Crash of a Piper PA-60 Aerostar (Ted Smith 600) in Plymouth: 1 killed

Date & Time: Jul 23, 1990 at 0934 LT
Operator:
Registration:
N8060J
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Detroit – Jackson
MSN:
60-0543-175
YOM:
1978
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
7000
Captain / Total hours on type:
2000.00
Circumstances:
A Piper PA-28, N55354, had departed Plymouth, MI and was climbing from 1,300 feet msl on a course of about 282° with a ground speed of 80 knots. At about the same time, a Piper PA-60, N8060J, was cruising at 2,100 feet msl on a flight from Detroit to Jackson, MI, on a course of about 258° with a ground speed of 165 knots. Subsequently, the 2 aircraft converged and collided at 2,100 feet msl. Both aircraft then plunged to the ground and crashed. Radar data and wreckage exam revealed the PA-60 had converged from the right rear of the PA-28; the PA-28 converged on the PA-60 from its lower, left, forward area. The PA-28 was on an instrument training flight with a rated private pilot and an instructor pilot (cfi) aboard. The investigation did not reveal which seat the cfi was occupying. No flight plan had been filed for either flight, nor was there any indication that either flight crew had obtained ATC/radar assistance. The pilot, sole on board, was killed.
Probable cause:
Inadequate visual lookout by the pilot of the PA-60. A factor related to the accident was that neither of the flight crews had obtained ATC/radar assistance.
Final Report:

Crash of a Boeing 737-222 in Kinston

Date & Time: Jul 22, 1990 at 1455 LT
Type of aircraft:
Operator:
Registration:
N210US
Flight Phase:
Survivors:
Yes
Schedule:
Kinston - Charlotte
MSN:
19555
YOM:
1968
Crew on board:
5
Crew fatalities:
Pax on board:
22
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
10100
Captain / Total hours on type:
3300.00
Aircraft flight hours:
51264
Circumstances:
As engine power was increased for takeoff, the n°1 engine accelerated beyond target epr. Engine shut down had to be done with the fuel shut off lever. The asymmetric thrust was controlled with nose wheel steering. Before the airplane could be stopped the nose wheels separated from the landing gear. The investigation revealed that the fuel pump output spline to the fuel control had stripped. It occurred at such a time that the fuel control sensed an underspeed and increased Fuel flow. Misalignment of the spline shaft resulted from improper machining during pump modification. The nose gear inner cylinder failed in fatigue in an area of excessive grinding during overhaul. Two passengers were slightly injured.
Probable cause:
Failure of the fuel pump control shaft because of improper machining by the repair facility during maintenance modification of the pump and improper procedures during overhaul of the nose landing gear.
Final Report:

Crash of a De Havilland DHC-3 Otter in Beaver Village: 2 killed

Date & Time: Jun 30, 1990 at 1130 LT
Type of aircraft:
Operator:
Registration:
N17689
Flight Phase:
Survivors:
Yes
Schedule:
Fairbanks - Arctic Village
MSN:
431
YOM:
1964
Crew on board:
1
Crew fatalities:
Pax on board:
8
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8400
Captain / Total hours on type:
165.00
Aircraft flight hours:
7111
Circumstances:
The pilot reported a substantial loss of power while in cruise flight. He was unable to maintain altitude and the aircraft crashed into trees. An examination of the recently overhauled engine revealed a fractured exhaust rocker arm that caused the loss of power.
Probable cause:
Mechanical failure of an exhaust rocker arm.
Final Report:

Crash of a Piper PA-46-310P Malibu in Lakeville: 1 killed

Date & Time: Jun 26, 1990 at 1616 LT
Operator:
Registration:
N315RC
Flight Phase:
Survivors:
No
Schedule:
Flint – Akron
MSN:
46-8508044
YOM:
1985
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
983
Captain / Total hours on type:
197.00
Aircraft flight hours:
710
Circumstances:
During IFR departure, pilot received progressive altitude clearances to climb to 15,000 feet. At 1607 edt, he was vectored for 'a good rate of climb' thru 14,000 feet with clearance to proceed on course after leveling 14,000 feet for 15,000 feet. Radar data indicated a steady climb til aircraft was above 13,000 feet. As it climbed from 13,300 feet to 13,900 fet (max recorded altitude), its speed slowed from about 115 knots to below 80 knots. At 1613 edt, pilot was cleared to proceed direct and change frequency. Radar data showed that after reaching 13,900 feet, aircraft deviated from course and entered steep descent. Radar contact was lost and inflight breakup occurred. Pieces of wings and stabilizers were found up to 1.5 mile from fuselage. Trajectory study disclosed breakup occurred between 6,000 feet and 9,000 feet msl. Exam of fractures on major components revealed characteristics typical of overstress; no preexisting cracks were found. No autopilot failure or bird strike was found. Clouds were layered to 20,000 feet; freezing level was about 12,500 feet. There was evidence aircraft was in or near convective precipitation above freezing level for about 1.5 minute before rapid descent. Found Pitot heat switch 'off' and induction air door in its primary position. The pilot, sole on board, was killed.
Probable cause:
The pilot's failure to use the airplane's ice protection equipment, which resulted in a performance loss due to induction icing, propeller icing, or both, while flying in convective instrument meteorological conditions (IMC) at and above the freezing level. The performance loss led to a stall, the recovery from which probably was exacerbated by the pilot's improper response to erroneous airspeed indications that resulted from blockage of the pitot tube by atmospheric icing.
Final Report:

Crash of a Piper PA-31-310 Navajo in Panama City: 2 killed

Date & Time: Jun 26, 1990 at 0515 LT
Type of aircraft:
Registration:
N18PA
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Panama City - Tampa
MSN:
31-7712068
YOM:
1977
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
7524
Captain / Total hours on type:
600.00
Aircraft flight hours:
5993
Circumstances:
Witnesses described the takeoff as a long ground roll, slow climb, and engines not sounding normal. The airplane then settled into trees. Teardown of the left engine revealed water present in the fuel injector lines of #1, #3 and #5 cylinders. #3 nozzle plugged. Intake valves dark and sooty. Pistons 1, 3 and 5 had considerable amounts of dark carbon deposits. Teardown of right engine revealed extensive carbon buildups throughout. An engine test run was performed by the director of maintenance day before accident. Personnel formerly employed by the operator provided written statements of allegations pertaining to the general condition of company airplanes, falsification of maintenance records, and improper maintenance procedures being performed on company airplanes. Both occupants were killed.
Probable cause:
A loss of power on both engines during takeoff as a result of inadequate maintenance. In addition, the pilot failed to abort the takeoff.
Final Report:

Crash of a Cessna 207A Skywagon near Aialak Bay: 5 killed

Date & Time: Jun 25, 1990 at 1430 LT
Registration:
N9985M
Flight Phase:
Survivors:
No
Site:
Schedule:
Seward - Seward
MSN:
207-0775
YOM:
1984
Crew on board:
1
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
540
Aircraft flight hours:
3391
Circumstances:
Two airplanes departed Seward within minutes of each other on a local flightseeing trip, and their flight routes were to be the same. After reaching Aialak Bay, this airplane passed the other and started the return trip to seward. The pass they would normally use was obscured by clouds. The peninsula that separated Aialak Bay and Seward was the only part of land that was obscured by weather. The bases of the clouds were at 1,200 feet msl. The airplane was located on the northeast side, at the 2,700 foot level of a mountain, and the wreckage was scattered along 330°. The pilot had been hired less than 2 months before the accident as a ground handler and fueler, and for pilot training. Two days before the accident he was authorized to fly part 135 flightseeing trips.
Probable cause:
The pilot-in-command's attempt to fly under visual flight rules while in instrument meteorological conditions. Contributing factors to the accident were the low ceiling and surrounding mountainous terrain.
Final Report:

Crash of a Short SC.7 Skyvan 3 Variant 100 in Kako Mine

Date & Time: Jun 23, 1990 at 1410 LT
Type of aircraft:
Operator:
Registration:
N50GA
Flight Type:
Survivors:
Yes
Schedule:
Bethel - Kako Mine
MSN:
1856
YOM:
1969
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3236
Captain / Total hours on type:
977.00
Aircraft flight hours:
15689
Circumstances:
The non-scheduled, all cargo, air taxi flight was landing at the mining strip and upon touchdown the pilot-in-command released the yoke with his left hand and grabbed the nose steering tiller. The pilot-in-command stated that before he could apply reverse thrust, the nose of the airplane came up off the ground and the airplane began to veer to the right. He applied left rudder and power to the right engine, but the airplane left the right side of the runway.
Probable cause:
The pilot-in-command's failure to maintain control of the airplane through the touchdown and landing phase.
Final Report:

Crash of a Cessna 208A Cargomaster in Fresno

Date & Time: Jun 6, 1990 at 1715 LT
Type of aircraft:
Operator:
Registration:
N803FE
Flight Type:
Survivors:
Yes
Schedule:
Fresno - Oakland
MSN:
208-0015
YOM:
1985
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
9275
Captain / Total hours on type:
335.00
Circumstances:
The engine lost oil pressure while climbing through 6,000 feet, and the pilot requested to return to his departure airport. ATC informed the pilot of a closer airport. The pilot secured the engine, feathered the prop, and made a power-off descent to the airport. The pilot elected to make a downwind approach to runway 12L due to his altitude. The airplane overflew the runway and touched down past the departure end. It penetrated the airport perimeter fence, struck several trees, a sign post, a light pole, and an auto before coming to rest in a residential area. Examination of the wreckage revealed the loss of pressure was due to oil leaking. The oil filler cap was found improperly adjusted after the original installation. The maintenance manual does not approve any field repairs on the oil filler cap engaging mechanisms. The airplane's flaps were found at a 7° intermediate setting.
Probable cause:
A loss of engine oil pressure due to improper maintenance performed on the engine oil filler cap by an unknown person. In addition, the pilot misjudged his landing approach to the runway during the forced landing which resulted in an overshoot and collision with objects. A tailwind contributed to the overshoot.
Final Report:

Crash of a Boeing 737-2X6C in Unalakleet

Date & Time: Jun 2, 1990 at 0937 LT
Type of aircraft:
Operator:
Registration:
N670MA
Flight Type:
Survivors:
Yes
Schedule:
Anchorage - Unalakleet
MSN:
23121
YOM:
1984
Flight number:
BF3087
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
12000
Captain / Total hours on type:
6400.00
Copilot / Total hours on type:
80
Circumstances:
On june 2, 1990, at 09:37 Alaskan daylight time, Markair, Inc., flight 3087, a Boeing 737-2X6C, registered in the us as N670MA, crashed about 7.5 miles short of runway 14, Unalakleet, Alaska, while executing a localizer approach to that runway. The flight originated at 0828 at Anchorage International Airport, Anchorage, Alaska. Instrument meteorological conditions existed at the time, and the flight was on an IFR flight plan. The captain, the first officer, and a flight attendant sustained minor injuries. Another flight attendant sustained serious injuries. There were no passengers on board, and the aircraft was destroyed. The flight was operated under far part 121.
Probable cause:
Deficiencies in flightcrew coordination, their failure to adequately prepare for and properly execute the unk loc runway 14 non precision approach and their subsequent premature descent.
Final Report:

Crash of a Cessna T303 Crusader in DeLand

Date & Time: May 28, 1990 at 0803 LT
Type of aircraft:
Registration:
N4973V
Flight Type:
Survivors:
Yes
Schedule:
Daytona Beach - DeLand
MSN:
303-00285
YOM:
1984
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1520
Captain / Total hours on type:
100.00
Aircraft flight hours:
2542
Circumstances:
During an NDB approach in instrument conditions with the landing gear extended, the fire warning light for the right engine illuminated. The right engine was shut down and a missed approach was initiated; however, the landing gear would not retract and the aircraft would not maintain altitude. As it descended into the top of an overcast at an altitude of about 600 feet, the pilots tried to restart the engine, but to no avail. Subsequently, the aircraft descended below the clouds at an altitude of about 150 feet to 170 feet. As the instructor (cfi) landed the aircraft in an open field, the nose gear encountered soft dirt and the aircraft nosed over. An exam revealed that an electrical power jumper wire between 2 bus bars had become chafed and shorted. The left and right isolation circuit breakers and the bus tie circuit breaker were found in the tripped (open) position. This resulted in a false fire warning light and prevented the landing gear from being retracted.
Probable cause:
The chafed and shorted electrical wiring between bus bars, which caused a partial electrical failure, resulted in a false fire warning indication, and prevented the restart of the right engine.
Final Report: