Crash of a Fokker F27 Friendship 500RF in Kinston

Date & Time: Mar 8, 2003 at 1027 LT
Type of aircraft:
Operator:
Registration:
N712FE
Flight Type:
Survivors:
Yes
Schedule:
Greensboro - New Bern
MSN:
10613
YOM:
1981
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8130
Captain / Total hours on type:
1450.00
Copilot / Total flying hours:
2911
Copilot / Total hours on type:
955
Aircraft flight hours:
26665
Aircraft flight cycles:
28285
Circumstances:
According to the pilot, an unsafe right gear indication was received during the approach, and the control tower controller confirmed the right gear was not fully extended. On landing roll the right main landing gear collapsed and the airplane slid off of the runway. Examination of the right main landing gear revealed the drag brace was fractured. The fracture was located at the lower side of a transition from a smaller internal diameter on the upper piece to a larger internal diameter on the lower piece. The region of the fracture surface was flat and perpendicular to the tube longitudinal axis. The region had a smooth, curving boundary, also consistent with fatigue. The fatigue features emanated from multiple origins at the inner surface of the tube. The Federal Aviation Administration (FAA) issued an Airworthiness Directive (AD) requiring an inspections of main landing gear drag stay units. The AD was prompted by the fracture of a drag stay tube from fatigue cracking that initiated from an improperly machined transition radius at the inner surface of the tube. According to Fokker ,the Fokker F27 Mark 500 airplanes (such as the incident airplane) were not equipped with drag stay units having part number 200261001, 200485001, or 200684001. One tube, part number 200259300, had a change in internal diameter (stepped bore), and the other tube, part number 200485300, had a straight internal bore. AD 97-04-08 required an ultrasonic inspection to determine if the installed tube had a straight or stepped bore. A review of maintenance records revealed that the failed drag stay tube had accumulated 28, 285 total cycles.
Probable cause:
The fatigue failure of the main drag stay tube. A factor is no inspection procedure required.
Final Report:

Crash of a Beechcraft 60 Duke in Kinston: 3 killed

Date & Time: Apr 1, 1991 at 1326 LT
Type of aircraft:
Registration:
N311MC
Flight Type:
Survivors:
No
Schedule:
Kinston – Stuart
MSN:
P-366
YOM:
1976
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
3
Captain / Total flying hours:
2345
Captain / Total hours on type:
500.00
Circumstances:
During takeoff from runway 22, the pilot reported that he had a problem, then there was no further communication from the aircraft. Several witnesses saw an object fall from the aircraft and one witness observed that a 'hood' had opened. The aircraft was maneuvered onto final approach to runway 36. A witness said that as the aircraft was lining up on final approach, it entered a steep bank and descended out of his sight. Subsequently, it collided with trees in a 27° descent, crashed and burned. A bag from the nose baggage compartment was found near the departure end of runway 22. No preimpact part failure or system malfunction of the aircraft was found. Before the flight, a ramp person observed the pilot servicing the left engine with oil, but he did not know if the pilot had secured the baggage door. An examination of the recovered door assembly failed to disclose a malfunction of the rear latch assembly. The forward latch assembly area was destroyed by fire. All three occupants were killed.
Probable cause:
The pilot diverted his attention and failed to maintain control of the aircraft, while maneuvering for a precautionary landing. Factors related to the accident were: the unsecured baggage compartment door and the pilot's inadequate preflight.
Final Report:

Crash of a Boeing 737-222 in Kinston

Date & Time: Jul 22, 1990 at 1455 LT
Type of aircraft:
Operator:
Registration:
N210US
Flight Phase:
Survivors:
Yes
Schedule:
Kinston - Charlotte
MSN:
19555
YOM:
1968
Crew on board:
5
Crew fatalities:
Pax on board:
22
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
10100
Captain / Total hours on type:
3300.00
Aircraft flight hours:
51264
Circumstances:
As engine power was increased for takeoff, the n°1 engine accelerated beyond target epr. Engine shut down had to be done with the fuel shut off lever. The asymmetric thrust was controlled with nose wheel steering. Before the airplane could be stopped the nose wheels separated from the landing gear. The investigation revealed that the fuel pump output spline to the fuel control had stripped. It occurred at such a time that the fuel control sensed an underspeed and increased Fuel flow. Misalignment of the spline shaft resulted from improper machining during pump modification. The nose gear inner cylinder failed in fatigue in an area of excessive grinding during overhaul. Two passengers were slightly injured.
Probable cause:
Failure of the fuel pump control shaft because of improper machining by the repair facility during maintenance modification of the pump and improper procedures during overhaul of the nose landing gear.
Final Report: