Crash of a Cessna 340A in Wise River: 1 killed

Date & Time: Sep 5, 1996 at 1157 LT
Type of aircraft:
Registration:
N128RP
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Butte - McCall
MSN:
340A-0084
YOM:
1976
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Captain / Total flying hours:
2500
Aircraft flight hours:
1500
Circumstances:
The pilot received a full weather briefing from a Flight Service Station (FSS) on the morning of the accident. The FSS briefer told the pilot that moderate turbulence and icing prevailed along the pilot's intended route of flight, and that there were forecasts for isolated thundershowers. The briefer advised the pilot to call for an update just prior to departure. The pilot departed on the flight almost 3 hours later without calling for an update. He received an IFR clearance after 15 minutes of delays, then proceeded on course to his destination. About 35 minutes after departure, while cruising at 16,000 feet, the pilot reported that he was 'in the clouds and the bumps are big time.' About 3 minutes later, the pilot radioed that he was 'in a dive and I don't...' The airplane impacted terrain in a nose-down, inverted attitude and exploded. Analysis of recorded radar and meteorological data indicates that the airplane encountered a thunderstorm, strong updrafts, downdrafts, and turbulence.
Probable cause:
The pilot's attempt to fly in adverse meteorological conditions which led a loss of aircraft control. Factors contributing to the accident include: the pilot's failure to obtain the most current information of the meteorological conditions prior to departure, a thunderstorm, and turbulence.
Final Report:

Ground fire of a Douglas DC-10-10CF in Newburgh

Date & Time: Sep 5, 1996 at 0554 LT
Type of aircraft:
Operator:
Registration:
N68055
Flight Type:
Survivors:
Yes
Schedule:
Memphis - Boston
MSN:
47809
YOM:
1975
Flight number:
FDX1406
Crew on board:
3
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
12344
Captain / Total hours on type:
2504.00
Copilot / Total flying hours:
6535
Copilot / Total hours on type:
1101
Aircraft flight hours:
38271
Aircraft flight cycles:
17818
Circumstances:
The airplane was at FL 330 when the flightcrew determined that there was smoke in the cabin cargo compartment. An emergency was declared and the flight diverted to Newburgh/Stewart International Airport and landed. The airplane was destroyed by fire after landing. The fire had burned for about 4 hours after after smoke was first detected. Investigation revealed that the deepest and most severe heat and fire damage occurred in and around container 06R, which contained a DNA synthesizer containing flammable liquids. More of 06R's structure was consumed than of any other container, and it was the only container that exhibited severe floor damage. Further, 06R was the only container to exhibit heat damage on its bottom surface, and the area below container 06R showed the most extensive evidence of scorching of the composite flooring material. However, there was insufficient reliable evidence to reach a conclusion as to where the fire originated. The presence of flammable chemicals in the DNA synthesizer was wholly unintended and unknown to the preparer of the package and shipper. The captain did not adequately manage his crew resources when he failed to call for checklists or to monitor and facilitate the accomplishment of required checklist items. The Department of Transportation hazardous materials regulations do not adequately address the need for hazardous materials information on file at a carrier to be quickly retrievable in a format useful to emergency responders.
Probable cause:
An in-flight cargo fire of undetermined origin.
Final Report:

Crash of a Cessna 421B Golden Eagle II near Conchas

Date & Time: Aug 30, 1996 at 1830 LT
Operator:
Registration:
N55HU
Flight Phase:
Survivors:
Yes
Schedule:
Albuquerque - Alva
MSN:
421B-0014
YOM:
1970
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
2934
Captain / Total hours on type:
67.00
Aircraft flight hours:
2700
Circumstances:
At 1615, the pilot called FSS for a weather briefing and to file an IFR flight plan. He was told that there was thunderstorm activity, which was building in intensity, extending from Raton, New Mexico, to Garden City, Kansas, with some scattered activity in the Oklahoma panhandle. The briefer further reported that the thunderstorm activity was moving east, southeast. The pilot checked in with Albuquerque Center at 1750 during his departure climb to 21,000 feet. At 1755, convective SIGMET 70C was issued for isolated severe thunderstorms located 10 miles north, northeast, of Las Vegas, New Mexico. FAA Order 7110.65J, Air Traffic Control, section 2-6-2, states that 'controllers shall advise pilots of hazardous weather that may impact operations within 150 NM of their sector or area of jurisdiction.' SIGMET 70C was not given to the pilot by the center controller. Radio contact was lost at 1823. The pilot reported that the airplane was in VMC, approaching precipitation, when they encountered hail and the pilot's windshield was broken out which resulted in the airplane's depressurization.
Probable cause:
The pilot's inadvertent flight into hail which shattered the pilot's windshield and resulted in his incapacitation due to hypoxia.
Final Report:

Crash of a Lockheed C-130H Hercules on Mt Sleeping Indian: 9 killed

Date & Time: Aug 17, 1996 at 2250 LT
Type of aircraft:
Operator:
Registration:
74-1662
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Jackson Hole - New York
MSN:
4597
YOM:
1975
Flight number:
Havoc 58
Crew on board:
8
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
9
Captain / Total flying hours:
1744
Captain / Total hours on type:
904.00
Copilot / Total flying hours:
188
Copilot / Total hours on type:
149
Circumstances:
The aircraft departed Jackson Hole Airport at 2245LT on a flight to New York-JFK, carrying eight crew members and a U.S. Secret Service agent. The purpose of the flight was to transport a U.S. Secret Service communications vehicle to New York after President Bill Clinton spent some vacations in Jackson Hole. Five minutes after takeoff, while climbing by night, the four engine aircraft struck the slope of Mt Sleeping Indian (Mt Sheep - 3,427 metres high) located about 18 km southeast of the airport. The aircraft disintegrated on impact and all nine occupants were killed.
Probable cause:
Controlled flight into terrain after the crew's failure to properly plan for a night departure from an unfamiliar airport. The crew did not follow the published instrument departure procedures and was relatively inexperienced.
Final Report:

Crash of a Piper PA-31T Cheyenne II in Pottstown

Date & Time: Aug 14, 1996 at 0708 LT
Type of aircraft:
Registration:
N163SA
Flight Phase:
Survivors:
Yes
Schedule:
Pottstown - Philadelphia
MSN:
31-7920025
YOM:
1979
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
15000
Captain / Total hours on type:
1000.00
Aircraft flight hours:
4993
Circumstances:
During an attempted takeoff, the airplane collided with a taxiway sign, a fence, a light pole and came to rest between two buildings. According to the pilot in command (seated in the right seat), a preflight and run-up inspection was completed successfully. He stated that a pilot rated passenger (in the left front seat) was following along with a placard checklist. He stated that the airplane was accelerated for takeoff on runway 7, and at 500 feet down the 2700 foot long runway with the airspeed at redline, rotation was initiated and the airplane veered to the right. He stated that shortly thereafter the right engine surged and he noted the matched power levers, but he did not record the engine power instruments. A passenger (seated in a forward facing seat behind the pilot in command) reported that the pilot rated passenger's hand was on the throttle(yellow-knobbed handles) at the time of the accident The reported visibility was 1/8 mile in fog. The prescribed takeoff minimums for that airport is 400 feet and 1 mile visibility. Post accident examination of the engines and their systems revealed no evidence of preimpact mechanical malfunction. The pilot reported that there was no mechanical malfunction.
Probable cause:
The pilot's failure to maintain directional control during takeoff/ground run resulting in inflight collision with a fence. Related factors were the pilot's poor planning/decision making, and the fog.
Final Report:

Crash of a Grumman G-21A Goose near Dutch Harbor: 2 killed

Date & Time: Aug 11, 1996 at 1615 LT
Type of aircraft:
Operator:
Registration:
N660PA
Flight Phase:
Survivors:
No
Schedule:
Anderson Bay - Dutch Harbor
MSN:
B138
YOM:
1945
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
20000
Captain / Total hours on type:
8000.00
Aircraft flight hours:
13381
Circumstances:
On August 11, 1996, about 1615 Alaska daylight time, an amphibious Grumman G21-G, N660PA, is presumed to have been involved in a fatal accident about 20 miles south of Dutch Harbor, Alaska. The airplane was being operated as a visual flight rules (VFR) cross-country on demand passenger flight under Title 14 CFR Part 135 when the accident occurred. The airplane, registered to and operated by Peninsula Airways Inc., Anchorage, Alaska, is presumed to have been destroyed. The certificated airline transport pilot, and the sole passenger are presumed to have received fatal injuries. Low ceilings were reported in the area of departure by the operator. VFR company flight following procedures were in effect. The flight originated from Anderson Bay, on the Island of Unalaska, about 1610.
Probable cause:
Due to lack of evidences, the exact cause of the accident could not be determined.
Final Report:

Crash of a Cessna 404 Titan II in Benton Harbor

Date & Time: Aug 3, 1996 at 0740 LT
Type of aircraft:
Operator:
Registration:
N8919G
Flight Type:
Survivors:
Yes
Schedule:
Kalamazoo - Benton Harbor
MSN:
404-0098
YOM:
1977
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3250
Captain / Total hours on type:
53.00
Aircraft flight hours:
10624
Circumstances:
The pilot said that during the landing approach, the flight visibility was inadequate for landing, and he aborted the landing. Witnesses observed the airplane touchdown long and fast, then it
entered fog that shrouded the runway. Subsequently, the airplane collided with trees, then impacted on marshland about 70 feet below the runway elevation. No mechanical anomalies were found with the airplane or engines that would prevent flight. On the day before the accident, the pilot's duty day began at 0500. He had a 9-hour rest period (during the day) that did not involve any sleep. The pilot said that after work on the day before the accident, he arrived home about 2300. His wife said he awoke about 0230 on the accident date, then he returned to bed and arose between 0430 and 0500, departing for work about 0530. During his regular duty day rest period, the pilot would drive a total of 4 hours to and from his home each day. The pilot said he would generally get to bed about 2300 to 2330, arising about 0430 each work day. Also, he said he needed between 6 and 8 hours of sleep at night.
Probable cause:
The pilot's delay in initiating a go-around after not attaining the proper touchdown point during the landing, and his failure to remain clear of obstructions (trees) during the go-around. Factors relating to the accident were the adverse weather condition (fog and low ceiling), pilot fatigue, and the proximity of trees to the runway.
Final Report:

Crash of a De Havilland DHC-4A Caribou in New Stuyahok

Date & Time: Aug 2, 1996 at 1100 LT
Type of aircraft:
Operator:
Registration:
N800NC
Flight Type:
Survivors:
Yes
Schedule:
Anchorage - New Stuyahok
MSN:
98
YOM:
1963
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
15670
Captain / Total hours on type:
850.00
Aircraft flight hours:
14638
Circumstances:
The airplane's nose gear collapsed during a landing roll on a gravel airstrip. Subsequent examination of the nose gear locking mechanism disclosed a failed hydraulic drag strut locking actuator.
Probable cause:
The collapse of the nose gear precipitated by the failure of the hydraulic nose gear drag strut locking actuator.
Final Report:

Crash of a Cessna 340A in Richland: 2 killed

Date & Time: Jul 27, 1996 at 0855 LT
Type of aircraft:
Operator:
Registration:
N341TL
Flight Type:
Survivors:
No
Schedule:
Richland - Richland
MSN:
340A-1268
YOM:
1981
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
4239
Captain / Total hours on type:
1240.00
Circumstances:
The pilot-under-instruction (PUI) who possessed an expired medical, and the pilot-in-command (PIC), an ATP pilot with 1240 hours in the Cessna 340, departed on the third training flight for the PUI in the aircraft. The second training flight, flown the previous Saturday, had included single-engine work. The aircraft was observed in the vicinity of the Richland airport by witnesses, several of whom reported the left propeller turning slowly. All witnesses reported seeing the aircraft descending rapidly to the ground in a nose down attitude and several witnesses described the descent as a spin. The aircraft impacted the ground in a near vertical, nose low attitude and was destroyed by fire. Postcrash examination of the aircraft revealed the left propeller in the feathered position and power signatures on the blades of the right propeller. Disassembly of both engines revealed no pre-impact mechanical malfunction. The gear and flaps were up and the rudder trim tab showed about 5 degrees of left tab trim. The information manual for the Cessna 340 indicates that the air minimum control speed (single engine), Vmca is 82 KIAS. The manual also indicates that a more suitable airspeed for one engine inoperative training events is 91 KIAS.
Probable cause:
The pilot-in-command's allowing the aircraft's airspeed to decrease below the single-engine minimum control speed (Vmc) resulting in a stall/spin condition. Factors contributing to the accident were the pilot-in-command's allowing the left engine to be shut down as well as his allowing the aircraft's airspeed to decelerate below the manufacturer's recommended intentional one-engine inoperative airspeed. A third factor was the aircraft's low altitude at the stall/spin entry which precluded a successful recovery.
Final Report:

Crash of a Douglas DC-6A in Russian Mission: 4 killed

Date & Time: Jul 20, 1996 at 1506 LT
Type of aircraft:
Operator:
Registration:
N313RS
Flight Type:
Survivors:
No
Schedule:
Emmonak – Aniak
MSN:
44663
YOM:
1955
Flight number:
HU033
Crew on board:
3
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
14200
Captain / Total hours on type:
7200.00
Aircraft flight hours:
38248
Circumstances:
The cargo flight was en route, when a fire erupted in or near the #3 engine. During subsequent emergency procedures, the flight crew pulled the fire handle first. Later, they feathered the #3 engine. The fire did not extinguish. During an attempt to land at a rural, intermediate airstrip, while the airplane was in the traffic pattern, witnesses saw fire coming from the area of the #3 engine. They stated the right wing buckled upward, and the airplane crashed. Examination of the wreckage revealed a failure of the master rod in the front bank of cylinders of the #3 engine. Metallurgical tests revealed a crack in the top of the master rod head, which had resulted from corrosion pits. The side of the master rod head was measured and found to be out of round. The master rod shank also fractured due to fatigue. The operator's training procedures and the Douglas Aircraft emergency checklist procedures, required that the engine's propeller be feathered first, and then the fire extinguishing system to be activated. According to information derived from the airplane's cockpit voice recorder, the flight crew reversed that order. The effectiveness of the fire suppression system is diminished if the propeller is not feathered first.
Probable cause:
Fatigue failure of the master connecting rod, which originated from corrosion pitting, subsequently compromised the engine crankcase, and resulted in a fire; and failure of the flight crew to follow emergency procedures by pulling the fire handle before feathering the propeller, which diminished the effectiveness of the fire suppression system.
Final Report: