Crash of a BAe 3101 Jetstream 31 in Caracas: 3 killed

Date & Time: Nov 18, 2004 at 1302 LT
Type of aircraft:
Operator:
Registration:
YV-1083C
Survivors:
Yes
Schedule:
El Vigía – Caracas
MSN:
762
YOM:
1987
Flight number:
VNE213
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
19
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
After landing on runway 09, the twin engine aircraft went out of control, veered off runway to the right and eventually collided with the fire station located between both runways 08 and 09 at Caracas-Maiquetía-Simón Bolívar Airport. Two female passengers were killed while 19 other occupants suffered injuries of various degrees. Few hours later, a third passenger died from his injuries. Weather conditions were poor at the time of the accident with heavy rain falls, and the runway surface was wet.

Crash of a BAe 3201 Jetstream 32EP in Kirksville: 13 killed

Date & Time: Oct 19, 2004 at 1937 LT
Type of aircraft:
Operator:
Registration:
N875JX
Survivors:
Yes
Schedule:
Saint Louis – Kirksville
MSN:
875
YOM:
1990
Flight number:
AA5966
Crew on board:
2
Crew fatalities:
Pax on board:
13
Pax fatalities:
Other fatalities:
Total fatalities:
13
Captain / Total flying hours:
4234
Captain / Total hours on type:
2510.00
Copilot / Total flying hours:
2856
Copilot / Total hours on type:
107
Aircraft flight hours:
21979
Aircraft flight cycles:
28973
Circumstances:
On October 19, 2004, about 1937 central daylight time, Corporate Airlines (doing business as American Connection) flight 5966, a BAE Systems BAE-J3201, N875JX, struck trees on final approach and crashed short of runway 36 at Kirksville Regional Airport (IRK), Kirksville, Missouri. The flight was operating under the provisions of 14 Code of Federal Regulations Part 121 as a scheduled passenger flight from Lambert-St. Louis International Airport, in St. Louis, Missouri, to IRK. The captain, first officer, and 11 of the 13 passengers were fatally injured, and 2 passengers received serious injuries. The airplane was destroyed by impact and a post impact fire. Night instrument meteorological conditions (IMC) prevailed at the time of the accident, and the flight operated on an instrument flight rules flight plan.
Probable cause:
the pilots' failure to follow established procedures and properly conduct a non precision instrument approach at night in IMC, including their descent below the minimum descent altitude (MDA) before required visual cues were available (which continued unmoderated until the airplane struck the trees) and their failure to adhere to the established division of duties between the flying and non flying (monitoring) pilot.
Contributing to the accident was the pilots' failure to make standard callouts and the current Federal Aviation Regulations that allow pilots to descend below the MDA into a region in which safe obstacle clearance is not assured based upon seeing only the airport approach lights. The pilots' unprofessional behavior during the flight and their fatigue likely contributed to their degraded performance.
Final Report:

Crash of a BAe 3201 Jetstream 32EP in Luleå

Date & Time: Sep 17, 2003 at 1828 LT
Type of aircraft:
Operator:
Registration:
SE-LNT
Flight Type:
Survivors:
Yes
Schedule:
Pajala – Luleå
MSN:
948
YOM:
1991
Flight number:
EXC403
Country:
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
31000
Captain / Total hours on type:
2000.00
Copilot / Total flying hours:
660
Copilot / Total hours on type:
237
Aircraft flight hours:
13494
Circumstances:
The pilots were scheduled to fly the aircraft, a BAe Jetstream 32, on scheduled flight EXC403 from Pajala Airport to Luleå/Kallax Airport. This was the third flight together for the day. Before takeoff they noted that the flight was planned without passengers. Since the co-pilot was shortly to undergo an Operator’s Proficiency Check and the commander had long flying experience, including as an instructor, the commander decided to take the opportunity to have the co-pilot train flying with simulated engine failure. The takeoff from Pajala was at 17.57 hrs with the co-pilot as Pilot Flying. During the climb the commander reduced thrust on the right engine to simulate engine failure. This was done by moving the engine control lever to its rear stop. The commander understood this to represent what is termed ”simulated feather” in which an engine generates no drag and causes the least possible resistance. The exercise passed off without problem and the co-pilot had no difficulties in handling the aircraft. It was decided to practise flying with simulated engine failure during the landing as well. During the approach to Luleå/Kallax Airport when the aircraft was at an altitude of about 3500 feet the commander accordingly reduced thrust on the right engine once again. The co-pilot understood that the whole landing, including touchdown, would be with one engine on reduced thrust. However, the commander’s intention was to restore normal thrust on the right engine before touchdown. Prior to landing the reference speed (Vref1) had been calculated at 107 knots IAS2 and the flaps lowered 20°, based on the calculated landing mass of 5 640 kg. During the approach when the aircraft was at about 3500 feet, the commander reduced right engine thrust. According to the FDR recording thrust was reduced initially to just over 19 % and subsequently, for six minutes, further to just under 11% at the same time as altitude decreased to 900 feet. The co-pilot flew the aircraft in a right turn to runway 32 and started his final 2 nautical miles from the runway threshold at a height of 900 feet. The final was entered with a somewhat higher glide angle than normal. As the aircraft approached the runway threshold the thrust on the right engine had decreased to approximately 7%. The approach took place with applied rudder and opposite banking to counteract the lateral forces generated by the asymmetrical thrust. During the approach the co-pilot experienced an inertia in the ailerons that he had never experienced previously. Shortly after the aircraft had crossed the runway threshold and was about 5 metres above the runway, both the co-pilot and the commander felt how the aircraft suddenly yawed and rolled to the right. Neither pilot remembers hearing the stall warning sounding. Despite application of full aileron and rudder the pilots were unable to stop the aircraft’s uncontrolled motion. This continued until the right wing tip hit the ground. The fuselage then struck the ground. The aircraft slid on its belly about 50 metres alongside the runway before stopping. The pilots hastily evacuated the aircraft. The accident was observed by the air traffic controller who immediately alarmed the airport rescue service, which arrived at the accident scene within a minute or so. After its arrival the commander boarded the aircraft and turned off the fuel supply and the main electricity, whereafter the rescue service covered the aircraft with foam. The accident occurred on 17 September 2003 at 18.28 hrs in position 6532N 02207E; 20 m above sea level in daylight.
Probable cause:
The accident was caused by shortcomings in the company’s quality assurance system, operational routines and regulations. These contributed to the facts that:
- the commander considered he was able to serve as a flying instructor on an aircraft type and in a flight situation for which he was neither qualified nor authorised,
- the pilot's lacked necessary familiarity with the aircraft type’s special flight characteristics during asymmetrical thrust, and
- the pilot's lacked familiarity with the regulations in force for flying training.
Final Report:

Crash of a BAe 3102 Jetstream 31 in Wick

Date & Time: Sep 17, 2003 at 1447 LT
Type of aircraft:
Operator:
Registration:
G-EEST
Survivors:
Yes
Schedule:
Aberdeen – Wick
MSN:
781
YOM:
1987
Location:
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
4
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
7885
Captain / Total hours on type:
1195.00
Copilot / Total flying hours:
6800
Copilot / Total hours on type:
1000
Aircraft flight hours:
17845
Aircraft flight cycles:
20730
Circumstances:
The aircraft was landing on Runway 31 at Wick Airport. It crossed the threshold at 130 kt which was 21 kt faster than the correct threshold speed. After the co-pilot closed the power levers the aircraft floated about six feet above the runway surface. The aircraft touched down and bounced before touching down a second time more heavily, cracking a wing spar and flexing the aircraft structure sufficient to allow the right propeller to contact the runway. The aircraft bounced again before touching down for the third and final time. The investigation determined that just before the first touchdown, one or both power levers were moved aft of the flight idle position. It was concluded that both the commander and co-pilot were making inputs on the flying controls from that moment onwards until after the second, heavy touchdown. There was no evidence of any technical fault on the aircraft and the weather conditions were well within the limitations set for the aircraft. No safety recommendations were made.
Probable cause:
It is reasonable to conclude that the manoeuvres conducted by G-EEST during the landing were the result of combined control inputs made by the commander and co-pilot. The evidence indicates that this period of combined control started at least 0.28 seconds before the first touchdown and finished at some stage after the second and damaging touchdown. After the first touchdown the aircraft became airborne in a high-drag, low-lift configuration which was intended for ground operation only and a 5.6g impact ensued on the second touchdown. There was no evidence of any technical fault on the aircraft that could have been a factor and the meteorological conditions were within the limitations set for the aircraft. A more complete understanding of the accident might have been possible with additional flight data parameters such as engine performance, aircraft pitch, and power lever position.
Final Report:

Crash of a BAe 3101 Jetstream 31 in Yacuiba

Date & Time: Jan 17, 2003 at 0900 LT
Type of aircraft:
Operator:
Registration:
CP-2404
Survivors:
Yes
Schedule:
Yacuiba - Santa Cruz
MSN:
680
YOM:
1985
Location:
Country:
Crew on board:
2
Crew fatalities:
Pax on board:
19
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
8194
Copilot / Total flying hours:
832
Circumstances:
During the takeoff roll at Yacuiba Airport, at V2 speed, the right engine lost power. The captain decided to continue the takeoff procedure. During initial climb, decision was taken to return for an emergency landing and the crew shut down the right engine and feathered its propeller. After touchdown on runway 20, the aircraft was unable to stop within the remaining distance, overran, lost its nose gear and collided with bushes and small trees, coming to rest about 50 metres past the runway end. All 21 occupants escaped uninjured while the aircraft was damaged beyond repair.
Probable cause:
The accident was the consequence of the combination of the following factors:
- Excessive speed upon landing,
- Delayed application of the brake systems,
- The runway length available was limited according to the conditions in force,
- The total weight of the aircraft upon landing,
- The aircraft configuration,
- The direction and intensity of the wind,
- An inadequate crew training.
Additionally, the exact cause of the loss of power on the right engine was not clearly determined at the time the final report was published.
Final Report: