Crash of an Ilyushin II-76TD in Kandahar

Date & Time: Feb 14, 2008
Type of aircraft:
Registration:
UN-76020
Flight Type:
Survivors:
Yes
MSN:
00434 50493
YOM:
1984
Country:
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Upon landing at Kandahar Airport, the engine n°1 exploded and caught fire. The crew was able to stop the aircraft and to evacuate the cabin. The left wing and wing root suffered fire damage.

Crash of a BAe 3103 Jetstream 31 in Los Roques

Date & Time: Feb 13, 2008 at 0920 LT
Type of aircraft:
Operator:
Registration:
YV186T
Survivors:
Yes
Schedule:
Porlamar - Los Roques
MSN:
616
YOM:
1983
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
14
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Upon landing at Los Roques Airport, the left main gear collapsed. The aircraft veered off runway to the left and came to rest on the edge of a lagoon. All 16 occupants escaped uninjured while the aircraft was damaged beyond repair.
Probable cause:
Failure of the left main gear upon landing for unknown reasons.

Crash of a Britten-Norman BN-2A-26 Islander in Anguilla

Date & Time: Feb 2, 2008 at 1420 LT
Type of aircraft:
Operator:
Registration:
VP-AAG
Flight Type:
Survivors:
Yes
Schedule:
Anguilla - Sint Maarten
MSN:
88
YOM:
1969
Country:
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4217
Captain / Total hours on type:
693.00
Circumstances:
The commander intended to fly the BN-2 Islander aircraft from Anguilla Wallblake International Airport (AXA) to the neighbouring island of St Maarten (SXM) to await cargo inbound on another flight. The cabin of the aircraft was configured for cargo operations with no passenger seats fitted, as the only other planned occupant was the operator’s Chief Engineer, who would be sitting beside the commander in the right hand seat. However, the commander asked the operator if he could take a family member with him to SXM. The operator agreed and an extra seat was fitted. Witnesses stated that the commander appeared "rushed" prior to departure. The commander stated that he partially carried out the normal pre-flight inspection. He then started the engines. Before taxiing he realised that the nose landing gear chocks were still in place so he shut down the left hand engine, removed and stowed the chocks and then restarted the left engine. The aircraft took off from runway 10 at 14:15 hrs. At between 100 ft and 150 ft the commander initiated a left turn but after some initial movement the ailerons jammed. When he discovered that he was unable to straighten the ailerons he attempted to return to land on runway 10. The other flight controls did not appear to be restricted. With the ailerons jammed, the aircraft continued to turn to the left, losing altitude as it flew over a settlement to the north of the aerodrome, until pointed directly at the Air Traffic Control tower, causing the Air Traffic Control Officer (ATCO) to abandon the tower. The commander judged that the aircraft was too fast and high to attempt a landing and therefore initiated a go-around, applying full power. He continued the left turn, losing height and speed to position the aircraft for another approach but, as the aircraft descended over the northern edge of the runway, its left wing struck the perimeter fence. On impact the aircraft spun about its vertical axis with its wings level and continued sliding sideways on its right side for approximately 80 ft before coming to rest facing north-west.
Probable cause:
The commander was probably distracted from his normal duties whilst arranging additional seating to accommodate the second passenger. He did not complete the requisite pre-flight check or the subsequent check of full and free movement of the flight controls, either of which would have revealed an obstruction to proper operation of the ailerons.
Final Report:

Crash of a Beechcraft C90A King Air in Mount Airy: 6 killed

Date & Time: Feb 1, 2008 at 1128 LT
Type of aircraft:
Registration:
N57WR
Flight Type:
Survivors:
No
Schedule:
Cedartown - Mount Airy
MSN:
LJ-1678
YOM:
2003
Crew on board:
1
Crew fatalities:
Pax on board:
5
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
780
Aircraft flight hours:
800
Circumstances:
While flying a non precision approach, the pilot deliberately descended below the minimum descent altitude (MDA) and attempted to execute a circle to land below the published circling minimums instead of executing the published missed approach procedure. During the circle to land, visual contact with the airport environment was lost and engine power was never increased after the airplane had leveled off. The airplane decelerated and entered an aerodynamic stall, followed by an uncontrolled descent which continued until ground impact. Weather at the time consisted of rain, with ceilings ranging from 300 to 600 feet, and visibility remaining relatively constant at 2.5 miles in fog. Review of the cockpit voice recorder (CVR) audio revealed that the pilot had displayed some non professional behavior prior to initiating the approach. Also contained on the CVR were comments by the pilot indicating he planned to descend below the MDA prior to acquiring the airport visually, and would have to execute a circling approach. Moments after stating a circling approach would be needed, the pilot received a sink rate aural warning from the enhanced ground proximity warning system (EGPWS). After several seconds, a series of stall warnings was recorded prior to the airplane impacting terrain. EGPWS data revealed, the airplane had decelerated approximately 75 knots in the last 20 seconds of the flight. Examination of the wreckage did not reveal any preimpact failures or malfunctions with the airplane or any of its systems. Toxicology testing detected sertraline in the pilot’s kidney and liver. Sertraline is a prescription antidepressant medication used for anxiety, obsessive-compulsive disorder, panic disorder, posttraumatic stress disorder, and social phobia. The pilot’s personal medical records indicated that he had been treated previously with two other antidepressant medications for “anxiety and depression” and a history of “impatience” and “compulsiveness.” The records also documented a diagnosis of diabetes without any indication of medications for the condition, and further noted three episodes of kidney stones, most recently experiencing “severe and profound discomfort” from a kidney stone while flying in 2005. None of these conditions or medications had been noted by the pilot on prior applications for an airman medical certificate. It is not clear whether any of the pilot’s medical conditions could account for his behavior or may have contributed to the accident.
Probable cause:
The pilot's failure to maintain control of the airplane in instrument meteorological conditions. Contributing to the accident were the pilot's improper decision to descend below the minimum descent altitude, and failure to follow the published missed approach procedure.
Final Report:

Crash of a Boeing 727-259 in Trinidad

Date & Time: Feb 1, 2008 at 1035 LT
Type of aircraft:
Operator:
Registration:
CP-2429
Survivors:
Yes
Schedule:
La Paz – Cobija
MSN:
22475/1690
YOM:
1980
Country:
Crew on board:
8
Crew fatalities:
Pax on board:
151
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
Following an uneventful flight from La Paz, the crew started the descent to Cobija Airport when he was informed by ATC that a landing was impossible due to poor weather conditions at destination. The crew decided to divert to the Trinidad-Jorge Heinrich Arauz Airport which is located about 600 km southeast of Cobija Airport. On final approach to Trinidad Airport, the crew reported technical problems and was forced to attempt an emergency landing. The aircraft crash landed in a dense wooded and marshy area located 4 km short of runway. All 159 occupants were rescued but the aircraft was damaged beyond repair.
Probable cause:
The crew was forced to attempt an emergency landing due to fuel exhaustion. The crew decided to divert to Trinidad Airport which is located 600 km southeast of Cobija Airport while weather conditions were considered as good at Rio Branco Airport located 160 km northeast of Cobija.

Crash of a Grumman G-21A Goose off Marathon

Date & Time: Jan 29, 2008 at 1723 LT
Type of aircraft:
Registration:
N21A
Flight Type:
Survivors:
Yes
Schedule:
Marathon - Marathon
MSN:
B129
YOM:
1946
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
16000
Captain / Total hours on type:
100.00
Aircraft flight hours:
24456
Circumstances:
On January 29, 2008, about 1723 eastern standard time, a Grumman G-21A, amphibian airplane N21A, impacted the ocean during landing near Marathon, Florida. The certificated airline transport pilot and passenger received serious injuries and the airplane sustained substantial damage. The flight was operated as a personal flight under the provisions of 14 Code of Federal Regulations (CFR) Part 91, and no flight plan was filed. Visual meteorological conditions prevailed at the time of the accident. The flight departed from the Florida Keys Marathon Airport (MTH) in Marathon, Florida, on January 29, 2008, about 1615. According to the pilot he departed MTH and after take off and the checklist accomplished he proceeded in a westerly direction to inspect a water-work area. The pilot stated that other then that, he had no further recollection of the flight. According to the Federal Aviation Administration (FAA) the passenger stated that the pilot was practicing takeoffs and landings. During a water landing, the left wing contacted the water and the airplane water looped. A Good Samaritan rescued them from the water in his boat and brought them ashore where rescue personal were waiting. Examination of the airplane by the FAA revealed no mechanical malfunctions or failures of the airplane or engine, and none were reported by the pilot or passenger.
Probable cause:
The pilot’s failure to maintain control of the airplane during a water landing.
Final Report:

Crash of a De Havilland DHC-8-202 in Bogotá

Date & Time: Jan 28, 2008 at 2302 LT
Operator:
Registration:
HK-3997
Survivors:
Yes
Schedule:
Maracaibo – Bogotá
MSN:
391
YOM:
1994
Flight number:
ARE053
Country:
Crew on board:
4
Crew fatalities:
Pax on board:
37
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
14992
Captain / Total hours on type:
5552.00
Copilot / Total flying hours:
555
Copilot / Total hours on type:
6
Aircraft flight hours:
19565
Circumstances:
Following an uneventful flight from Maracaibo, the crew completed a night approach and landing on runway 13L at Bogotá-El Dorado Airport. After touchdown, the crew initiated the braking procedure but due to a technical issue on the left engine, the aircraft was unable to stop within the remaining distance. It overran, went through a perimeter fence and came to rest in a grassy area with its left main gear folded. All 41 occupants were evacuated, among them two passengers were seriously injured. The aircraft was damaged beyond repair.
Probable cause:
Carrying out a landing with an unresolved issue on the left engine, causing the aircraft to be unable to stop within the remaining distance available. The failure to correct the maintenance reports in a satisfactory manner and the failure to properly follow-up on repetitive entries were considered as contributing factors.
Final Report:

Crash of a Casa 212 Aviocar 200 in Long Apung: 3 killed

Date & Time: Jan 26, 2008 at 0936 LT
Type of aircraft:
Operator:
Registration:
PK-VSE
Flight Type:
Survivors:
No
Schedule:
Tarakan – Long Apung
MSN:
412/92N
YOM:
1993
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
21019
Captain / Total hours on type:
14234.00
Copilot / Total flying hours:
16849
Copilot / Total hours on type:
16849
Aircraft flight hours:
11750
Aircraft flight cycles:
13749
Circumstances:
On 26 January 2008, a Casa 212-200 aircraft, registered PK-VSE, was being operated by PT. Dirgantara Air Service as a cargo charter flight from Tarakan Airport to Long Apung Airport. There were 3 persons on board; two pilots and one aircraft maintenance engineer/load master. The aircraft was certified as being airworthy prior to departure. The aircraft departed from Tarakan at 0011 UTC (08:11 local time), and the estimated time arrival at Long Apung was 0136. At 0411 the pilot of another aircraft received a distress signal and informed air traffic services at Tarakan. Searchers subsequently found the aircraft wreckage at an elevation of 2,766 feet, about 3.4 NM from Long Apung Airport. The coordinates of the accident site were 01° 39.483′ S and 115° 00.265′ E near Lidung Payau Village, Malinau, East Kalimantan. The accident site was on the left downwind leg of the runway 35 circuit.
Probable cause:
The following findings were identified:
• The aircraft was certified as being airworthy prior to departure.
• All crew members held appropriate and valid flight crew licenses.
• The pilots continued flight into instrument meteorological conditions.
• The aircraft impacted terrain in controlled flight.
• The cargo was not adequately restrained.
Causes:
The crew did not appear to have awareness of the aircraft’s proximity with terrain until impact with terrain was imminent. The pilot attempted to continue the flight in instrument meteorological
conditions, below the lowest safe altitude.
Final Report:

Crash of a Casa C-295M in Mirosławiec: 20 killed

Date & Time: Jan 23, 2008 at 1907 LT
Type of aircraft:
Operator:
Registration:
019
Flight Type:
Survivors:
No
Schedule:
Warsaw– Powidz – Poznań-Krzesiny – Mirosławiec – Świdwin – Krakow
MSN:
S-043
YOM:
2007
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
16
Pax fatalities:
Other fatalities:
Total fatalities:
20
Aircraft flight hours:
300
Circumstances:
The aircraft departed Warsaw at 1651LT on a flight to Krakow with intermediate stops in Powidz, Poznań-Krzesiny, Mirosławiec and Świdwin, carrying 36 passengers and a crew of four. They were returning to their base after intending the 50th Annual Aviation Safety Conference held in Warsaw. Nine passengers deplaned at Powidz and 11 others at Poznań-Krzesiny AFB. On approach to Mirosławiec by night, the crew encountered poor weather conditions with a ceiling at 300 feet, visibility 2 sm and mist. On short final, the aircraft was unstable. With a rate of descent of 6,000 feet per minute and at a speed of 148 knots, the aircraft impacted trees and crashed in a wooded area located 1,300 metres short of runway threshold, bursting into flames. The aircraft was totally destroyed and all 20 occupants were killed.
Crew:
Maj Jarosław Haładus,
Adj Robert Kuźma,
Adj Michał Smyczyński,
Sgt Janusz Adamczyk.
Passengers:
Gen Brig Andrzej Andrzejewski,
Col Dariusz Maciąg,
Col Jerzy Piłat,
Lt Col Wojciech Maniewski,
Lt Col Zbigniew Książek,
Lt Col Dariusz Pawlak,
Lt Col Zdzisław Cieślik,
Maj Robert Maj,
Maj Mirosław Wilczyński,
Maj Grzegorz Jułga,
Maj Piotr Firlingier,
Maj Krzysztof Smołucha,
Cpt Karol Szmigiel,
Cpt Paweł Zdunek,
Cpt Leszek Ziemski,
Cpt Grzegorz Stepaniuk,

Probable cause:
Inadvertent loss of spatial and situational awareness by the aircraft crew during final stages of PAR approach, which, within 12 seconds period before crash, resulted in the aircraft’s bank increasing unmonitored and accompanying altitude loss, while the flight crew apparently was trying to establish visual contact with runway and approach lights.

Among the secondary causes the Board listed:
- Improper flight crew selection for the flight:
- The PIC did not have any previous experience on this version of CASA C-295 aircraft, which was additionally equipped with 2 IRS/GPS LN-100G units instead of 2 TOPSTAR 100-2 GPS receivers, and, ironically, with EGPWS Mk. V - unfortunately lack of cryptographic modules in GPS receivers, which made IRS/GPS LN-100G system almost useless (IRS alone with no GPS enhancement) caused flight crew to use handheld GPS receivers (Garmin GPSMAP 196),
- The SIC was not rated in CASA C-295 aircraft for night/IMC operations,
- Poor flight crew coordination and cooperation (poor MCC & CRM):
- improper altimeter setting procedures,
- probably both pilots were looking for visual cues and nobody was observing flight instruments in the very last seconds before they crash),
- Poor weather conditions in vicinity of Miroslawiec AB; ceiling 300 feet, visibility 2 sm, in mist. Icing was excluded as a factor.
- Spatial disorientation of the flight crew,
- EGPWS Audio warning was inhibited (the flight crew missed EGPWS test before departure from Warsaw, even though it was a checklist item, and never corrected the problem - the PIC was not familiar with the system - he has never flown before CASA C-295M equipped with EGPWS) - in result no audio warning of excessive bank angle, high terrain closure rate and high sink rate was available to the flight crew, as well as no automatic height above ground callouts were given,
- The flight crew failed to monitor radio-altimeter indication during both approaches,
- Both pilots concentrated their attention outside of the cockpit during final seconds before crash and did not scan flight instruments.
- The military PAR controller did a poor job during the approach, he let for the non-stabilized approach, he was not compensating properly for left crosswind of 20 kts and allowed the aircraft to stay high above glide slope during both PAR approaches, he also was not fully aware of altimeter setting (QNH or QFE) and altitude reports by flight crew– improper values QNH/QFE were used by the flight crew during first approach, additionally PIC has set his altimeter to QFE, while SIC to QNH. During the approach the controller’s instructions were hesitant and inconsistent, probably making the flight crew to believe their approach was going well.
- The military PAR controller was giving improper suggestions to the flight crew - he was questioning them during final stage of approach whether they see approach or runway lights or not, instead of continuous talking them down to the runway threshold,
- Altimeter indications were improperly interpreted by the flight crew,
- Improperly performed search for visual contact by the flight crew during final stage of approach,
- Improper, lacking weather situation analysis performed by the PIC before the flight,
- The flight crew did not properly set DH/MDA (they did the same error on previous two legs before crash).

Contributing factors were:
- The SIC was not rated in CASA C-295 aircraft for night/IMC operations (the SIC total flight time was 800 hours including 100 hours in CASA C-295M),
- The PIC has no previous experience on the accident version of CASA C-295 aircraft, (although he logged 800+ hours in another version of CASA C-295M aircraft used by Polish AF and his total flight time was 2500 hours),
- Because of lack of GPS enhancement to IRS, the flight crew used Garmin GPSMAP 196 handheld GPS receiver,
- The PIC had no previous experience in PAR approaches in IMC, close to minimums, which in Miroslawiec AB were reported to be aprox. ceiling 270 feet and visibility of 3300 feet,
- The military PAR controller had no previous experience in conducting PAR approaches of aircraft other than Sukhoi Su-22,
- The aircraft was improperly vectored to final approach by military APP controller (the same person performing PAR controller duties) which resulted in rushed, non-stabilized first approach, because the aircraft started descent on final approach segment being twice as high as glide slope,
- Lack of instrument approach procedures meeting ICAO standards at Polish military airports, including Miroslawiec AB, published in Aeronautical Information Publication (AIP),
- Use of different units by pilots and controller (the aircraft’s altimeters were scaled in feet and hPa, while the controller was using meters and millimeters of Hg, there was also misunderstanding regarding use of QNH and QFE),
- Even though the aircraft was equipped with ILS receiver, the ILS equipment at Miroslawiec AB was inoperative (it was installed in 2001, but since then has never worked properly, and therefore was not used, despite several repair attempts - now, 2 months after the crash, it is reported to work properly - the crew had available only military PAR (unable to meet ICAO standards), assisted with 2 military NDBs located 4 km and 1 km from the threshold of runway 30),
- The information on minimum weather conditions and available navaids in Miroslawiec AB were improperly disseminated (dispatch personnel had no information the ILS in Miroslawiec AB was inoperative).

Crash of a Piper PA-46-500TP Malibu Meridian in San Antonio: 1 killed

Date & Time: Jan 18, 2008 at 1230 LT
Registration:
N169CA
Flight Type:
Survivors:
No
Schedule:
Waco – San Antonio
MSN:
46-97300
YOM:
2007
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1049
Captain / Total hours on type:
58.00
Aircraft flight hours:
111
Circumstances:
The pilot attempted to intercept an instrument landing system localizer three times without success. The pilot told Air Traffic Approach Control that he was having trouble performing a "coupled" approach and that he was trying to "get control" of the airplane. The airplane disappeared from radar, subsequently impacting a field and then a barn. The airplane came to rest in an upright position and a post crash fire ensued. A review of radar and voice data for the flight revealed that during the three approach attempts the pilot was able to turn to headings and climb to altitudes when assigned by air traffic control. Postmortem toxicology results were consistent with the regular use of a prescription antidepressant, and the recent use of a larger-than-maximal dose of an over-the-counter antihistamine known to cause impairment. There were no preimpact anomalies observed during the airframe and engine examinations that would have prevented normal operation.
Probable cause:
The pilot's failure to execute an instrument approach. Contributing to the accident was the pilot's impairment due to recent use of over-the-counter medication.
Final Report: