Crash of a Piper PA-31-350 Navajo Chieftain in Springfield: 4 killed

Date & Time: Mar 10, 1979 at 2216 LT
Registration:
N27530
Flight Type:
Survivors:
No
Schedule:
Farmingdale - Springfield
MSN:
31-7852047
YOM:
1978
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
400
Circumstances:
On final approach to Springfield-Hartness State Airport by night and poor weather conditions, the pilot failed to realize his altitude was too low when the airplane struck the ground and crashed. The aircraft was destroyed and all four occupants were killed.
Probable cause:
Controlled collision with ground on final approach due to improper IFR operation. The following contributing factors were reported:
- Low ceiling,
- Rain,
- Fog,
- Visibility down to zero,
- Below minimums weather conditions,
- Published missed approach procedures not followed.
Final Report:

Crash of a Nord 262A-33 off Los Angeles: 3 killed

Date & Time: Mar 10, 1979 at 1752 LT
Type of aircraft:
Operator:
Registration:
N418SA
Flight Phase:
Survivors:
Yes
Schedule:
Los Angeles - Santa Maria
MSN:
41
YOM:
1967
Flight number:
WI235
Crew on board:
3
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
8500
Captain / Total hours on type:
879.00
Copilot / Total flying hours:
5600
Copilot / Total hours on type:
424
Aircraft flight hours:
11300
Circumstances:
On March 10, 1979, Swift Aire Lines, Inc., Flight 235, an Aerospatiale Nord 262, N418SA, was being operated as a scheduled passenger flight from Los Angeles, California, to Santa Maria, California. About 1745 PST, flight 235 departed the commuter passenger terminal at the Los Angeles International Airport to taxi to the end of runway 24L via the parallel taxiway. The flight was operating on an instrument flight rules (IFR) flight plan; there were four passengers and three crew members on board. At 1748:11, the crew reported that it was ready for takeoff, and at 1749:04, the flight was cleared to taxi into position on runway 24L and hold. At 1749:34, the tower controller cleared the flight for takeoff and cautioned "possible turbulence, preceding heavy departure. You'll be more than 6 miles in trail." The crew acknowledged the clearance and began the takeoff roll. At 1750:27, the flight was changed over to the departure control radio frequency. At 1751:08, the crew of Flight 235 reported, "We got an emergency, we are going down." The departure controller asked if the flight wanted to return to land. At 1751:14, the crew replied, "We lost both of them." Witnesses who were located along the flightpath of the aircraft at the time of the accident stated that when the aircraft lifted off the runway exhaust smoke from both engines was visible, and when the aircraft crossed the departure end of the runway, the right propeller was observed slowing to a stop. As the aircraft crossed the shoreline, popping sounds were heard from the left engine, and the aircraft stopped climbing and turned north paralleling the shoreline. The witnesses did not hear any engine sounds after the aircraft turned parallel to the shoreline. The witnesses also stated that as the aircraft flew north along the shoreline, it descended in a wings-level attitude, it contacted the water smoothly, bounced twice, impacted the water in a nose down attitude, and sank almost immediately. The flight attendant, who was seated in a rear passenger seat during the takeoff, said that she listened to the crew over the intercom until she heard the gear-up call by the captain and that, until the gear-up call, everything had been normal. At that point, she removed her headset. Shortly thereafter, she noticed that there was no engine noise, and she looked out of the window. Seeing that the aircraft was over water, she then briefed the passengers on crash landing and ditching procedures. She stated that before the aircraft struck the water, the crew had given her two aural warnings of an emergency landing. One passenger stated that acceleration was good during the takeoff and climb out to about 300 to 400 ft. Ile said that shortly after he heard the landing gear go up, he heard a pop, and the right engine lost power and stopped running. This was followed by an increase in power on the left engine, and the aircraft continued to climb momentarily. Then, as it leveled off, the left engine quit. He said it appeared that the captain tried to restart the left engine. The accident occurred during the hours of dusk.
Probable cause:
The National Transportation Safety Board determines that the probable cause of the accident was the flightcrew's mismanagement of an emergency procedure following an autofeather of the right propeller which resulted in their shutting down the remaining engine. Contributing to the accident was the unavailability of vital restart information to the crew. The following findings were reported:
- Shortly after landing gear retraction, the right propeller autofeathered and the engine shut down,
- The right engine shutdown was followed closely by the shutdown of the left engine,
- A leak or break in the propeller pressure line to the autofeather selector probably caused the right propeller to autofeather and the engine to shut down,
- The left engine was shut down inadvertently,
- The left engine probably was shut down because the flight crew failed to properly identify the engine on which the autofeather occurred and moved the left power lever to the stop position,
- A possible restart attempt was not successful because the flight crew was probably unaware that feathering the propeller was a prerequisite to a successful airborne restart,
- The engine restart procedures contained in the aircraft operations manual did not contain sufficient information to effect a restart from an unfeathered condition,
- After the left engine was shut down, there was enough altitude and time available for the crew to get a restart,
- The fatalities occurred when the crewmembers and passenger became trapped or disoriented, or both, by the fast, rushing water that entered the aircraft after it was ditched in the Santa Monica Bay.
Final Report:

Crash of a Rockwell Aero Commander 520 off New Orleans: 1 killed

Date & Time: Mar 4, 1979 at 1630 LT
Registration:
N4178B
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
South Bimini – Tampico
MSN:
520-85
YOM:
1953
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
664
Captain / Total hours on type:
12.00
Circumstances:
En route from South Bimini to Tampico, Mexico, the airplane suffered a double engine failure. The pilot ditched the aircraft off New Orleans. Seriously injured, he was rescued but apparently died a week later.
Probable cause:
As the airplane was not recovered, it was not possible to establish the cause of the accident. Illegal flight suspected.
Final Report:

Crash of a Beechcraft 70 Queen Air in Gulfport: 8 killed

Date & Time: Mar 1, 1979 at 1504 LT
Type of aircraft:
Registration:
N777AE
Flight Phase:
Survivors:
No
Schedule:
Gulfport - New Orleans
MSN:
LB-34
YOM:
1970
Crew on board:
1
Crew fatalities:
Pax on board:
7
Pax fatalities:
Other fatalities:
Total fatalities:
8
Captain / Total flying hours:
1528
Captain / Total hours on type:
15.00
Circumstances:
Following takeoff from Gulfport-Biloxi Airport, the twin engine airplane encountered difficulties to gain height and sufficient speed. It stalled then crashed in a marsh located 1,500 feet past the runway end. The aircraft was destroyed and all eight occupants were killed.
Probable cause:
Stall during initial climb after the pilot failed to maintain flying speed. The following contributing factors were reported:
- Improper emergency procedures,
- Inadequate preflight preparation,
- Inadequate inspection of aircraft on part of the maintenance personnel,
- Operational supervisory personnel: deficiency, company maintained equipment, services, regulation,
- Rules, regulations, standards personnel,
- Improperly loaded aircraft,
- Wing flap control system eélectrical,
- Nose baggage door opened during takeoff,
- Starter interrupt system,
- Flaps inoperative,
- Inadequate part 135 training.
Final Report:

Crash of a Beechcraft E18S in Indianapolis

Date & Time: Feb 27, 1979 at 0718 LT
Type of aircraft:
Operator:
Registration:
N711TL
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Indianapolis – Louisville
MSN:
BA-317
YOM:
1957
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1920
Captain / Total hours on type:
100.00
Circumstances:
Just after liftoff at Indianapolis Airport, while in initial climb, the twin engine airplane stalled and crashed. Both occupants were injured and the aircraft was destroyed.
Probable cause:
It was determined that the loss of control was the consequence of wake turbulences coming from a preceding Boeing 727 that just took off from the same runway. Uncontrolled collision with ground due to vortex turbulences.
Final Report:

Crash of a Piper PA-31T Cheyenne I in Baltimore: 3 killed

Date & Time: Feb 23, 1979 at 1958 LT
Type of aircraft:
Operator:
Registration:
N6123A
Flight Type:
Survivors:
Yes
Schedule:
Lynchburg - Baltimore
MSN:
31-7804008
YOM:
1978
Crew on board:
2
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
6522
Captain / Total hours on type:
136.00
Circumstances:
While on approach to Baltimore-Martin State Airport, the crew encountered poor weather conditions. The visibility was reduced to 1/4 of a mile due to low ceiling and fog. On final, the twin engine airplane struck power cables. The captain increased engine power and initiated a go-around before diverting to Baltimore-Washington-Thurgood Marshall International Airport. On approach, while trailing about 1,500 feet of wire, the airplane went out of control and crashed in flames few hundred yards from the runway threshold. A passenger was seriously injured while three other occupants were killed.
Probable cause:
Collision with wires on final approach and subsequent uncontrolled collision with ground due to improper IFR operation. The following contributing factors were reported:
- Foreign material affecting normal operations,
- Low ceiling,
- Fog,
- Visibility about 1/4 mile or less.
Final Report:

Crash of a Beechcraft D18 3NM in Memphis

Date & Time: Feb 23, 1979 at 0040 LT
Type of aircraft:
Registration:
N12VT
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Cedar Rapids - Memphis - Springfield
MSN:
A-780
YOM:
1952
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7300
Captain / Total hours on type:
120.00
Circumstances:
The pilot, sole on board, was completing a night cargo flight from Cedar Rapids to Springfield with an intermediate stop in Memphis. Cleared by ATC to align on runway for takeoff, the pilot increased engine power and entered the runway when the aircraft was struck by a Federal Express (FedEx) Dassault Falcon 20 registered N36FE that just landed on the same runway. The right wing of the Falcon struck the Beechcraft that caught fire instantly. The crew of the Falcon 20 was able to stop normally and the aircraft was slightly damaged. The Beech 18 was destroyed by fire and its pilot evacuated with minor injuries.
Probable cause:
Ground collision between two aircraft after traffic control personnel issued improper or conflicting instructions.
Final Report:

Crash of a Piper PA-31-350 Navajo Chieftain in Claude

Date & Time: Feb 23, 1979 at 0026 LT
Registration:
N61517
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Houma - Amarillo
MSN:
31-7552021
YOM:
1975
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7119
Captain / Total hours on type:
7.00
Circumstances:
While on a night cargo flight from Houma to Amarillo, one of the engine failed due to fuel exhaustion. The pilot reduced his altitude and attempted an emergency landing in a prairie. Upon landing, the airplane collided with fences and came to rest. Both occupants were seriously injured and the aircraft was damaged beyond repair.
Probable cause:
Engine failure in flight due to fuel exhaustion. The following contributing factors were reported:
- Collision with fences,
- Inadequate preflight preparation,
- Mismanagement of fuel,
- Inattentive to fuel supply,
- Fuel exhaustion,
- Hidden obstructions,
- Complete failure on one engine,
- Pilot failed to check quantity of fuel in tanks prior to takeoff.
Final Report:

Crash of a Cessna 421A Golden Eagle I in Kansas City: 3 killed

Date & Time: Feb 22, 1979 at 0955 LT
Type of aircraft:
Registration:
N77PM
Survivors:
No
Schedule:
Des Moines - Kansas City
MSN:
421A-0129
YOM:
1968
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
16000
Captain / Total hours on type:
420.00
Circumstances:
On approach to Kansas City-Charles B. Wheeler-Downtown Airport, the pilot encountered very bad weather conditions with low ceiling, fog and windshear. In a zero visibility, he failed to realize his altitude was too low when the airplane struck trees and crashed in flames few miles short of runway 19 threshold. The aircraft was destroyed upon impact and all three occupants were killed.
Probable cause:
Collision with trees on final approach due to improper IFR operation. The following contributing factors were reported:
- Low ceiling,
- Fog,
- Windshear,
- Visibility at zero.
Final Report:

Crash of a Piper PA-61 Aerostar (Ted Smith Aerostar 601P) near New Braunfels: 2 killed

Date & Time: Feb 17, 1979 at 1435 LT
Operator:
Registration:
N9779Q
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
San Antonio – Lake Charles
MSN:
61-0407-143
YOM:
1977
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
1200
Circumstances:
While in cruising altitude on a flight from San Antonio to Lake Charles, the twin engine airplane went out of control, entered a dive and crashed near New Braunfels, Texas. The aircraft was totally destroyed by impact forces and a post crash fire and both occupants were killed.
Probable cause:
Uncontrolled descent and subsequent ground collision after the pilot attempted operation beyond experience/ability level. The following contributing factors were reported:
- Improper IFR operation,
- Suffered a spatial disorientation,
- One day prior to the accident, flight instructor recommended the pilot not to fly IFR till 10 hours additional dual instruction received.
Final Report: