Crash of a Vickers 803 Viscount off Wexford: 61 killed

Date & Time: Mar 24, 1968 at 1058 LT
Type of aircraft:
Operator:
Registration:
EI-AOM
Flight Phase:
Survivors:
No
Schedule:
Cork - London-Heathrow
MSN:
178
YOM:
1957
Flight number:
EI712
Country:
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
57
Pax fatalities:
Other fatalities:
Total fatalities:
61
Captain / Total flying hours:
6683
Captain / Total hours on type:
1679.00
Copilot / Total flying hours:
1139
Copilot / Total hours on type:
900
Aircraft flight hours:
18806
Aircraft flight cycles:
16923
Circumstances:
Viscount aeroplane type 803, registration: EI-AOM departed from Cork Airport at 10.32 hours en route for London operating as Aer Lingus Flight 712. The take-off was normal. The flight was cleared by Air Traffic Control to proceed via Airways Blue 10, Green 1 at flight level 170 (17,000'). At 10.38, when the aeroplane had passed through 7,000', clearance on course to Tuskar was given. At 10.40, after the flight had reported it was by Youghal at 7,500' climbing to 17,000', ATC Cork suggested that if desired, the flight could route direct to Strumble. No direct acceptance of this suggestion was received. At 10.57.07 the flight reported "by Bannow (a reporting point on the route at 51º 68' N - 06º 12' W) level 170 (17,000') estimating Strumble at 03". The flight was instructed to change to the London Airways frequency of 131.2, and this was acknowledged by the reply "131.2". The time of this call was 10.57.29. At 10.58.02, London Radar intercepted a call (garbled and simultaneous with another call) which appeared to be, and was later confirmed as "Echo India Alpha Oscar Mike with you", and eight (8) seconds later, a call was intercepted which was interpreted as "Five thousand feet descending spinning rapidly". This call was also heard by another Aer Lingus aircraft en route Dublin-Bristol (The word "Five" was later, after repeated acoustic analysis, interpreted as more likely to be the word "twelve".) This was the last call received from the aircraft. At 11.10, London ATC advised Shannon ATC that they had no radio contact with EI-AOM. At 11.13 London advised Shannon that they had requested Aer Lingus Flight EI 362 (Dublin-Bristol) to search west of Strumble. This flight descended to 500' in good visibility, but saw nothing. Between 11.13 and 11.25, efforts were made to make radio contact with the flight, with no result, and at 11.25 a full alert was declared. At 12.36 a report from the U.K. was received by Haulbowline that wreckage had been sighted in position 51º 57' N, 06º 10' W Rosslare Lifeboat was proceeding, but two surface vessels within 4 nautical miles of this position saw nothing. At 12.52 hours the Air Corps reported that they had dispatched a Dove aeroplane and a helicopter to search. At 13.10 hours there were ten aircraft from the U.K. in the search area. At 15.30 hours the reported sighting of wreckage was cancelled. Nothing positive was discovered on this day. On 25 March 1968, at 06.15 hours, the search was resumed by aircraft and ships from the U.K., and at 12.41 hours, wreckage was sighted and bodies recovered from a position 6 nautical miles north-east of Tuskar Rock. More floating wreckage was reported scattered for a further 6 nautical miles north-west of this point. The Irish Naval Service ship, L.E. Macha, which had been on patrol off the north-west coast, joined in the search on 26 March 1968, and took over duty as Search Controller. A total of 13 bodies was eventually recovered in the search during the next few days, together with a quantity of light floating wreckage-mostly cabin furnishings, and some baggage, seat cushions, and the wheels and inner cylinder from the port main landing gear. One additional body was recovered later. The position of the main wreckage remained obscure in spite of prolonged and diligent search by sonar equipped ships of the British Navy and trawling by Irish trawlers-"Glendalough" from Kilmore Quay and "Cu na Mara" of the Irish Fisheries Board (An Bord Iascaigh Mhara). Eventually, on 5 June 1968 "Glendalough" hauled in position 1.72 nautical miles from Tuskar Rock with Tuskar bearing 280º, in 39 fathoms and brought up a quantity of positively identifiable wreckage. The "Cu na Mara" in the same location also brought up wreckage. On the following day more wreckage was brought up by these trawlers, and divers from H.M.S. Reclaim confirmed a mass of wreckage "like a scrap yard" in this position. Subsequent salvage operations confirmed that a major portion of the aircraft at least was located here. Two eyewitnesses, one a sailor on a coastal vessel, who thought he had seen an aircraft crash into the sea but did not report it at the time, and another witness on shore, who saw a splash in the sea near the Tuskar Rock, gave the time as between 11.10 and 11.15. The position lines of these two witnesses approximately cross the location where the main wreckage was eventually found. The aircraft was totally demolished by violent impact with the sea. The bulk of the wreckage was found in 39 fathoms of water with all parts lying in close proximity. About 60-65% of the aircraft (by weight) was recovered, and included the major parts of three engines, a few parts of the fourth, and all four propellers, the almost complete primary structure of the wings from tip to tip, and the fin and rudder. None of the wreckage displayed any evidence of fire or explosion. No part of the tail planes or elevators were recovered, with the exception of small portions of the spring tab and trim tab. The recovered wreckage revealed extensive damage to the whole structure, which virtually disintegrated.
Probable cause:
There is not enough evidence available on which to reach a conclusion of reasonable probability as to the initial cause of this accident. The probable cause of the final impact with the sea was impairment of the controllability of the aircraft in the fore and aft (pitching) plane. Speculation continued since the time of the accident, prompted by a hypothesis posed in the report, that the Viscount may have been initially upset by the possible presence of another airborne object, drone or missile in its vicinity at the time. On the 30th anniversary of the accident, following newspaper articles and television programmes focusing on the possible involvement of U.K ships and missile ranges on the Welsh Coast in the downing of the aircraft, it was decided that Irish and U.K. officials would review all files held relating to the accident to see if the cause of the accident could be established. It was a.o. concluded that "the possibility of a cause other than a (near) collision with another airborne object being the initial cause of the upset ... does not appear to have been adequately examined in the 1970 Report." Following the review, in July 2000, the Irish Minister for Public Enterprise commissioned an independent study of the accident circumstances. The International Study Team published their findings in December 2001:
- An initial event, which cannot be clearly identified, disturbed the air flow around the horizontal tail surfaces and the pitch control of the aircraft. In the light of what was observed by non-skilled people there was a strong indication that structural fatigue, flutter, corrosion or bird strike could have been involved,
- It is possible that the sensitivity of the engine fuel control units to negative accelerations imposed during the initial upset, had an adverse effect on the subsequent flight path of the aircraft,
- The severe manoeuvres of the aircraft following the initial upset and the subsequent flight would have been outside the airworthiness certification envelope and may have resulted in some deformation of the structure,
- A number of possible causes for an impairment of pitch control were examined and it is considered very possible that excessive spring tab free play resulted in the fatigue failure of a component in the tab operating mechanism thus inducing a tailplane-elevator tab free flutter condition,
- The loads induced by the flutter condition would be of sufficient magnitude and frequency to cause a fatigue failure of the port tailplane within the timescale estimated for EI-AOM,
- There was no involvement of any other aircraft or missile.
Final Report:

Crash of a Vickers 745D Viscount in Akron

Date & Time: Dec 11, 1967 at 1526 LT
Type of aircraft:
Operator:
Registration:
N7429
Survivors:
Yes
Schedule:
Detroit - Akron
MSN:
127
YOM:
1956
Crew on board:
3
Crew fatalities:
Pax on board:
15
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
11000
Captain / Total hours on type:
8000.00
Circumstances:
After touchdown at Akron-Canton Airport, the four engine airplane encountered difficulties to stop within the remaining distance. It overran, lost its undercarriage and went down an 23 feet embankment before coming to rest 400 feet further. A passenger was seriously injured while all other occupants escaped uninjured. The aircraft was written off.
Probable cause:
Wrong approach configuration on part of the pilot-in-command who misjudged distance and speed upon landing and failed to initiate a go-around procedure.
Final Report:

Crash of a Vickers C-90 Viscount in Rio de Janeiro

Date & Time: Dec 8, 1967
Type of aircraft:
Operator:
Registration:
2100
Flight Type:
Survivors:
Yes
Schedule:
Brasília – Rio de Janeiro
MSN:
141
YOM:
1956
Country:
Crew on board:
4
Crew fatalities:
Pax on board:
14
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The four engine aircraft was completing a flight from Brasília to Rio de Janeiro, carrying a delegation of the Brazilian government, among them Arturo da Costa e Silva, President of the Republic of Brazil. Upon landing at Santos Dumont Airport, the right main gear collapsed. The airplane sank on its belly and slid for several yards before coming to rest in flames. All 18 occupants escaped uninjured while the aircraft was considered as damaged beyond repair.
Probable cause:
Failure of the right main gear upon landing.

Crash of a Vickers 745D Viscount in Raleigh

Date & Time: Nov 28, 1967 at 2100 LT
Type of aircraft:
Operator:
Registration:
N7465
Survivors:
Yes
MSN:
231
YOM:
1957
Crew on board:
4
Crew fatalities:
Pax on board:
39
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8862
Captain / Total hours on type:
3982.00
Circumstances:
After touchdown at Raleigh-Durham Airport by night, the nosewheel collapsed. The airplane slid on the runway for several yards until it came to rest. All 43 occupants escaped uninjured while the aircraft was later considered as damaged beyond repair.
Probable cause:
Failure of the nosewheel steering system upon touchdown due to fatigue fracture. A valve body on the nosewheel steering jack twin valve failed, causing oscillations.
Final Report:

Crash of a Vickers 808 Viscount in Bristol

Date & Time: Sep 21, 1967 at 0859 LT
Type of aircraft:
Operator:
Registration:
EI-AKK
Survivors:
Yes
Schedule:
Dublin - Bristol
MSN:
422
YOM:
1959
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
17
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
5005
Captain / Total hours on type:
1300.00
Copilot / Total flying hours:
2200
Copilot / Total hours on type:
592
Aircraft flight hours:
18375
Circumstances:
Before leaving Dublin no landing forecast for Lulsgate was available but the forecast conditions for Filton, 10 miles north of Lulsgate, were well above the company minima of 260 ft critical height and 800 rn RVR. About 25 minutes before commencing the approach to land and whilst the aircraft was on the airway near Strumble, the latest weather conditions for Lulsgate obtained by radio from air traffic control, showed that there was 3/8 cloud at 1 000 ft, visibility was 1 500 m with the sun tending to disperse cloud and mist. After leaving the airway, the aircraft was positioned by Lulsgate radar for an approach to runway 28 on a right-hand base leg. At 0752 hours GMT before the final approach was commenced, the latest weather conditions were passed by the Lulsgate rabar controller who was also the approach controller, these conditions showed a surface wind northerly 8 to 10 kt, QFE 979, QNH 1 001, visibility in mist 1 800 m. During the final turn on to the approach at 6 miles, the aircraft drifted to the left of the extended centre line which was regained closing from left to right during the final descent. At five miles from touchdown, still to the left of the centre line, a descent from 1 500 ft (QFE) was commenced at a rate of 300 ft per mile with advisory altitudes being passed every half mile. The air was calm and the commander was able to achieve a high degree of precision during the approach; heights were accurately flown during the descent and the aircraft's track, cow verging on the centre line, was steady, When the aircraft was between 3 and 34 miles from touchdown, the controller informed it that visibility had deteriorated to 1 200 m. At two miles, when steering 2950, the aircraft intercepted the approach centre line and its heading was corrected to 290°; at one and a half miles at 500 ft, a further heading correction was made on to 287°. A drift to the right, away from the centre line, became apparent when the aircraft was between 1 and 12 miles from touchdown and the controller gave further corrections to the left to 285° and 280°. At one mile from touchdown at 350 feet, a further left correction to 275° was given but the aircraft continued to track to the right of the centre line. At half a mile from touchdown, when the talk-down was complete, the controller informed the aircraft it was well to the right of the centre line and that it should overshoot if the runway was not in sight. Shortly afterwards the aircraft was seen, by a controller, heading towards the control tower before commencing its corrective turn to the left. The commander, who was at the controls of the aircraft, said it was possible to refer to the ground and natural horizon until passing through about 650 ft when a thin layer of cloud followed by misty conditions required the remainder of the approach to be made on instruments. Whilst descending through 300 ft, the commander asked the co-pilot if he could see anything but just as he replied in the negative the commander saw the approach lights ahead and to his left and he promptly commenced an 'St turn to line up with them. As he did so he called for 400 of flap and less power in order to reduce the airspeed from 130 kt to about 112 kt. During this phase, he lost contact with the lights "for some seconds" but he elected to continue the approach because the last reported visibility was 1 200 rn and he was confident the runway lights would shortly appear ahead. When they came into view the aircraft was over the left-hand side of the runway and not properly aligned with it; the commander said he attempted to turn on to the runway centre line as he flared out for the landing. During this manoeuvre, although he was not aware of it, the starboard wing tip and No. 4 propeller struck the runway; the aircraft then touched down on all its wheels with considerable port drift. The commander took overshoot action, applying full power, calling for 20° of flap and the undercarriage to be raised; the airspeed had, in the meanwhile, fallen below 100 kt. The commander realised that the aircraft was not accelerating normally and saw that it was headed towards buildings on the northern perimeter of the aerodrome; rather than risk flying into these obstructions, he flew the aircraft on to the ground with its undercarriagi retracting. The aircraft touched down starboard wing first, ground-looped tb the right as it slid along the remaining section of the adjacent runway, then crashed tail first through a fence. Ten of the occupants of the passenger cabin were injured, three of them seriously; fire did not break out; rescue and fire vehicles arrived promptly on the scene. The accident occurred at 0759 hours.
Probable cause:
The accident was caused by an attempt to align the aircraft with the runway at too low a height following the commander's incorrect decision to continue the approach when visual guidance became obscured below critical height. A crash landing became necessary during an attempted overshoot after the aircraft had touched the ground and sustained damage during a turn at a low height.
Final Report:

Crash of a Vickers 803 Viscount in Ashbourne: 3 killed

Date & Time: Jun 22, 1967 at 0835 LT
Type of aircraft:
Operator:
Registration:
EI-AOF
Flight Type:
Survivors:
No
Schedule:
Dublin - Dublin
MSN:
176
YOM:
1957
Country:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Aircraft flight hours:
17447
Circumstances:
The Viscount had departed Dublin at 06:44 GMT for a pilot conversion training flight on an IFR flight plan. The instructor planned to spend 2 hours in a sector NW of Dublin, followed by practicing circuits and landings for one hour. Eyewitnesses reported seeing the aircraft entering a vertical dive from low altitude. The plane crashed and caught fire. All three crew members were killed.
Source: ASN
Probable cause:
An unintentional stall and incipient spin at a low altitude from which recovery was not possible. There is not enough evidence to determine the circumstances leading to the stall and incipient spin but the behaviour of the aircraft in the final stages was such as to indicate that it was not under control of the flight instructor.

Crash of a Vickers 812 Viscount in Southend: 2 killed

Date & Time: May 3, 1967
Type of aircraft:
Operator:
Registration:
G-AVJZ
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Southend - Southend
MSN:
360
YOM:
1958
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The crew was involved in a local test flight out from Southend Airport in the goal to renew the Airworthiness certificate. Shortly after takeoff, while in initial climb, a technical failure occurred on the engine number four. The crew was forced to shut down the engine and to feather its propeller when control was lost. The airplane lost height and crashed in an open field located near the airport, broke in two and came to rest. While all three crew members were injured, two people on the ground were killed.
Probable cause:
Loss of control during takeoff after feathering of No.4 propeller had been initiated.

Crash of a Vickers 818 Viscount off East London: 25 killed

Date & Time: Mar 13, 1967 at 1910 LT
Type of aircraft:
Operator:
Registration:
ZS-CVA
Survivors:
No
Schedule:
Port Elizabeth – East London – Bloemfontein – Johannesburg
MSN:
317
YOM:
1958
Flight number:
SA406
Country:
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
20
Pax fatalities:
Other fatalities:
Total fatalities:
25
Captain / Total flying hours:
12344
Captain / Total hours on type:
3231.00
Copilot / Total flying hours:
3995
Copilot / Total hours on type:
109
Circumstances:
On 13th March 1967 Vickers Viscount aircraft ZS-CVA, "Rietbok", was on a scheduled public transport flight No. SA 406 from Port Elizabeth to Johannesburg via East London and Bloemfontein. Its Estimated Time of Arrival at East London was 1714 GMT, but the weather there was poor. The captain had indicated that he would probably overfly East London, but that he would have a look at conditions there before deciding to do so. The last communication from the aircraft was when it notified East London Airport Control that it was "at 2,000 ft. with the coastline in sight". It is estimated that the aircraft was then between 20 and 15 nautical miles from the Airport and that the time was approximately 1709 GMT. At 1710.08 GMT the aircraft crashed into the sea. The approximate position of the crash was 33°13.45’ S. , 27°38.3’ E. On board were Captain Gordon Benjamin Lipawsky, First Officer Brian Albert Richard Trenwith, 3 cabin crew and 20 passengers. Air-sea rescue operations were put in hand promptly, but there were no survivors. Bits of floating wreckage, consisting mainly of cabin interior fittings, were recovered by naval vessels and other pieces were washed ashore. The main wreckage of the aircraft is believed to he lying at a depth of between 180 and 220 feet, approximately 1½ miles off-shore. Extensive salvage operations were attempted, but were hindered by murky water, a current up to 8 kts and dangerous sea conditions. The aircraft was lost and all 25 occupants were killed.
Probable cause:
The available data is not sufficient for the originating cause of the accident to be determined with any degree of probability. In the opinion of the Board certain possibilities can be excluded as being inconsistent with the evidence and/or as being remote and improbable: among these possibilities are structural failure, failure of controls or control surfaces, multiple engine failure, instrument failure, explosion, fire, a "bad weather" accident and pilot error. However, on the evidence the Board cannot exclude as the originating cause of the accident a heart attack suffered by the captain in the air, with ensuing loss of control of the aircraft, and with the first officer being unable in the time available to regain sufficient control to prevent contact with the sea.
Final Report:

Crash of a Vickers 745D Viscount in Norfolk

Date & Time: Jan 19, 1967 at 1359 LT
Type of aircraft:
Operator:
Registration:
N7431
Survivors:
Yes
MSN:
129
YOM:
1956
Crew on board:
4
Crew fatalities:
Pax on board:
46
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
14048
Captain / Total hours on type:
352.00
Circumstances:
Following a normal touchdown at Norfolk Municipal Airport, the crew started the braking procedure when the airplane collided with a snow plow. A wing was torn off and the snowplow was dragged over several meters. There were no injuries but the aircraft was damaged beyond repair.
Probable cause:
It was determined that the snowplows driver went onto runway without clearance after he misinterpreted ATC instructions.
Final Report:

Crash of a Vickers 701 Viscount in Rio de Janeiro

Date & Time: Oct 31, 1966
Type of aircraft:
Operator:
Registration:
PP-SRM
Flight Type:
Survivors:
Yes
Schedule:
Rio de Janeiro - Rio de Janeiro
MSN:
19
YOM:
1953
Country:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was completing a local training flight at Rio de Janeiro-Santos Dumont Airport. After touchdown, the four engine airplane was unable to stop within the remaining distance, overran and came to rest. All three crew members were unhurt while the aircraft was damaged beyond repair.