Crash of a Pilatus PC-12/47E in Ubatuba

Date & Time: May 1, 2018 at 1743 LT
Type of aircraft:
Operator:
Registration:
PR-WBV
Flight Type:
Survivors:
Yes
Schedule:
Angra dos Reis – Campo de Marte
MSN:
1129
YOM:
2009
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4500
Captain / Total hours on type:
126.00
Copilot / Total flying hours:
3200
Copilot / Total hours on type:
120
Aircraft flight hours:
1361
Circumstances:
At the beginning of the descent to Campo de Marte Airport while on a flight from Angra dos Reis, the crew reported engine problems and diverted to Ubatuba Airport. After touchdown on runway 09 which is 940 metres long, a maneuver was performed aiming at exchanging speed for altitude, causing the airplane to veer off runway and to crash in a swampy area located in the left hand side of the overshoot area. The airplane struck several trees, lost its both wings and empennage and was destroyed. Both crew members and two passengers were injured while six other passengers escaped unhurt.
Probable cause:
At the beginning of the descent to Campo de Marte Airport, a failure occurred in the aircraft's propeller pitch control system, which tended to feather the engine.
The following findings were identified:
a) the pilots held valid Aeronautical Medical Certificates (CMA);
b) the PIC held valid Single-Engine Land Airplane (MNTE) and Airplane IFR Flight (IFRA) ratings;
c) the SIC held valid Single-Engine Land-Airplane (MNTE) and Multi-Engine LandAirplane (MLTE) ratings;
d) the pilots had qualification and experience in the type of flight;
e) the aircraft had a valid Airworthiness Certificate (CA);
f) the aircraft was within the prescribed weight and balance limits;
g) the records of the airframe, engine, and propeller logbooks were up to date;
h) the meteorological conditions were compatible with the conduction of the flight;
i) on 02Oct2017, a modification was made in the approved type-aircraft project;
j) on 06Mar2018, the engine of the aircraft was replaced with a rental engine, on account of damage caused by FOD;
k) the aircraft returned to the maintenance organization responsible for the engine replacement, due to recurrent episodes of Engine NP Warning Light illumination;
l) the maintenance organization inspected the powerplant, washed the compressor, and performed a pre-flight, after which the aircraft returned to operation;
m) the aircraft took off from SDAG, bound for SBMT;
n) between engine start-up and takeoff from SDAG, there were two drops of the propeller rotation (NP) to values below 950 RPM;
o) after taking off from SDAG, the aircraft climbed to, and maintained, FL145;
p) moments after the aircraft started descent, and upon reduction of the PCL, the propeller rotation began to drop quickly and continuously;
q) the adoption of the procedures prescribed for the situation “ENGINE NP - In flight, If propeller is below 1640” had no effect;
r) the NP dropped to a minimum value of 266 RPM;
s) the crew decision was to land in SDUB;
t) after the touchdown, a maneuver was performed aiming at exchanging speed for altitude, and deviation of the aircraft to a swampy area located in the left-hand side of the overshoot area;
u) in the functional tests of the engine performed after the occurrence, one verified normal operating conditions and full response to control demands;
v) upon examination of the propeller, and measurement of the beta ring distance, one verified that the ring displacement was outside the limits specified by the manufacturer;
w) it was not possible to identify whether such discrepancy had resulted from a maintenance procedure or from the impact during the emergency landing;
x) analysis of the propeller-governor revealed that the internal components were in operating condition;
y) the aircraft sustained substantial damage, and
z) the PIC suffered serious injuries, the SIC and two of the passengers were slightly injured, while the other six passengers were not hurt.

Contributing factors:
- Training – undetermined.
Even though the PIC had undergone simulator training less than a year before the occurrence, his difficulty perceiving the characteristics of the emergency experienced in order to frame it in accordance with his simulated practice suggests deficiencies in the processes related to qualification and training. The SIC, in turn, was not required to undergo that type of training, since the occurrence airplane had a Class-aircraft classification bestowed by the regulatory agency. The training and qualification process available to him in face of the circumstances may have contributed
to his lack of ability to recognize and participate in the management of the failure with due proficiency, when one also considers the selection of procedures and his assisting role in relation to the speeds and configuration of the aircraft.

- Instruction – a contributor.
As for the SIC, considering the fact that the aircraft classification did not require simulator sessions or other types of specific training, it was possible to note that he was not sufficiently familiar with emergencies and abnormal situations, something that prevented him from giving a better contribution to the management of the situation.

- Piloting judgment – a contributor.
There was inadequate assessment of the flight parameters on the final approach, something that made the landing in SDUB unfeasible, when one considers the 940 meters of available runway.

- Aircraft maintenance – undetermined.
During the measurement of the distance of the beta ring performed in the analysis of the propeller components, one verified that the displacement of the ring was outside the limits specified by the manufacturer. It was not possible to identify whether such displacement was due to a maintenance action or the result of a ring-assembly event at the time of propeller replacement. However, such discrepancy may have resulted from the impact of the propeller blades during the emergency landing. Furthermore, the aircraft was subject to inspection of the failure related to the ENGINE
NP warning light illumination prior to the accident. Given the fact that such illumination was intermittent, and the investigation could not identify the reasons for the warning, the aircraft was released for return to flight without in-depth investigation as to the root cause and possible implications of a failure related to the inadvertent drop in RPM.

- Memory – undetermined.
Although the PIC had undergone training in a class D aircraft-simulator certified by the manufacturer, it was not possible to verify the necessary association between the trained procedures and his performance in joining the traffic pattern and landing with a powerless aircraft in emergency. Furthermore, since the PIC frequently landed in the location selected for the emergency landing attempt, it is likely that he sought to match such emergency approach with those normally performed, in which he could count both on the “aerodynamic brake” condition with the propeller at IDLE and on the use of the reverse.

- Perception – a contributor / undetermined.
There was not adequate recognition, organization and understanding of the stimuli related to the condition of propeller feathering, which led to a lowering of the crew’s situational awareness.
Such reduction of the situational awareness made it difficult to assess the conditions under which the emergency could be managed, as the crew settled on the idea of landing in SDUB, without observing the condition of the airfield, meteorology, distance necessary for landing without control the engine, best glide speed, approach, and aircraft configuration.

- Decision-making process – a contributor / undetermined.
Since the first decisions made for identification of the emergency condition, it was not possible to verify the existence of a well-structured decision-making process contemplating appropriate assessment of the scenario and available alternatives. Objective aspects related to the SDUB runway, such as runway length and obstacles, the actual condition of the aircraft at that time, or contingencies, were not considered.

- Support systems – a contributor.
The Aircraft Manual and the QRH did not clearly contemplate the possibility of propeller feathering in flight, making it difficult for the pilots to identify the abnormal condition, and making it impossible for them to adopt appropriate and sufficient procedures for the correct management of the emergency. Considering the possibility that the application of the “ENGINE NP - In Flight”
emergency procedure prescribed by the QRH would not achieve the desired effect, there were no further instructions as to the next actions to be taken, leaving to the crew a possible
interpretation and selection of another procedure of the same publication.

- Managerial oversight – undetermined.
As for the maintenance workshop responsible for the tasks of engine replacement, together with adjustment of the propeller and its components: in the inspection at the request of the pilots after an event of ENGINE NP warning light illumination, the maintenance staff released the aircraft for return to operation. The investigation committee raised the possibility that the supervision of the services performed, by allowing the release of the aircraft, was not sufficient to guarantee mitigation of the risks related to the aircraft operation with the possibility of an intermittent recurrence of the failure.
Final Report:

Crash of a Cessna 402B in Tanner-Hiller

Date & Time: Apr 26, 2018 at 1715 LT
Type of aircraft:
Registration:
N87266
Flight Type:
Survivors:
Yes
Schedule:
Keene - Tanner-Hiller
MSN:
402B-1097
YOM:
1976
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
330
Aircraft flight hours:
9193
Circumstances:
The private pilot was conducting a local, personal flight. The pilot reported that he checked the weather conditions at three local airports before the flight but stated that he did not trust the wind reports. He added that he did not get a preflight weather briefing. Once at the destination airport, he conducted two go-arounds due to gusting wind conditions. During the third attempted landing, he made a steep approach at a normal approach speed and flared the airplane about midway down the 3,000-ft-long runway. The airplane floated down the runway for much longer than the pilot expected before touching down. Despite applying maximum braking, there was insufficient remaining runway to stop, and the airplane skidded off the runway, impacted trees, and subsequently caught fire, which resulted in substantial damage to the airframe. The wind conditions reported at an airport located about 13 miles away included a tailwind of 16 knots, gusting to 27 knots. Given the tailwind conditions reported at this airport and the pilot's description of the approach and landing, it is likely that the pilot conducted the approach to the runway in a tailwind that significantly increased the airplane's groundspeed, which resulted in a touchdown with insufficient runway remaining to stop the airplane, even with maximum braking.
Probable cause:
The pilot's improper decision to land with a tailwind, which resulted in a touchdown with insufficient runway remaining to stop the airplane.
Final Report:

Crash of a McDonnell Douglas MD-83 in Alexandria

Date & Time: Apr 20, 2018 at 1420 LT
Type of aircraft:
Operator:
Registration:
N807WA
Survivors:
Yes
Schedule:
Chicago - Alexandria
MSN:
53093/2066
YOM:
1993
Flight number:
WAL708
Crew on board:
7
Crew fatalities:
Pax on board:
94
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
13335
Captain / Total hours on type:
6466.00
Copilot / Total flying hours:
4590
Copilot / Total hours on type:
2474
Aircraft flight hours:
43724
Circumstances:
The airplane suffered a right main landing gear collapse during landing at the destination airport. The airplane sustained substantial damage to the right lower wing skin when it contacted the runway after the landing gear collapse. The crew stopped the airplane on the runway and an emergency evacuation was performed through three of the four doors on the airplane. The escape slide at the left forward door did not deploy or inflate due to the depletion of the gas charge in the reservoir. The reservoir depleted due to a leak in the valve assembly and was not caught during multiple inspections since installation of the slide assembly in the airplane. The landing gear cylinder fractured under normal landing loads due to the presence of a fatigue crack on the forward side of the cylinder in an area subject to an AD inspection for cracks. The most recent AD inspection of the cylinder was performed 218 landings prior when the fatigue crack was large enough to be detectable. A previous AD inspection performed 497 landings prior to the accident also did not detect the crack that would have been marginally detectable at the time.
Probable cause:
The failure of the right main landing gear under normal loads due to fatigue cracking in an area subject to an FAA Airworthiness Directive that was not adequately inspected.
Final Report:

Crash of an Antonov AN-74-200 in Akola

Date & Time: Apr 14, 2018
Type of aircraft:
Operator:
Registration:
EK-74036
Flight Type:
Survivors:
Yes
MSN:
365 470 98 965
YOM:
1995
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The aircraft was completing a humanitarian mission, carrying five crew members and a load of various goods. After landing, the aircraft was unable to stop within the remaining distance. It overran, lost its left main gear and came to rest. All five occupants evacuated safely and the aircraft was damaged beyond repair.

Crash of a Cessna 208B Grand Caravan in Atqasuk

Date & Time: Apr 11, 2018 at 0818 LT
Type of aircraft:
Operator:
Registration:
N814GV
Flight Type:
Survivors:
Yes
Schedule:
Utqiagvik – Atqasuk
MSN:
208B-0958
YOM:
2002
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7713
Aircraft flight hours:
9778
Circumstances:
The pilot was on a visual flight rules flight transporting mail to a remote village. He reported that when he was about 15 minutes from the destination, he checked the automated weather observing system (AWOS) for updated weather information for the destination and recalled that the visibility was reported as 7 miles. However, the information he recalled was not consistent with what was actually reported by the AWOS; 18 minutes before the accident, the AWOS reported no more than 1 3/4 miles visibility. As he descended the airplane from 2,500 ft to 1,500 ft in the terminal area, he observed reduced visibility conditions that would require an instrument approach procedure. According to the pilot, while maneuvering toward the initial approach fix, he heard the autopilot disconnect, and the airplane began an uncommanded descent. He said that he remembered pulling on the control wheel and thought he had leveled off, but then the airplane impacted terrain, which resulted in substantial damage to the fuselage, vertical stabilizer, and rudder. He could not recall if he had heard terrain warnings or alerts before the impact. An airplane performance study indicated that the airplane was in a continuous descent from 2,500 ft until the final data point about 12 ft above the surface; the airplane was not leveled off at any time during the descent. In the final 15 seconds of recorded data, the rate of descent increased from about 500 fpm to about 2,300 fpm before decreasing to 1,460 fpm at the last recorded data point. Postaccident examinations of the airframe, engine, flight control, and autopilot components revealed no mechanical malfunctions or failures that would have precluded normal operation or affected flight controllability. It is likely that the unexpected instrument approach procedure increased the pilot's workload as he maneuvered to set up for the approach. Further, when the autopilot disconnected, the airplane continued to descend; although the pilot reported that he heard the autopilot disconnect, he did not arrest the airplane's descent rate. Given the low visibility conditions, it is likely that the pilot did not detect the airplane's descent, and the airplane descended into the terrain.
Probable cause:
The pilot's decision to continue a visual flight rules flight into an area of instrument meteorological conditions and his subsequent failure to level the airplane after the autopilot disconnected, which resulted in a collision with terrain.
Final Report:

Crash of a Cessna 525 Citation CJ4 in Marion

Date & Time: Apr 2, 2018 at 1709 LT
Type of aircraft:
Operator:
Registration:
N511AC
Survivors:
Yes
Schedule:
Jackson - Marion
MSN:
525C-0081
YOM:
2012
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
35437
Captain / Total hours on type:
2537.00
Aircraft flight hours:
2537
Circumstances:
A single-engine airplane was taking off from runway 15 about the same time that a multi-engine business jet landed on a nearly perpendicular runway (runway 22). The single-engine airplane, piloted by a private pilot, was departing on a local flight. The jet, piloted by an airline transport pilot, was rolling down the runway following a straight-in visual approach and landing. The single-engine airplane collided with the empennage of the jet at the intersection of the two runways. Witnesses in the airport lounge area heard the pilot of the single-engine airplane announce on the airport's universal communications (UNICOM) traffic advisory frequency a few minutes before the accident that the airplane was back-taxiing on the runway. The pilot of the jet did not recall making any radio transmissions on the UNICOM frequency and review of the jet's cockpit voice recorder did not reveal any incoming or outgoing calls on the frequency. The pilots of both airplanes were familiar with the airport, and the airport was not tower controlled. The airport had signage posted on all runways indicating that traffic using the nearly perpendicular runway could not be seen and instructed pilots to monitor the UNICOM. A visibility assessment confirmed reduced visibility of traffic operating from the nearly perpendicular runways. The reported weather conditions about the time of the accident included clear skies with 4 miles visibility due to haze. Both airplanes were painted white. It is likely that the pilot of the jet would have been aware of the departing traffic if he was monitoring the UNICOM frequency. Although the jet was equipped with a traffic collision avoidance system (TCAS), he reported that the system did not depict any conflicting traffic during the approach to the airport. Although the visibility assessment showed reduced visibility from the departing and arrival runways, it could not be determined if or at what point during their respective landing and takeoff the pilot of each airplane may have been able to see the other airplane. In addition to the known reduced visibility of the intersecting runways, both airplanes were painted white and there was reported haze in the area, which could have affected the pilots' ability to see each other.
Probable cause:
The failure of both pilots to see and avoid the other airplane as they converged on intersecting runways. Contributing to the accident was the jet pilot's not monitoring the airport's traffic advisory frequency, known reduced visibility of the intersecting runways, and hazy weather condition.
Final Report:

Crash of a Beechcraft C99 Airliner in Hastings

Date & Time: Mar 16, 2018 at 0750 LT
Type of aircraft:
Operator:
Registration:
N213AV
Flight Type:
Survivors:
Yes
Schedule:
Omaha – Hastings
MSN:
U-213
YOM:
1983
Flight number:
AMF1696
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
6500
Captain / Total hours on type:
1145.00
Copilot / Total flying hours:
853
Copilot / Total hours on type:
21
Aircraft flight hours:
17228
Circumstances:
According to the operator's director of safety, during landing in gusty crosswind conditions, the multi-engine, turbine-powered airplane bounced. The airplane then touched down a second time left of the runway centerline. "Recognizing their position was too far left," the flight crew attempted a go-around. However, both engines were almost at idle and "took time to spool back up." Without the appropriate airspeed, the airplane continued to veer to the left. A gust under the right wing "drove" the left wing into the ground. The airplane continued across a grass field, the nose landing gear collapsed, and the airplane slid to a stop. The airplane sustained substantial damage to the fuselage and left wing. The director of safety reported that there were no preaccident mechanical failures or malfunctions with the airplane that would have precluded normal operation. The automated weather observation system located at the accident airport reported that, about the time of the accident, the wind was from 110° at 21 knots, gusting to 35 knots. The pilot landed on runway 04. The Beechcraft airplane flight manual states the max demonstrated crosswind is 25 knots. Based on the stated wind conditions, the calculated crosswind component was 19 to 33 knots.
Probable cause:
The pilot's decision to land in a gusty crosswind that exceeded the airplane's maximum demonstrated crosswind and resulted in a runway excursion.
Final Report:

Crash of a Pilatus PC-6/B2-H2 Turbo Porter in Grenoble

Date & Time: Mar 15, 2018 at 1215 LT
Registration:
F-BTCG
Flight Type:
Survivors:
Yes
Schedule:
Grenoble - Grenoble
MSN:
551
YOM:
1963
Location:
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2000
Captain / Total hours on type:
500.00
Aircraft flight hours:
12260
Circumstances:
The pilot, accompanied by an aircraft mechanic, departed Grenoble-Aples-Isère Airport (saint-Geoirs) to carry out a check flight following a maintenance operation on the airplane. Once in an open area south of the aerodrome, the pilot began the maneuvers provided for in the test program. At the end of a stall maneuver, he found that his actions on the rudder pedals have no effect. However, it maintained control of the ailerons and elevators. He informed the aerodrome controller of the problem and indicated that he was coming back to to land to the paved runway 09. Unable to determined the exact nature of the damage, the pilot chose to land with the flaps retracted. He managed with difficulty to aligne the airplane witn the runway 09 centerline. On final, at an altitude of 300 feet, the pilot changed his mind and decided to land on the unpaved right-hand runway 09 which adjoins the paved runway. On very short final, at flare, while reducing power, at a height of about 1-2 metres, the airplane rolled to the right then to the left, causing the wing tips and the propeller to struck the ground. The aircraft exited the unpaved runway to the left and came to rest on the right edge of the paved runway. Both occupants evacuated safely and the aircraft was damaged beyond repair.
Probable cause:
The rudder control broke in flight, causing a significant alteration of the aircraft yaw controllability. This failure considerably increased the pilot's workload and stress. In these conditions, it became difficult for him to keep the airplane aligned with the runway centreline upon landing. Monitoring the alignment of the aircraft was done to the detriment of the speed. It is very likely that the oscillations during the final step resulted from a stall of the aircraft at low speed.
Final Report:

Crash of a Beechcraft B200 Super King Air in Blue Creek

Date & Time: Mar 15, 2018 at 0200 LT
Operator:
Registration:
YV3284
Flight Type:
Survivors:
Yes
MSN:
BB-1277
YOM:
1987
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
By night, the pilot attempted to land in a prairie located in Blue Creek, west Belize. The airplane belly landed and slid for few dozen metres before coming to rest, almost broken in two. The pilot leaved the scene but was quickly arrested by the local police. It is believed that it was an illegal flight as the registration on the aircraft (YV3224) is wrong. It appears that the correct registration was YV3284.

Crash of a De Havilland DHC-8-Q402 Dash-8 in Kathmandu: 51 killed

Date & Time: Mar 12, 2018 at 1419 LT
Operator:
Registration:
S2-AGU
Survivors:
Yes
Schedule:
Dhaka - Kathmandu
MSN:
4041
YOM:
2001
Flight number:
BS211
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
67
Pax fatalities:
Other fatalities:
Total fatalities:
51
Captain / Total flying hours:
5518
Captain / Total hours on type:
2824.00
Copilot / Total flying hours:
390
Copilot / Total hours on type:
240
Aircraft flight hours:
21419
Aircraft flight cycles:
28649
Circumstances:
On March 12, 2018, a US Bangla Airlines, Bombardier DHC-8-402, S2-AGU, flight number BS211 departed Hazrat Shahjalal International Airport, Dhaka, Bangladesh at 06:51 UTC on a schedule flight to Tribhuvan International Airport (TIA), Kathmandu, Nepal. The aircraft overflew part of Bangladesh and Indian airspace en-route to Nepal. At 0641, Dhaka Ground Control contacted the aircraft requesting for its Bangladesh ADC number which was recently made mandatory a few weeks ago by Bangladesh authority for all international outbound flights. The crew provided the ADC number as 2177 as provided in the Flight Plan. The Ground Controller again asked the crew if they had the ADC for Bangladesh. At 0642, PIC then contacted the Operations to confirm the Bangladesh ADC number. As per the CVR records, changes in the PIC’s vocal pitch and language used indicated that he was agitated and experiencing high levels of stress at the time while communicating with Dhaka Ground Control and airlines operations. The aircraft finally took off at 0651. As the aircraft was in a climb phase, the PIC overheard a communication between Operations and another US Bangla aircraft regarding the fuel onboard but the PIC without verifying whether the message was meant for him or not, engaged in some unnecessary conversation with the Operations staff. The Captain's vocal pitch and language used indicated that he was very much emotionally disturbed and experiencing high level of stress. The aircraft established its first contact with Kathmandu Control at 0752:04. At 0807:49 the First Officer contacted Kathmandu Control and requested for descent. Kathmandu Control gave descend clearance to FL160 with an estimated approach time of 0826 which was acknowledged by the First Officer. At 0810 the flight was handed over to Kathmandu Approach. At 0811, Kathmandu Approach instructed the aircraft to descend to 13,500 ft and hold over GURAS. The crew inserted the HOLD in the Flight Management System. At 0813:41 Kathmandu Approach further instructed the aircraft to reduce its speed and descend to 12500 ft. At 0816 Kathmandu Approach instructed the aircraft to further descend to 11500 ft., and cleared for VOR approach RWY 02 maintaining minimum approach speed. Both the crew forgot to cancel the hold on the FMS as they were engaged in some unnecessary conversation. Upon reaching GURAS, the aircraft turned left to enter the holding pattern over GURAS, it was noticed by PIC and FO and immediately PIC made correction and simultaneously this was alerted to the crew by Approach Control also. Once realizing the aircraft flying pattern and ATC clearance, the PIC immediately selected a heading of 027° which was just 5° of interception angle to intercept the desired radial of 202° inbound to KTM. The spot wind recorded was westerly at 28kt. The aircraft continued approach on heading mode and crossed radial 202° at 7 DME of KTM VOR. The aircraft then continued on the same heading of 027° and deviated to the right of the final approach course. Having deviated to the right of the final approach path, the aircraft reached about 2-3 NM North east of the KTM VOR and continued to fly further northeast. At 0827, Kathmandu Tower (TWR) alerted the crew that the landing clearance was given for RWY 02 but the aircraft was proceeding towards RWY 20. At 0829, Tower Controller asked the crew of their intention to which the PIC replied that they would be landing on RWY 02. The aircraft then made an orbit to the right. The Controller instructed the aircraft to join downwind for RWY 02 and report when sighting another Buddha Air aircraft which was already on final for RWY 02. The aircraft instead of joining downwind leg for RWY 02, continued on the orbit to the right on a westerly heading towards Northwest of RW 20. The controller instructed the aircraft to remain clear of RWY 20 and continue to hold at present position as Buddha air aircraft was landing at RW 02 (from opposite side) at that time. After the landing of Buddha Air aircraft, Tower Controller, at 08:32 UTC gave choice to BS211 to land either at RW 20 or 02 but the aircraft again made an orbit to the right, this time northwest of RWY 20. While continuing with the turn through Southeastern direction, the PIC reported that he had the runway in sight and requested tower for clearance to land. The Tower Controller cleared the aircraft to land but when the aircraft was still turning for the RWY it approached very close to the threshold for RWY 20 on a westerly heading and not aligned with the runway. At 08:33:27 UTC, spotting the aircraft maneuvering at very close proximity of the ground and not aligned with the RWY. Alarmed by the situation, the Tower Controller hurriedly cancelled the landing clearance of the aircraft by saying, "Takeoff clearance cancelled". Within the next 15-20 seconds, the aircraft pulled up in westerly direction and with very high bank angle turned left and flew over the western area of the domestic apron, continued on a southeasterly heading past the ATC Tower and further continued at a very low height, flew over the domestic southern apron area and finally attempted to align with the runway 20 to land. During this process, while the aircraft was turning inwards and momentarily headed towards the control tower, the tower controllers ducked down out of fear that the aircraft might hit the tower building. Missing the control tower, when the aircraft further turned towards the taxi track aiming for the runway through a right reversal turn, the tower controller made a transmission by saying, "BS 211, I say again...". At 08:34 UTC the aircraft touched down 1700 meters down the threshold with a bank angle of about 15 degrees and an angle of about 25 degrees with the runway axis (approximately heading Southeast) and to the left of the center line of runway 20, then veered southeast out of the runway through the inner perimeter fence along the rough down slope and finally stopped about 442 meters southeast from the first touchdown point on the runway. All four crew members (2 cockpit crew and 2 cabin crew) and 45 out of the 67 passengers onboard the aircraft were killed in the accident. Two more passengers succumbed to injury later in hospital during course of treatment. The aircraft caught fire after 6 seconds of touchdown which engulfed major portions of the aircraft.
Probable cause:
The Accident Investigation Commission determines that the probable cause of the accident is due to disorientation and a complete loss of situational awareness in the part of crewmember. Contributing to this the aircraft was offset to the proper approach path that led to maneuvers in a very dangerous and unsafe attitude to align with the runway. Landing was completed in a sheer desperation after sighting the runway, at very close proximity and very low altitude. There was no attempt made to carry out a go around, when a go around seemed possible until the last instant before touchdown on the runway.
The following contributing factors were reported:
- Improper timing of the pre-flight briefing and the commencement of the flight departure in which the operational pre-flight briefing was given in early morning but the flight departure time was around noon and there were four domestic short flights scheduled in between.
- The PIC, who was the pilot flying, seemed to be under stress due to behavior of a particular female colleague in the company and lack of sleep the preceding night.
- A very steep gradient between the crew.
- Flight crew not having practiced visual approach for runway 20 in the simulator.
- A poor CRM between the crew.

An investigation into the captain's behaviour showed that he had history of depression while serving in the Bangladesh Air Force in 1993 and was removed from active duty after evaluation by a psychiatrist. He was re-evaluated by a psychiatrist in January 2002 and was declared to be fit for flying. Examinations in successive annual medical checks were not focused on his previous medical condition of depression, possibly because this was not declared in the self-declaration form for annual medicals. During the flight the captain was irritable, tensed, moody, and aggressive at various times. He was smoking during the flight, contrary to company regulations. He also used foul language and abusive words in conversation with the junior female first officer. He was engaged in unnecessary conversation during the approach, at a time when sterile cockpit rules were in force. The captain seemed very unsecure about his future as he had submitted resignation from this company, though only verbally. He said he did not have any job and did not know what he was going to do for living.
Final Report: