Crash of a Rockwell Aero Commander 560A in Davis: 2 killed

Date & Time:
Operator:
Registration:
N91NR
Flight Phase:
Survivors:
No
Schedule:
Berkley Springs - Charleston
MSN:
560-234
YOM:
1955
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
3096
Captain / Total hours on type:
457.00
Circumstances:
En route from Berckley Springs to Charleston, while in normal cruise, both engines failed. The crew elected to make an emergency landing when control was lost. The airplane crashed and was destroyed upon impact, killing both occupants.
Probable cause:
Uncontrolled descent following a double engine failure caused by a fuel exhaustion. The following contributing factors were reported:
- Inadequate preflight preparation,
- Mismanagement of fuel,
- Fuel exhaustion,
- Failed to maintain flying speed,
- Failure to provide adequate directives, manual, equipment,
- Fuel gauge read approximately 10 gallons high,
- Did not use positive method for checking fuel.
Final Report:

Crash of a Rockwell Grand Commander 680F in Fort Myers: 1 killed

Date & Time:
Registration:
N770W
Flight Type:
Survivors:
No
MSN:
680-1038-54
YOM:
1961
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
5202
Circumstances:
On approach to Fort Myers-Page Field Airport, one of the engine failed. The airplane lost height, hit power cables and crashed few miles short of runway. The aircraft was destroyed and the pilot, sole on board, was killed.
Probable cause:
Engine malfunction on approach following a fuel starvation. The following contributing factors were reported:
- Collision with wires/poles,
- Improper in-flight decisions,
- Mismanagement of fuel,
- Inattentive to fuel supply,
- Fuel starvation,
- High obstructions,
- Fuel selectors on LH and RH outboard wing tanks, no fuel in these tanks.
Final Report:

Crash of a Rockwell Aero Commander 560 in Skaneateles: 1 killed

Date & Time:
Operator:
Registration:
N2692B
Flight Phase:
Survivors:
No
Schedule:
Skaneateles – Salisbury – Wilmington
MSN:
560-192
YOM:
1955
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
11200
Captain / Total hours on type:
3300.00
Circumstances:
Just after liftoff at Skaneateles Airstrip, the twin engine airplane touched the runway and drifted to the left, causing the left main gear to struck a snowbank. The takeoff was continued when the airplane went out of control and rolled inverted. The pilot, sole on board, was killed.
Probable cause:
Ground loop during takeoff run after the pilot diverted attention from operation of aircraft. The following contributing factors were reported:
- Failed to maintain directional control,
- Failed to abort takeoff,
- Failed to follow approved procedures,
- Airport conditions.
Final Report:

Crash of a Beechcraft TC-45G Expeditor in El Vado

Date & Time:
Type of aircraft:
Operator:
Registration:
N9907Z
Flight Type:
Survivors:
Yes
MSN:
AF-105
YOM:
1952
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
After landing on a snow covered runway, the twin engine airplane ground looped, hit a barrel and came to rest. The aircraft was set afire and destroyed and the pilot disappeared. Transport of contraband.
Probable cause:
Ground looped after the pilot failed to maintain directional control on a snow covered runway. Illegal flight.
Final Report:

Crash of a Learjet 24A in Anchorage: 6 killed

Date & Time:
Type of aircraft:
Registration:
N651LJ
Survivors:
Yes
Schedule:
Deadhorse - Anchorage
MSN:
24-125
YOM:
1966
Crew on board:
2
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
6
Captain / Total flying hours:
9832
Captain / Total hours on type:
321.00
Circumstances:
During a final approach completed in limited visibility due to low clouds and fog, the crew failed to realize that his altitude was too low when the airplane struck the ground and crashed 914 metres short of runway threshold. Both pilots and four passengers were killed while two other passengers were seriously injured.
Probable cause:
Controlled flight into terrain on final approach due to improper IFR operation. The following contributing factors were reported:
- Improper in-flight decisions,
- Inadequate preflight preparation,
- Low ceiling,
- Fog,
- Visibility 1/4 mile or less,
- Pilot descended below published minimums,
- Low fuel state,
- Did not refuel before takeoff,
- Overflew suitable airports.
Final Report:

Crash of a Rockwell Grand Commander 680 in Owensville: 1 killed

Date & Time:
Registration:
N108E
Flight Phase:
Survivors:
No
Schedule:
Saint Louis - Vichy
MSN:
680-954-19
YOM:
1960
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
1126
Captain / Total hours on type:
180.00
Circumstances:
While cruising in poor weather conditions (fog and rain), the pilot lost control of the airplane that entered a spin and crashed in a field. The pilot, sole on board, was killed.
Probable cause:
Uncontrolled descent after the pilot suffered a spatial disorientation in flight following a failure of the electrical system (inverter). The following contributing factors were reported:
- Rain,
- Fog,
- The two aircraft inverters were not rotating at impact,
- Instrument fragmentation precluded instrument investigations.
Final Report:

Crash of a Rockwell Grand Commander 680 in Pagosa Springs: 4 killed

Date & Time:
Registration:
N6221D
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Pagosa Springs - Burbank
MSN:
680-489-159
YOM:
1957
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
1600
Circumstances:
Just after liftoff from Pagosa Springs Airfield, while climbing, the right engine failed. The pilot was able to feather the propeller but the airplane lost height and crashed in flames in a canyon. The aircraft was totally destroyed and all four occupants were killed.
Probable cause:
Powerplant failure for undetermined reasons. The following contributing factors were reported:
- Improper emergency procedures,
- Airport conditions,
- High density altitude,
- Flew into blind canyon,
- Right engine quit, propeller feathered,
- Aircraft hit canyon wall,
- High obstructions at end of runway,
- Density altitude 7,400 feet.
Final Report:

Crash of a Mitsubishi MU-2B-30 near Rollinsville: 9 killed

Date & Time:
Type of aircraft:
Operator:
Registration:
N133MA
Flight Phase:
Survivors:
No
Site:
Schedule:
Denver - Granby
MSN:
506
YOM:
1970
Crew on board:
1
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
9
Captain / Total flying hours:
3885
Captain / Total hours on type:
307.00
Circumstances:
The airplane was completing a charter flight from Denver to Granby on behalf of Conquest Aero Resources. While cruising in poor weather conditions (low clouds and snow falls), the pilot failed to realize his altitude was insufficient when the airplane struck a mountain located near Rollinsville. The wreckage was found two days later, on December 28, and all nine occupants have been killed.
Probable cause:
Controlled flight into terrain after the pilot continued VFR flight into adverse weather conditions. The following contributing factors were reported:
- Improper in-flight decisions,
- Disregard of good operating practice,
- High obstructions,
- Low ceiling,
- Snow,
- Fog.
Final Report:

Crash of a Beechcraft D18S in Bloserville: 1 killed

Date & Time:
Type of aircraft:
Operator:
Registration:
N91A
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Reading - Altoona
MSN:
A-113
YOM:
1946
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
15314
Captain / Total hours on type:
6063.00
Circumstances:
While cruising by night at an insufficient altitude, the twin engine airplane crashed in a field near Bloserville. The aircraft was destroyed and the pilot, sole on board, was killed. He was completing a cargo flight from Reading to Altoona.
Probable cause:
Controlled flight into terrain after the pilot misjudged altitude. The following contributing factors were reported:
- Physical impairment,
- Alcoholic impairment of efficiency and judgment,
- Blood alcohol 0,98‰ .
Final Report:

Crash of a Beechcraft E18S in Kansas City: 2 killed

Date & Time:
Type of aircraft:
Operator:
Registration:
N7010
Flight Type:
Survivors:
No
Schedule:
Lincoln - Kansas City
MSN:
BA-179
YOM:
1956
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
4720
Circumstances:
During a night approach to Kansas City Airport, while on a ferry flight from Lincoln, the airplane went out of control, rolled over and crashed in flames. The aircraft was totally destroyed and both occupants were killed.
Probable cause:
Uncontrolled descent on final approach for undetermined reasons. The following contributing factors were reported:
- Low ceiling,
- Icing conditions including sleet, freezing rain,
- Fog,
- Sound of engine surging heard.
Final Report: