (DC-3) was flying straight and level. The little plane (A36) was just to the west of the big plane. The little plane then hit the big plane near the middle." After impact, pieces of acft were seen falling. Another witness saw the DC-3 heading north and the A36 circling it above and below. On its last pass, the A36 circled behind the DC-3, then crossed over the top and hitting the top of the DC-3. About 5 seconds after impact, the DC-3 gently rolled/turned westbound (apparently descending and gaining airspeed); the left wing then came off, followed by the right wing about 2 seconds later. Parts of the A36 empennage were found 3590 to 4,910 feet from the main wreckage. There was evidence that during impact, the DC-3 elevator and rudder controls were severed. No preimpact anomalies were found. At 1445 cst, an AIRMET had been issued, forecasting light to moderate turbulence below 8,000 feet msl. Toxicology tests of the DC-3 copilot's blood showed 0.127 mcg/ml amitriptyline (a prescription antidepressant with sedative side effects), 0.039 mcg/ml nortriptyline (metabolite of amitriptyline), and an undetermined amount of ephedrine and phenylpropanolamine (over-the-counter medications used in cold preparations, diet aids and stimulants).
Probable cause:
Failure of the Beech A36 pilot to maintain clearance from the modified Douglas DC-3, while positioning the A36 for photography of the DC-3.
Final Report:

Crash of a Fokker 100 in São Paulo: 99 killed

Date & Time: Oct 31, 1996 at 0827 LT
Type of aircraft:
Operator:
Registration:
PT-MRK
Flight Phase:
Survivors:
No
Site:
Schedule:
São Paulo – Rio de Janeiro
MSN:
11440
YOM:
1993
Flight number:
KK402
Country:
Crew on board:
6
Crew fatalities:
Pax on board:
89
Pax fatalities:
Other fatalities:
Total fatalities:
99
Captain / Total flying hours:
6433
Captain / Total hours on type:
2392.00
Copilot / Total flying hours:
3000
Copilot / Total hours on type:
230
Aircraft flight hours:
8171
Circumstances:
TAM flight 402 was a regular flight between São Paulo (CGH) and Rio de Janeiro (SDU). At 08:25 the flight received clearance for takeoff from runway 17R. Wind was given as 060 degrees. At 08:26:00 the throttles were advanced for takeoff power. Ten seconds later a double beep was heard. The captain said "O auto-throttle tá fora" and the copilot adjusted the throttles manually and informed the captain: "thrust check". With this information he confirmed that the takeoff power had been adjusted and verified. At 08:26:19 the airplane accelerated through 80 kts. At 08:26:32 the copilot indicated "V one". Two seconds later the airplane rotated at a speed of 131 kts. At 08:26:36 the air/ground switch transited from "ground" "to "air". The speed was 136 kts and the airplane was climbing at an angle of 10 degrees. At that same moment a shock was felt and the EPR of engine no. 2 dropped from 1.69 to 1.34, indicating the loss of power. In fact, the no. 2 engine thrust reverser had deployed. An eye witness confirmed to have seen at least two complete cycles of opening and closing of the no. 2 thrust reverser buckets during the flight. The loss of power on the right side caused the plane to roll to the right. The captain applied left rudder and left aileron to counteract the movement of the plane. The copilot advanced both thrust levers, but they retarded again almost immediately, causing the power of the no. 1 engine to drop to 1.328 EPR and engine no. 2 to 1,133 EPR. Both crew members were preoccupied by the movement of the throttles and did not know that the thrust reverser on the no. 2 engine had deployed. The throttles were forced forward again. At 08:26:44 the captain ordered the autothrottle to be disengaged. One second later the no. 2 thrust lever retarded again and remained at idle for two seconds. The airspeed fell to 126 kts. At 08:26:48 the copilot announced that he had disengaged the autothrottles. He then jammed the no. 2 thrust lever fully forward again. Both engines now reached 1,724 EPR. With the thrust reverser deployed, the airspeed declined at 2 kts per second. At 08:26:55 the stick shaker activated, warning of an impeding stall. The airplane rolled to a 39 degree bank angle and the GPWS activated: "Don't sink!". Seven seconds later the airplane impacted a building and crashed into a heavily populated neighborhood.
Probable cause:
The following findings were reported:
a. Contributing Factors
Psychological Aspect - Contributed
a) organizational aspect
The lack of information, instructions in writing and practice, contributed to the non-recognition of the abnormality during its unfolding.
b) Individual aspect
The unusual occurrence of the quick reduction of the lever, on a particularly difficult phase of the operation (transition from take-off run to flight); the nonoccurrence of failure discriminating (sound and visual) warnings, and the lack of cognizance and specific training for such abnormality bring on surprise and distraction of the crew members' attention.
- The release of the restriction of the lever of engine 2 at the idle detent without the occurrence of the abnormality warnings strengthened the tendency (in at least one of the crew members) to try to recover the power on the engine.
- The lack of warnings and the difficulties that are characteristic of such abnormality have diverted the crew members' concentration from the procedures provided for, to concentrate it on the solution of the abnormality, initially imagined as being an auto-throttle failure, and later the recovery of thrust
- The occurrence of auto-throttle failure warnings (before the 80 Kt) and the lack of specific reverse opening warnings (Master Caution and RSVS UNLK) have strengthened, in the crew members, the belief that they were experiencing an autothrottle failure (illusion).
b. Material Factor
(1). Desing Deficiency - Contributed
The reverser fault tree chart made recently by the manufacturer considering the Post-Mod version, even not taking into account a dormant fail, has indicated that the probability of an inadvertent opening of the reversers is of the order of 10"6. The Post-Mod version does not meet the airworthiness requirements of FAR/RBHA 25.1309.
On two phases of the complete reversers cycle, at the beginning of the opening and at the end of the shell closing, it is possible to apply power higher than IDLE with the shells partially open, which does not meet RBHA/FAR 25.933.
The reverser unlocked indication system is inhibited at speeds higher than 80 Kt and up to the height of 1000 feet, exactly at an instant when the pilots would need such information most.
The SECONDARY LOCK ACTUATORS (S/N 874 and S/N 870) that equipped the aircraft that suffered the accident, on the operational tests proposed and carried out, presented a performance much below the minimum acceptable to assure the safety and reliability of the system.
The applicable FAR 25.993(a)(3) requirements determine that each [reverse] system is to be provided with means to prevent the engine from producing power higher than idle power upon a failure on the reverse system [not stipulating the type of failure]. Such requirement has not been complied with, both in relation to the control system, which permitted the shells to open in flight, and in relation to protection, which became non-existent when the separation of the FEEDBACK CABLE occurred due to the unpredicted pilot's action on the lever, with the intention of recovering the power of the affected engine.
The TURNBUCKLE is installed on the side to which the connection moves when the reverser is commanded to open, i.e., the same side towards which the connection moves when the situation occurs in which the lever is forcibly held forward while the reverser is opening (deploying).
The THRUST SELECTOR VALVE may be moved with less than 2% of the normal functioning pressure, when the selector valve is de-energized, which was the condition at the time of the accident.
The inductive loads as those of SEC. LCK. ACTUATOR are detrimental to the contacts that command them, particularly on de-energization, in case there is no protection diode, which is apparently the case of SEC. LCK. ACTUATOR.
The THRUST REVERSER ACTUATOR, in the Post-Mod configuration, incorporated to the assembly line by the manufacturer, remains de-energized during the periods in which there is no commanding by the pilot, and this way it stays in an unstable and dangerous situation.
Design faults, an insufficient assessment of the fault tree diagram as compared to FAR 25.1309 and 25.933, and in the guidance to the operator not to train the abnormality that occurred on that phase, have indirectly contributed to the sequence of events that led to place the crew facing an unprecedented situation, without possibilities of recognizing and responding properly to avoid the loss of control.
c. Operational Factor
(1). Little experience on the aircraft - Indeterminate
Limitation of information and aids to the pilot. He had 230:00 total flight hours on this aircraft model, however the condition under which the unusual abnormality presented itself renders indeterminate the degree of experience that may be expected from a crew member to face such condition.
(2). Deficient Application of Control - Indeterminate
For three times, the thrust lever of engine 2 has been reduced and advanced. Such interventions on that lever have brought on the reduction of the thrust lever of the left hand engine, impairing the aircraft's performance. The non-return of the left hand lever to take-off thrust immediately, and the another four seconds delay in attaining such thrust, have contributed to deteriorate even more the aircraft's climbing capability.
The condition under which the unusual abnormality presented itself to the crew, and the lack of warning signals, has rendered the intentionality of the action indeterminate, and furthermore it was not possible to determine which of the two crew members has actuated the levers.
(3). Deficient Judgement - Indeterminate
The lack of cognizance, on the part of the crew members, for insufficiency of warning signals and information about the abnormality, has been a determinant for them to abandon the normal sequence of procedures, such as retracting the landing gear and actuating the Auto-Pilot, in order to take the initiatives of prioritizing the solution of an unusual situation installed in the cockpit, below safety height and that eventually brought on the loss of control of the aircraft, whereby it has also not been possible to determine which one of them took the initiative. Such facts render such aspect indeterminate.
d. Other Aspects
(1). External Inspection - Contributor
There is no condition of seeing the 'Secondary Lock' open, during the external inspection.
(2). Performing Action Below 400 feet - Contributor
Doctrinally, any action by a crew facing any abnormality in the cockpit environment below 400 feet is NOT RECOMMENDABLE.
The crew tried to manage the 'abnormality' concurrently with the control of the aircraft below 400 feet. Under such risk condition, a power reduction occurred on the other engine, compromising the aircraft's performance. As a consequence, the crew was obligated to prioritize the thrust needs to the detriment of other procedures.
(3). Inadequate Action In Face of an Unpredicted Failure - Contributor.
Based on the data collected on the SSFDR about the FUEL FLOW and EPR parameters, the lever of engine no. 2 was brought to the maximum power position, after the locking of said lever at the IDLE position.
Such locking occurred immediately after the lift-off, when the lever was reduced by itself to the 'IDLE' position, staying locked for about three (3) seconds. However, the system itself released the lever, inducing the copilot to bring it to the full power position, even after having informed the pilot about its locking.
It should be pointed out that the pilot has not requested such action after having been informed about the locking, as well as that the copilot has not asked whether such action should be done or not.
The airplane has not provided means for both pilots to be able to imagine how untimely such attitude would become at that extremely critical moment of the flight. In case the action has not been performed by the copilot, the suspicion falls upon the pilot, induced by the same reasons presented before.
Final Report:

Crash of a Boeing 707-323C in Manta: 34 killed

Date & Time: Oct 22, 1996 at 2244 LT
Type of aircraft:
Operator:
Registration:
N751MA
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Manta - Miami
MSN:
19582
YOM:
1967
Flight number:
OX406
Country:
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
34
Circumstances:
The aircraft departed Manta-Eloy Alfaro Airport on a cargo flight to Miami, carrying one passenger, three crew members and a load of frozen fish and flowers. Seven seconds after liftoff, while in initial climb, the crew informed ATC that the engine n°3 caught fire. The captain elected to maintain control but the aircraft lost altitude, struck the bell tower of the church La Dolorosa and crashed in a populated area located about 4 km west of the airport. The aircraft disintegrated on impact and several houses and building were destroyed. All four occupants as well as 30 people on the ground were killed. Fifty other people on the ground were seriously injured.
Probable cause:
It was reported that the engine n°3 suffered an uncontained failure during the takeoff roll as debris were found on runway 23.

Crash of an Antonov AN-124-100 in Torino: 4 killed

Date & Time: Oct 8, 1996 at 1050 LT
Type of aircraft:
Operator:
Registration:
RA-82069
Flight Type:
Survivors:
Yes
Site:
Schedule:
Moscow - Torino - Abu Dhabi - Bandar Seri Begawan
MSN:
977305591
YOM:
1993
Flight number:
SU9981
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
19
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total hours on type:
431.00
Circumstances:
The aircraft departed Moscow-Chkalovsky Airport bound for Torino, carrying 19 passengers and four crew members. The aircraft should be loaded with Ferrari cars to be delivered in Bandar Seri Begawan, Brunei, following a fuel stop at Abu Dhabi Airport. While descending to Torino-Caselle Airport, the crew was informed about the weather conditions at destination: wind variable at 3 knots, visibility 2,000 metres, RVR runway 36 more than 1,500 metres, light rain, scattered at 1,500 feet, scattered at 3,500 feet, broken at 7,000 feet, OAT and dew point 13°C, QNH 1012. On final approach to runway 36, the crew was unable to establish a visual contact with the runway and the captain decided to initiate a go-around procedure. Unfortunately, this decision was taken too late. While climbing, the aircraft struck trees and crashed onto houses located in the village of San Francesco al Campo, about one km from the runway end. The aircraft, a house and a barn were destroyed. Both pilots, two people on the ground and 20 cows in the barn were killed.
Probable cause:
The following findings were reported:
- Weather conditions were marginal,
- At the time of the accident, the runway length was 2,350 metres instead of 3,300 metres due to work in progress,
- The ILS CAT III system was inoperative during work in progress,
- The pilots were warned that the crew of an aircraft that landed on the same runway 36 about 11 minutes earlier established a visual contact with the runway at an altitude of 200 feet only,
- The crew continued the approach below MDA without establishing visual contact with the runway,
- Poor crew coordination,
- Poor approach planning,
- The crew failed to follow the approach checklist,
- The crew did not divide up the tasks in a correct manner,
- The crew did not prepare for a possible go-around procedure,
- The decision of the captain to initiate a go-around procedure was taken too late,
- The crew encountered engine trouble after the power levers were suddenly moved,
- The relative low experience of the captain on this type of aircraft.

Crash of an Antonov AN-24RV in Khartoum: 53 killed

Date & Time: May 3, 1996 at 2200 LT
Type of aircraft:
Operator:
Registration:
ST-FAG
Survivors:
No
Site:
Schedule:
Wau - Khartoum
MSN:
27307909
YOM:
1966
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
48
Pax fatalities:
Other fatalities:
Total fatalities:
53
Circumstances:
The aircraft was completing a charter flight from Wau to Khartoum, carrying 48 students from the Bahr al-Ghazalm University and five crew members. On approach to Khartoum-Haj Yusuf Airport, the crew encountered poor weather conditions and limited visibility due to a sandstorm and night. Unable to establish a visual contact with the runway, the crew abandoned the approach and initiated a go-around procedure. The crew then attempted several times to approach the airport of Khartoum and all attempts were abandoned, some sources are talking about nine attempts to land. On approach by night, the captain informed ATC he was short of fuel when the aircraft struck a building under construction and crashed about 15 km from the airport. The aircraft was totally destroyed and all 53 occupants were killed.
Probable cause:
The crew attempted several approaches in poor weather conditions and descended until the aircraft collided with obstacles and crashed.

Crash of a Douglas DC-8-55F in Asunción: 22 killed

Date & Time: Feb 4, 1996 at 1412 LT
Type of aircraft:
Operator:
Registration:
HK-3979X
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Barranquilla - Asunción - Campinas
MSN:
45882
YOM:
1966
Flight number:
ALA028
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
22
Captain / Total flying hours:
9100
Captain / Total hours on type:
5919.00
Copilot / Total flying hours:
3500
Copilot / Total hours on type:
3158
Aircraft flight hours:
66326
Aircraft flight cycles:
20567
Circumstances:
The aircraft was completing a positioning flight from Asunción to Campinas on behalf of Alas Paraguayas, under flight number ALA028. As there was no cargo on board, the crew decided to make profit of the situation to perform training upon takeoff. During the takeoff roll on runway 02, at Vr speed, the captain reduced the power on engine n°1 and after liftoff, he reduced power on engine n°2. With the undercarriage still down and the flaps at 15°, the aircraft became unstable, lost height and crashed in the district of Mariano Roque Alonso, about 1,500 metres past the runway end. The aircraft was destroyed by impact forces and a post crash fire and all four occupants were killed as well as 18 people on ground, most of them children taking part to a volleyball game.
Probable cause:
It was determined that the loss of control during initial climb was the consequence of the decision of the crew to perform training upon takeoff, intentionally reducing power on both engines n°1 and 2. This decision was taken at a critical phase of flight and the copilot-in-command was unable to maintain control of the aircraft, causing the aircraft to lose speed and to stall.
The following contributing factors were reported:
- The captain's experience in such configuration was low,
- Lack of flight safety doctrine in the cockpit during all flight,
- Execution of unauthorized takeoff training under uncontrolled conditions,
- Execution of such take-off training by a person who was not qualified as an instructor.
Final Report: