Crash of a Cessna 425 Conquest I in Canadian

Date & Time: Mar 28, 2011 at 0825 LT
Type of aircraft:
Operator:
Registration:
N410VE
Flight Type:
Survivors:
Yes
Schedule:
Grand Junction - Canadian
MSN:
425-0097
YOM:
1981
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
6
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
22500
Captain / Total hours on type:
1000.00
Aircraft flight hours:
7412
Circumstances:
While on a straight-in global-positioning-system approach, the airplane broke out of the clouds directly over the end of the runway. The pilot then remained clear of the clouds and executed a no-flap circling approach to the opposite direction runway. The pilot said that his airspeed was high when he touched down. The landing was hard, and the right main landing gear tire blew out, the airplane departed the runway to the left, and the left main landing gear collapsed. No preaccident mechanical malfunctions or failures were found that would have precluded normal operation.
Probable cause:
The pilot’s continuation of the approach with excessive airspeed, which resulted in a hard landing and a loss of directional control.
Final Report:

Crash of a Piper PA-46-500TP Malibu Meridian in Port Mansfield

Date & Time: Oct 29, 2010 at 1611 LT
Registration:
N234PM
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Port Mansfield – Sinton
MSN:
46-97200
YOM:
2005
Crew on board:
1
Crew fatalities:
Pax on board:
2
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
3500
Captain / Total hours on type:
5.00
Aircraft flight hours:
650
Circumstances:
The pilot reported that shortly after takeoff the engine lost power momentarily, just before losing power completely. The pilot performed an emergency landing in a nearby field. The airplane sustained substantial damage during the forced landing. The airframe, engine, and engine accessories were examined. Fuel was noted at the engine, and no anomalies were revealed that would have contributed to the accident. The cause of the loss of power could not be determined.
Probable cause:
The total loss of engine power for undetermined reasons because examination of the airframe and engine did not reveal any anomalies that would have contributed to the loss of engine power.
Final Report:

Crash of a Piper PA-61 Aerostar (Ted Smith 601) in Cleburne

Date & Time: Jul 22, 2010 at 1100 LT
Operator:
Registration:
N601AT
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Cleburne - Mena
MSN:
61-0332-095
YOM:
1976
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
28000
Captain / Total hours on type:
332.00
Circumstances:
After takeoff, the right engine experienced a loss of power followed by the left engine losing power. The pilot maneuvered the airplane toward the nearest open field and the airplane impacted terrain during landing, resulting in a circumferential split in fuselage near the aft pressure bulkhead. The airplane was equipped with 4 fuel tanks: 2 located in each wing outboard of the engine nacelle (65-gallon capacity), 1 main fuselage tank (about 44-gallon capacity), and 1 auxiliary tank located in forward section of baggage compartment (45-gallon capacity). The airplane was capable of carrying 209.5 gallons usable fuel and the pilot stated that prior to departure he filled the main fuselage tank to capacity, added 20 gallons in the auxiliary tank and 25 gallons in each wing tank, which he equated to a total of 131 gallons on board. The fuselage contained two fuel filler necks, one for each fuselage tank (main and auxiliary). The auxiliary tank was clearly placarded with a red placard visibly standing out against a silver paint stripe; the main tank was not clearly placarded, with a red placard blending easily with red paint stripe. A salvage retriever recalled that during recovery the left wing contained 17 gallons of fuel, the right wing contained 57 gallons of fuel, the main fuselage tank contained 2.5 gallons of fuel, and the auxiliary fuselage tank contained 28 gallons of fuel. A postaccident examination of the airplane and engines revealed no anomalies that would have precluded normal operation. The main fuselage tank and auxiliary fuselage tank were not breached and the fuel sumps contained check valves which prevent the back-flow of fuel from one fuel tank to another. Based on the evidence it is likely that the pilot exhausted the airplane's fuel supply in the main fuselage tank, which resulted in the loss of power to both engines.
Probable cause:
A total loss of engine power due to fuel starvation as a result of the pilot’s improper fuel management. Contributing to the accident were the critical fuel placards that were difficult to see due to the airplane's paint scheme.
Final Report:

Crash of a Cessna 421B Golden Eagle II in Alpine: 5 killed

Date & Time: Jul 4, 2010 at 0015 LT
Operator:
Registration:
N31AS
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Alpine - Odessa
MSN:
421B-0473
YOM:
1973
Crew on board:
2
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
5
Captain / Total flying hours:
1650
Captain / Total hours on type:
160.00
Aircraft flight hours:
2302
Circumstances:
The airplane impacted terrain shortly after takeoff. The wreckage distribution was consistent with a high airspeed, low angle-of-attack impact. Examination of the ground scars and wreckage indicated that the landing gear was down, the flaps were down, and the engines were operating at a high power setting at the time of impact. An examination of the airframe, engines, and related systems revealed no mechanical malfunctions or failures. According to the owner’s manual for the airplane, the flaps should have been retracted and the landing gear should have been brought up as soon as a climb profile was established. Based upon the location of the wreckage, the direction of the impact, and the location of the airport, it is likely that the airplane crashed within one or two minutes after takeoff. The extended landing gear and flaps degraded the climb performance of the airplane. The pilot held an airline transport pilot certificate and had recent night flight experience. Toxicological results were positive for azacyclonol and ibuprofen but were not at levels that would have affected his performance. According to family members, the pilot normally slept from 2230 or 2300 to 0700; the accident occurred at 0015. Although the investigation was unable to determine how long the pilot had been awake before the accident or his sleep schedule in the three days prior to the accident, it is possible that the pilot was fatigued, as the accident occurred at a time when the pilot was normally asleep. The company did not have, and was not required to have guidance or a policy addressing fatigue management.
Probable cause:
The degraded performance of the airplane due to the pilot not properly setting the flaps and retracting the landing gear after takeoff. Contributing to the accident was the pilot’s fatigue.
Final Report:

Crash of a Piper PA-46-500TP Malibu Meridian in Mendoza: 2 killed

Date & Time: Dec 7, 2009 at 1134 LT
Operator:
Registration:
N600YE
Flight Type:
Survivors:
No
Schedule:
Rockport – Austin
MSN:
46-97250
YOM:
2006
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
2
Captain / Total flying hours:
3513
Circumstances:
The pilot was established on the localizer portion of the instrument landing system approach outside the final approach fix in visual meteorological conditions above clouds. He was then given vectors away from the localizer course by an air traffic controller. The vectors were close together and included a left 90-degree turn, a descent, and a 180-degree right turn back toward the localizer course. During the right turn and descent, the airplane continued turning with increasing bank and subsequently impacted the ground. According to a pilot weather report and flight path data the pilot entered clouds as he was starting the right turn toward the localizer. The combination of descending turns while entering instrument conditions were conducive to spatial disorientation. Further, the heading changes issued by the air traffic controller were rapid, of large magnitude, and, in combination with a descent clearance, likely contributed to the pilot’s disorientation. Diphenhydramine, a drug that may impair mental and/or physical abilities, was found in the pilot’s toxicological test results. While the exact effect of the drug at the time of the accident could not be determined, it may have contributed to the development of spatial disorientation.
Probable cause:
The pilot’s spatial disorientation, which resulted in his loss of airplane control. Contributing to the pilot's spatial disorientation was the sequence and timing of the instructions issued by the air traffic controller. The pilot’s operation of the airplane after using impairing medication may also have contributed.
Final Report:

Crash of a Beechcraft B100 King Air 100 in Benavides: 4 killed

Date & Time: Oct 26, 2009 at 1143 LT
Type of aircraft:
Registration:
N729MS
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Uvalde - Leesburg
MSN:
BE-2
YOM:
1976
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
4
Captain / Total flying hours:
550
Circumstances:
The pilot obtained three weather briefings before departure. At that time, the current weather along the route of flight showed significant convective activity and a moving squall line, and the forecast predicted significant thunderstorm activity along the planned route of flight. The pilot was concerned about the weather and mentioned that he would be looking for "holes" in the weather to maneuver around via the use of his on-board weather radar. He decided to fly a route further south to avoid the severe weather. Radar data indicates that, after departure, the pilot flew a southerly course that was west of the severe weather before he asked air traffic control for a 150-degree heading that would direct him toward a "hole" in the weather. A controller, who said he also saw a "hole" in the weather, told the pilot to fly a 120-degree heading and proceed direct to a fix along his route of flight. The airplane flew into a line of very heavy to intense thunderstorms during cruise flight at 25,000 feet before the airplane began to lose altitude and reverse course. The airplane then entered a rapid descent, broke up in flight, and subsequently impacted terrain. Review of recorded precipitation data showed that there was substantial information available to the controller about moderate to extreme weather along the aircraft’s route of flight. While the controller stated that he saw a hole or clear area ahead of the aircraft, this is contradicted by both the recorded data and the statement of a second controller working the D-position at the time of the accident. The first controller did not advise the pilot of the severe weather that was along this new course heading and the pilot entered severe weather and began to lose altitude. The controller queried the pilot about his altitude loss and the pilot mentioned that they had gotten into some "pretty good turbulence." This was the last communication from the pilot before the airplane disappeared from radar. Review of recorded precipitation data showed that there was substantial information available to the controller about moderate to extreme
weather along the aircraft’s route of flight. The controller did not provide advisories to the pilot regarding the adverse weather's immediate safety hazard to the accident flight as required by Federal Aviation Administration Order 7110.65. Examination of the recovered sections of flight control surfaces revealed that all of the fractures examined exhibited signs consistent with overstress failure. There was no evidence of preexisting cracking on any of the fracture surfaces examined and no preaccident anomalies were noted with the engines.
Probable cause:
The pilot's failure to avoid severe weather, and the air traffic controller's failure to provide adverse weather avoidance assistance, as required by Federal Aviation Administration directives, both of which led to the airplane's encounter with a severe thunderstorm and the subsequent loss of control and inflight breakup of the airplane.
Final Report:

Crash of a Beechcraft B100 King Air in Aurora

Date & Time: Oct 6, 2009 at 1450 LT
Type of aircraft:
Registration:
N2TX
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Oklahoma City - Fort Worth
MSN:
BE-103
YOM:
1981
Location:
Crew on board:
1
Crew fatalities:
Pax on board:
3
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
4120
Captain / Total hours on type:
103.00
Aircraft flight hours:
1063
Circumstances:
The pilot added fuel to the multi-engine airplane prior to departure. While en route to the destination airport, the pilot noted that the fuel gauges indicated that the right main-tank appeared to be almost empty and the left tank appeared half full. The pilot initiated the crossfeed procedure in an effort to supply fuel to both engines from the left main tank. Shortly after beginning the crossfeed procedure, both engines experienced a total loss of power. The pilot notified air traffic control (ATC) and selected a field to perform a forced landing. Prior to touchdown, the right engine produced a surge of power and, in response, the airplane rolled to the left. The surge abruptly ended and the pilot continued the forced landing by lowering landing gear and extending the flaps. The airplane impacted the ground, coming to rest in an open field. A postimpact examination did not reveal any anomalies with the airframe or engine that would have precluded normal operation. Although both fuel tanks were ruptured, the accident scene did not contain a large amount of residual fuel. A small fuel slick was found on the surface of a nearby pond; however, the grass area underneath both wings did not contain dead grass; this would have been expected if there was more than a negligible amount of fuel in the tanks at time of impact.
Probable cause:
The loss of engine power due to fuel exhaustion as a result of the pilot's inadequate fuel management.
Final Report:

Crash of a Beechcraft E18S in Jones Creek

Date & Time: Oct 3, 2009 at 1030 LT
Type of aircraft:
Operator:
Registration:
N797SB
Flight Phase:
Survivors:
Yes
Schedule:
Angleton - Angleton
MSN:
BA-172
YOM:
1956
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
1832
Captain / Total hours on type:
37.00
Circumstances:
The pilot was spraying a marshy area for mosquitoes. After making a spray pass, he made a right 180-degree turn to an easterly heading and the right wing struck a radio tower. The pilot didn't know the extent of the damage and there appeared to be a "controllability issue." He elected to land in a pasture. During the landing, the airplane struck and killed a cow and a bull, then collided with a pile of wood, resulting in substantial damage. The unlit 100-foot radio tower was within the walls of a correctional facility, was used for ground communications, and has been there for several years. It was not marked on sectional charts.
Probable cause:
The pilot's failure to see and avoid the radio tower.
Final Report:

Ground accident of a Learjet 40 in Fort Worth

Date & Time: Jun 18, 2009
Type of aircraft:
Operator:
Registration:
N998AL
Flight Phase:
Flight Type:
Survivors:
Yes
MSN:
45-2029
YOM:
2005
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The Learjet 40 was being operated by two A&P mechanics for the purpose to taxi out for an engine test run on the n°1 engine. During taxi it was necessary to stop the aircraft for motor vehicle traffic. The mechanic advanced the throttles for taxi and to climb a 15 to 20 foot hill. When the mechanic attempted to reduce the throttles only the n° 2 engine could be retarded. The n°1 engine was at a high power setting and could not be reduced. The aircraft left 4 skid marks as the main tires were locked for approximately the length of a little more than a football field. The mechanics could not shut down the n°1 engine. Control of the aircraft was lost with the n°1 engine at a high power setting. The right wing impacted the corner of a hanger. The nose gear broke and an embankment stopped the aircraft. The mechanics were then able to shut down both engines and exited the aircraft with no injuries.
Probable cause:
The NTSB did not proceed to any investigation on this event.

Crash of an ATR42-320 in Lubbock

Date & Time: Jan 27, 2009 at 0437 LT
Type of aircraft:
Operator:
Registration:
N902FX
Flight Type:
Survivors:
Yes
Schedule:
Fort Worth - Lubbock
MSN:
175
YOM:
1990
Flight number:
FX8284
Location:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Captain / Total flying hours:
13935
Captain / Total hours on type:
2052.00
Copilot / Total flying hours:
2109
Copilot / Total hours on type:
130
Aircraft flight hours:
28768
Aircraft flight cycles:
32379
Circumstances:
Aircraft was on an instrument approach when it crashed short of the runway at Lubbock Preston Smith International Airport, Lubbock, Texas. The captain sustained serious injuries, and the first officer sustained minor injuries. The airplane was substantially damaged. The airplane was registered to FedEx Corporation and operated by Empire Airlines, Inc., as a 14 Code of Federal Regulations Part 121 supplemental cargo flight. The flight departed from Fort Worth Alliance Airport, Fort Worth, Texas, about 0313. Instrument meteorological conditions prevailed, and an instrument flight rules flight plan was filed.
Probable cause:
The National Transportation Safety Board determines that the probable cause of this accident was the flight crew’s failure to monitor and maintain a minimum safe airspeed while executing an instrument approach in icing conditions, which resulted in an aerodynamic stall at low altitude.
Contributing to the accident were:
-the flight crew’s failure to follow published standard operating procedures in response to a flap anomaly,
-the captain’s decision to continue with the unstabilized approach
-the flight crew’s poor crew resource management,
-fatigue due to the time of day in which the accident occurred and a cumulative sleep debt which likely impaired the captain’s performance.
Final Report: