Crash of a Cessna 560 Citation Encore in Upland: 1 killed

Date & Time: Jun 24, 2006 at 2226 LT
Type of aircraft:
Registration:
N486SB
Flight Type:
Survivors:
Yes
Schedule:
San Diego - Upland
MSN:
560-0580
YOM:
2001
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
2951
Captain / Total hours on type:
268.00
Aircraft flight hours:
2513
Circumstances:
The airplane touched down at night about 1,400 feet down the 3,864-foot runway and overran the runway surface, coming to rest about 851 feet beyond the departure end. The pilot was operating the airplane using a single-pilot waiver that he obtained two months prior to the accident. The airplane was certified by the Federal Aviation Administration with a flight crew of two. The pilot was returning from a personal event with his family, and landing at his home airport when the accident occurred. Witnesses stated that the pilot’s approach into the airport was not consistent with previous approaches in which the airplane would touch down directly on the runway numbers. They also stated that they heard the thrust reversers deploy, and then return to the stowed position. The airplane flight manual states that once the thrust reversers have been deployed, a pilot should not attempt to restow the thrust reversers and take off. Two sink rate warnings were issued during the approach to landing which should have alerted the pilot of the unstabilized approach. Performance calculations showed that the airplane would have required an additional 765 to 2,217 feet of runway for a full stop landing.
Probable cause:
The pilot's unstabilized approach to the runway and failure to obtain the proper touchdown point, which resulted in a runway overrun.
Final Report:

Crash of a De Havilland DHC-6 Twin Otter 300 in Jumla: 9 killed

Date & Time: Jun 21, 2006 at 1203 LT
Operator:
Registration:
9N-AEQ
Survivors:
No
Schedule:
Nepālganj – Surkhet – Jumla
MSN:
708
YOM:
1980
Location:
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
9
Aircraft flight hours:
23392
Aircraft flight cycles:
36092
Circumstances:
The twin engine aircraft departed Nepālganj Airport on a domestic service to Jumla with an intermediate stop in Surkhet, carrying six passengers, three crew members and a load consisting of bags containing grains for a total of 941 kilos. While approaching Jumla Airport, the crew was informed that runway 27 was in use with a wind from 240 at 4 knots. For unknown reasons, the captain started the approach to runway 09 at 1201LT. At an excessive speed, he missed the runway, initiated a go-around procedure and passed to the right of the tower. Then, he started a steep turn to the left when the aircraft lost height and speed and crashed in a field located 500 meters east of the airport, bursting into flames. The aircraft was totally destroyed by impact forces and a post crash fire and all 9 occupants were killed.
Probable cause:
The crew's attempt to make a sudden go-around while close to runway 09 threshold with a very low circuit altitude and subsequent attempt to turn in a tight circuit with excessive angle of bank that led to a stall. The aircraft subsequently contacted terrain due to insufficient clearance available for effective stall recovery. The quick decisions to change runway added to the crew workload at a critical period which was aggravated by the breakdown of cockpit discipline. The other contributory factors leading to the accident were:
- Violation of company Standard Operating Procedures by flight crew,
- Insufficient monitoring of its flight training program and line operations by Yeti management,
- Inadequate oversight of Yeti Airlines by CAAN.

Crash of a Boeing 737-301F in East Midlands

Date & Time: Jun 15, 2006 at 0502 LT
Type of aircraft:
Operator:
Registration:
OO-TND
Flight Type:
Survivors:
Yes
Schedule:
Liège - Stansted
MSN:
23515/1355
YOM:
1987
Flight number:
TAY325N
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8325
Captain / Total hours on type:
4100.00
Copilot / Total flying hours:
1674
Copilot / Total hours on type:
1377
Aircraft flight hours:
45832
Aircraft flight cycles:
34088
Circumstances:
On a scheduled cargo flight from Liège Airport to London Stansted Airport the crew diverted to Nottingham East Midlands Airport due to unexpectedly poor weather conditions at Stansted. The weather conditions at EMA required a CAT IIIA approach and landing. On approach, at approximately 500 feet agl, the crew were passed a message by ATC advising them of a company request to divert to Liverpool Airport. The commander inadvertently disconnected both autopilots whilst attempting to reply to ATC. He then attempted to re-engage the autopilot in order to continue the approach. The aircraft diverged to the left of the runway centreline and developed a high rate of descent. The commander commenced a go-around but was too late to prevent the aircraft contacting the grass some 90 m to the left of the runway centreline. The aircraft became airborne again but, during contact with the ground, the right main landing gear had broken off. The crew subsequently made an emergency landing at Birmingham Airport (BHX).
Probable cause:
Causal factors:
1. ATC inappropriately transmitted a company R/T message when the aircraft was at a late stage of a CAT III automatic approach.
2. The commander inadvertently disconnected the autopilots in attempting to respond to the R/T message.
3. The crew did not make a decision to go-around when it was required after the disconnection of both autopilots below 500 ft during a CAT III approach.
4. The commander lost situational awareness in the latter stages of the approach, following his inadvertent disconnection of the autopilots.
5. The co-pilot did not call ‘go-around’ until after the aircraft had contacted the ground.
Contributory factors:
1. The weather forecast gave no indication that mist and fog might occur.
2. The commander re-engaged one of the autopilots during a CAT III approach, following the inadvertent disconnection of both autopilots at 400 feet aal.
3. The training of the co-pilot was ineffective in respect of his understanding that he could call for a go-around during an approach.
Final Report:

Crash of a Beechcraft A90 King Air in Tampa: 1 killed

Date & Time: Jun 12, 2006 at 1235 LT
Type of aircraft:
Operator:
Registration:
N7043G
Flight Type:
Survivors:
Yes
Schedule:
Sarasota - Tampa
MSN:
LM-37
YOM:
1967
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
2120
Captain / Total hours on type:
457.00
Copilot / Total flying hours:
1208
Copilot / Total hours on type:
44
Aircraft flight hours:
15671
Circumstances:
The first officer reported that during cruise flight, both propeller secondary low pitch stop (SLPS) lights illuminated, indicating the SLPS system prevented both propellers from going below the low pitch hydraulic mechanical stop. The right occurred first, then the left approximately 1 minute later. Emergency procedures to correct the condition were ineffective. The right propeller feathered at some point during the flight, and the first officer reported that while operating single engine, they experienced a problem with the propeller governor. The flight proceeded direct to an airport with short runways approximately 3.2 nautical miles (nm) northwest of their present position, rather than to an air carrier airport located 8.5 nm away. The captain entered a close-in right base to runway 35 (2,688 feet long runway), while flying at 155 knots (51 knots above single engine reference speed). He turned onto final approach with the landing gear and flaps retracted, but overshot the runway. The airplane contacted a taxiway near the departure end of intended runway, and then collided with several obstacles before coming to rest at a house located past the departure end of runway 35. A post crash fire consumed the cockpit, cabin, and sections of both wings. Post accident examination of the airframe, engines, and propellers revealed no evidence of preimpact failure or malfunction. No determination was made as to the reason for the annunciation of both SLPS lights.
Probable cause:
The poor in-flight planning decision by the captain for his failure to establish the airplane on a stabilized approach for a forced landing, resulting in the airplane landing on a taxiway near the departure end of the runway. Contributing to the accident were the failure or malfunction of the primary hydraulic low pitch stop of both propellers for undetermined reasons, the excessive approach airspeed and the failure of the captain to align the airplane with the runway for the forced landing.
Final Report:

Crash of a Lockheed C-130H Hercules in Abéché: 5 killed

Date & Time: Jun 11, 2006 at 1830 LT
Type of aircraft:
Registration:
TT-PAF
Flight Type:
Survivors:
Yes
Schedule:
N’Djamena – Abéché
MSN:
5141
YOM:
1988
Country:
Region:
Crew on board:
0
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
5
Circumstances:
In unknown circumstances, the aircraft crashed upon landing at Abéché Airport and came to rest about 200 metres past the runway end, bursting into flames. At least five passengers were killed and several others were injured. The aircraft was destroyed. The accident occurred 30 minutes after the airport closing time at 1800LT.

Crash of a Casa NC-212-AB4 Aviocar 200 in Banda Neira

Date & Time: Jun 5, 2006 at 1013 LT
Type of aircraft:
Operator:
Registration:
PK-NCL
Survivors:
Yes
Schedule:
Ambon - Bandanaira
MSN:
185/34N
YOM:
1981
Flight number:
MZ9971
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
15
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
After landing on wet runway 10/28 at Banda Neira Airport, the aircraft slid then veered off runway to the right. While contacting soft ground, the undercarriage collapsed and the aircraft came to rest, broken in two. All 18 occupants escaped with minor injuries. The accident occurred in heavy rain falls.

Crash of a Douglas DC-10-10F in Managua

Date & Time: Jun 4, 2006 at 0510 LT
Type of aircraft:
Operator:
Registration:
N68047
Flight Type:
Survivors:
Yes
Schedule:
Miami - Managua
MSN:
47801/98
YOM:
1973
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The aircraft departed Miami-Intl Airport on a night cargo flight to Managua, carrying three crew members and a load consisting of 50 tons of chemical and toxic products. After touchdown on runway 09 which is 2,450 metres long, the aircraft was unable to stop within the remaining distance. It overran, went through a fence, lost its nose gear and came to rest 350 metres further in trees. All three crew members escaped uninjured while the aircraft was damaged beyond repair.

Crash of a Learjet 35A off Groton: 2 killed

Date & Time: Jun 2, 2006 at 1440 LT
Type of aircraft:
Operator:
Registration:
N182K
Survivors:
Yes
Schedule:
Atlantic City - Groton
MSN:
35-293
YOM:
1980
Crew on board:
2
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
18750
Captain / Total hours on type:
7500.00
Copilot / Total flying hours:
3275
Copilot / Total hours on type:
289
Aircraft flight hours:
11704
Circumstances:
The crew briefed the Instrument Landing System approach, including the missed approach procedures. Weather at the time included a 100-foot broken cloud layer, and at the airport, 2 miles visibility. The approach was flown over water, and at the accident location, there was dense fog. Two smaller airplanes had successfully completed the approach prior to the accident airplane. The captain flew the approach and the first officer made 100-foot callouts during the final descent, until 200 feet above the decision height. At that point, the captain asked the first officer if he saw anything. The first officer reported "ground contact," then noted "decision height." The captain immediately reported "I got the lights" which the first officer confirmed. The captain reduced the power to flight idle. Approximately 4 seconds later, the captain attempted to increase power. However, the engines did not have time to respond before the airplane descended into the water and impacted a series of approach light stanchions, commencing about 2,000 feet from the runway. Neither crew member continued to call out altitudes after seeing the approach lights, and the captain descended the airplane below the decision height before having the requisite descent criteria. The absence of ground references could have been conducive to a featureless terrain illusion in which the captain would have believed that the airplane was at a higher altitude than it actually was. There were
no mechanical anomalies which would have precluded normal airplane operation.
Probable cause:
The crew's failure to properly monitor the airplane's altitude, which resulted in the captain's inadvertent descent of the airplane into water. Contributing to the accident were the foggy weather conditions, and the captain's decision to descend below the decision height without sufficient visual cues.
Final Report:

Crash of a BAe 3101 Jetstream 31EP in Bocas del Toro

Date & Time: Jun 1, 2006 at 0755 LT
Type of aircraft:
Operator:
Registration:
HP-1477PST
Survivors:
Yes
Schedule:
Panama City - Bocas del Toro
MSN:
760
YOM:
1985
Flight number:
PST680
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
16
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Following an uneventful flight from Panama City, the crew completed the approach and landing at Bocas del Toro Airport. After touchdown on a wet runway following heavy rain falls, the aircraft was unable to stop within the remaining distance. It overran, lost its undercarriage and came to rest in bushes. All occupants were rescued, among them few were slightly injures. The aircraft was damaged beyond repair.

Crash of a Piper PA-464-310P Malibu in Abbeville

Date & Time: May 26, 2006 at 0835 LT
Operator:
Registration:
F-GOSD
Flight Type:
Survivors:
Yes
Schedule:
Toussus-le-Noble – Fairoaks
MSN:
46-8508099
YOM:
1985
Location:
Country:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
737
Captain / Total hours on type:
230.00
Circumstances:
The single engine aircraft departed Toussus-le-Noble Airport in the early morning on a private flight to Fairoaks with two people on board. About 40 minutes into the flight, at an altitude of 18,000 feet, the manifold pressure dropped from 30 to 28 inches of mercury. The pilot increased the engine power when the manifold pressure boosted to 33 inches of mercury then dropped again. Suddenly, a burning smell pervades the cabin. The pilot declared an emergency and elected to divert to Abbeville Airport which was at a distance of 15 NM from his position. While descending, he lowered the landing gear and reduced the engine power. Shortly before reaching FL100, the oil pressure warning light came on, the engine started to vibrate then stopped. At this time, the aircraft was 10 NM from Abbeville Airport, descending in IMC conditions. On short final, at a height of 300 feet, the pilot established a visual contact with the runway but his trajectory was too short. The aircraft crash landed in a field and came to rest 200 metres short of runway 20. Both occupants escaped uninjured while the aircraft was damaged beyond repair.
Probable cause:
Examination of the engine revealed a tightening defect in the connecting rod heads. The rupture of one of them caused a loss of oil pressure and damage to the movable coupling of the engine, which had been subject to repairs in March 2000 following a belly landing.
Final Report: