Crash of a Cessna 208B Super Cargomaster in Maiden: 1 killed

Date & Time: Jan 9, 1998 at 1704 LT
Type of aircraft:
Operator:
Registration:
N913FE
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Maiden - Greensboro
MSN:
208B-0013
YOM:
1987
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
4030
Captain / Total hours on type:
860.00
Aircraft flight hours:
6183
Circumstances:
The pilot was reported to be in a hurry as he positioned two aircraft and picked up the accident aircraft for his final positioning leg. He told company personnel he had a birthday party to go to and his family confirmed this. The pilot reported to company personnel that he was departing on runway 3 and that he would report in on his arrival at the destination. No further contacts with the flight were made and the wreckage of the aircraft was discovered off the end of the departure runway about 40 minutes after his reported takeoff. Examination showed the aircraft had run off the left side of the runway about 800 feet from the end and then crossed over the runway and entered into the woods at the departure end of the runway. Post crash examination showed no evidence of pre crash failure or malfunction of the aircraft structure, flight controls, or engine. The onboard engine computer showed the engine was producing normal engine power and the aircraft was traveling at 98 knots when electrical power was lost as it collided with trees. The aircraft's control lock was found tangled in the instrument panel near the left control yoke where it is normally installed and the lock had multiple abnormal bends, including a 90 degree bend in the last 1/2 inch of the lock where it engages the control column. Removal of the control lock and checking the flight controls for freedom is on the normal pilots checklist. The pilot was also found to not be wearing his shoulder harness.
Probable cause:
The pilot's failure to remove the control lock prior to takeoff and his failure to abort the takeoff when he was unable to initiate a climb, resulting in the aircraft over running the runway and colliding with trees on the departure end of the runway. Contributing to the accident was the pilot's self-induced pressure to arrive at his destination to attend a family affair.
Final Report:

Crash of a Douglas DC-6B in Nixon Fork Mine

Date & Time: Jan 2, 1998 at 1526 LT
Type of aircraft:
Operator:
Registration:
N861TA
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Nixon Fork Mine - Palmer
MSN:
43522
YOM:
1952
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
27000
Captain / Total hours on type:
16000.00
Aircraft flight hours:
46626
Circumstances:
During the takeoff roll, while passing 45 knots indicated airspeed, ice formed between the inner and outer panes of the airplane's windshield, obscuring the crew's vision. The flight crew aborted the takeoff, the airplane drifted off the left side of the snow covered runway, and caught fire. The crew reported the airplane and windshield were cold soaked and the temperature was -10 degrees Fahrenheit. The windshield anti-ice system blows air from a combustion heater between the windshield glass panes. The air source for the heater, once the airplane has forward airspeed, is two leading edge wing scoops. The crew told the NTSB investigator that the taxi time was too short for the windshield to warm up, and that during the taxi, snow was circulated around the airplane and into the wing scoops.
Probable cause:
The ingestion of snow into the windshield anti-ice system, and the resulting obscured windshield which made runway alignment not possible. Factors associated with this accident were the cold windshield, the reduced performance of the windshield anti-ice because of the short taxi by the crew, and the insufficient information on the system provided by the manufacturer.
Final Report:

Crash of a Swearingen SA227AC Metro III in Trinidad

Date & Time: Dec 31, 1997
Type of aircraft:
Operator:
Registration:
CP-2321
Flight Phase:
Survivors:
Yes
Schedule:
Trinidad - La Paz
MSN:
AC-643
YOM:
1986
Location:
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
18
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
During the takeoff roll, the crew lost control of the airplane that veered off runway, lost its undercarriage and came to rest. All 20 occupants escaped uninjured while the aircraft was written off.

Crash of a Cessna 402B in Watertown: 1 killed

Date & Time: Dec 30, 1997 at 1817 LT
Type of aircraft:
Registration:
N5087Q
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Watertown – Marshall
MSN:
402B-0565
YOM:
1974
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The pilot landed at Watertown, loaded and off-loaded cargo, and departed without getting out of the airplane. A witness reported seeing the airplane over the runway at an altitude of about 50 feet agl. The airplane was described to be bouncing and buffeting. Another witness reported the weather as overcast with occasional snow flakes. The airplane then descended, impacted the terrain and exploded. Post accident inspection revealed a 1/2 to 3/4 inch thick ridge of rime ice along the leading edge of the left horizontal stabilizer. Pieces of arc shaped ice were located along the wreckage path. Inspection of the wreckage failed to reveal any preimpact failure/malfunction of the engine or airframe which would have prevented flight.
Probable cause:
The pilot's failure to perform an aircraft preflight and to remove the ice which had accumulated on the airframe. A factor involved in the accident was the icing weather conditions which existed and the ice which accumulated on the airplane.
Final Report:

Crash of a Mitsubishi MU-2B-30 in DuPage: 2 killed

Date & Time: Dec 30, 1997 at 1705 LT
Type of aircraft:
Registration:
N999WB
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
DuPage - DuPage
MSN:
530
YOM:
1971
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1175
Captain / Total hours on type:
250.00
Copilot / Total flying hours:
4094
Copilot / Total hours on type:
10
Aircraft flight hours:
6275
Circumstances:
The airplane departed runway 1L and radar data indicated the airplane maintained about a 110 knot ground speed for 37 seconds as it climbed to 1,400 feet msl (642 feet agl) with a 008 degree heading. The last radar 14 seconds later indicated the airplane's heading was 342 degrees and had a 130 knot ground speed. The winds were 290/11. Witnesses reported seeing the airplane flying low and slow, and then it made a turn like a "barrel roll" to the left before impacting the ground. Examination of the engines and airframe revealed no pre-existent anomalies. The left and right propellers exhibited leading edge damage and chordwise abrasions. The pilot had a total of about 1,175 flight hours with about 250 hours in the type and model aircraft. The copilot had 4,094 total hours, but had 10 hours of turbine time and no flight time in the type and model of aircraft. The pilot had indicated he was practicing simulated single engine failures. The gear was fully retracted. The trim settings were set for a right engine out situation. The flap selector was set to "UP" flaps, but the flaps were found in transit at approximately 2 degrees of flaps. The Airplane Flight Manual indicated that during "Engine Failure in Takeoff-Gear Fully Retracted" stated that the required airspeed before selecting flaps to 5 degrees was 140 KCAS. The Pilot's Operating Handbook stated the flaps take approximately 31 seconds to retract from 20 to 0 flaps, or 21 seconds to retract from 5 to 0 flaps.
Probable cause:
The pilot in command failed to maintain control of the aircraft. A factor was the lack of experience of the pilot and copilot in the type and model of aircraft. An additional factor was the pilot did not follow the proper procedure when the flaps were raised before 140 knots was attained during a simulated single engine failure.
Final Report:

Crash of a Cessna 421C Golden Eagle III in Elkins

Date & Time: Dec 28, 1997 at 1340 LT
Registration:
N1348T
Flight Phase:
Survivors:
Yes
Schedule:
Elkins - Orlando
MSN:
421C-1059
YOM:
1981
Crew on board:
2
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3100
Captain / Total hours on type:
60.00
Aircraft flight hours:
3593
Circumstances:
The pilot/owner and a flight instructor had flown in to pick-up passengers. The owner was not multiengine rated and was receiving instruction from the instructor. The airplane was fueled and two adults and three children were boarded about 1 hour later. The owner was the flying pilot in the left seat. The owner stated that the 4,500 foot long runway was covered with 2 1/2 to 3 inches of snow and slush. He further stated that during the takeoff roll, 'The snow was so bad we could not get off the ground...' The pilot estimated that he aborted the takeoff at 100 mph, the braking action was zero, and the airplane went off the end of the runway. According to a witness, the five passengers arrived with 'lots of heavy bags.' After the accident, the baggage was removed before it could be weighed. An estimated airplane takeoff weight of 7,856 pounds was computed without baggage, based upon weights from the airplane weight and balance form, the police report, and FAA records. According to the Pilot's Operating Handbook, the maximum takeoff weight was published at 7,560 pounds.
Probable cause:
The flight instructor's failure to identify an unsafe runway condition and his delay in aborting the takeoff. Contributing was the aircraft's maximum takeoff weight exceeded, and a snow covered runway.
Final Report:

Crash of a Douglas C-47-DL off Guerrero Negro

Date & Time: Dec 20, 1997 at 1440 LT
Registration:
XA-CUC
Flight Phase:
Survivors:
Yes
Schedule:
Guerrero Negro - Isla de Cedros
MSN:
7377
YOM:
1943
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Shortly after takeoff from Guerrero Negro Airport, while climbing, the aircraft nosed down and crashed in the San Jose estuary, few hundred metres offshore. All five occupants were rescued while the aircraft was damaged beyond repair.

Crash of a Swearingen SA226T Merlin III in Byers: 1 killed

Date & Time: Dec 19, 1997 at 2017 LT
Registration:
N950TT
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Front Range - Aspen
MSN:
T-225
YOM:
1973
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
3316
Captain / Total hours on type:
479.00
Aircraft flight hours:
6599
Circumstances:
The pilot departed Front Range Airport (elevation 5512 feet) at approximately 2008, climbed to 7,000 feet msl, accelerated to 270 knots, and requested his IFR clearance. Weather at the time of N950TT's departure was 500 feet overcast; witnesses reported the tops of the thin cloud condition were 8,500 feet msl and it was very dark on top (no stars or moon). The pilot made several changes in airspeed and climb rate until radar indicated that he had entered an 8,500 fpm decent. The pilot reported to ATC that he had 'stalled' the airplane. Radar indicated that he then climbed at 7,500 fpm until his estimated airspeed was 10 knots, and then subsequently descended again at 8,400 fpm until he impacted the frozen ground. The pilot had flown 4 times for 7 hours in the previous 40 days. Five airline pilots, each of who had 3,000 to 5,000 hours in Swearingens, stated individually that even though the airplane is single pilot certified, they believed that 'its a two pilot airplane--because the work load is too high.'
Probable cause:
The pilot inadvertently stalling the airplane and his subsequent spatial disorientation which prevented him from maintaining airplane control. Factors were excessive workload on the pilot and the dark night light conditions.
Final Report:

Crash of an Ilyushin II-18V in Johannesburg

Date & Time: Dec 17, 1997 at 0620 LT
Type of aircraft:
Operator:
Registration:
RA-75554
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Johannesburg - Bujumbura
MSN:
185 0084 04
YOM:
1965
Flight number:
RMY202
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Aircraft flight hours:
18766
Aircraft flight cycles:
7040
Circumstances:
During the takeoff roll un runway 03L at Johannesburg-Jan Smuts Airport, the pilot-in-command started the rotation but the aircraft failed to respond. The captain decided to reject takeoff and initiated an emergency braking procedure. Unable to stop within the remaining distance, the aircraft overran, struck a concrete block, rolled for 200 metres then lost its left main gear and engine n°1 before coming to rest. All four occupants escaped uninjured while the aircraft was damaged beyond repair.
Probable cause:
It was determined that the total weight of the aircraft was five tons above MTOW while the CofG was too far forward, out of the envelope. In such conditions, the aircraft was not properly configured and a takeoff was impossible.

Crash of a Swearingen SA226TC Metro II in La Vertiente: 10 killed

Date & Time: Dec 12, 1997 at 1705 LT
Type of aircraft:
Registration:
CP-1635
Flight Phase:
Survivors:
Yes
Schedule:
La Vertiente - Santa Cruz
MSN:
TC-359
YOM:
1980
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
17
Pax fatalities:
Other fatalities:
Total fatalities:
10
Circumstances:
After takeoff from runway 01/19 at La Vertiente Airport, both engines lost power. The aircraft lost height, struck trees and crashed in a field some 300 metres past the runway end. A crew member and nine passengers were killed while nine other occupants were injured. The aircraft was completing a charter flight to Santa Cruz-Viru Viru Airport on behalf of Servicios Aéreos Vargas de España (SAVE), carrying employees of the Tesoro Bolivia Petroleum Company based in San Antonio, Texas.
Probable cause:
Loss of engine power for undetermined reasons.