Crash of a Vickers 290 Wellington I in Brandon: 1 killed

Date & Time: Aug 29, 1939 at 1400 LT
Type of aircraft:
Operator:
Registration:
L4214
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Mildenhall - Mildenhall
Location:
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
Shortly after take off from RAF Mildenhall, while climbing, the radio operator informed ATC that an engine exploded. The Captain decided to make a turn back to the airport via a circuit to the north when the situation became critical. He attempted an emergency landing in Brandon, some 13 km northeast of the airbase, when the aircraft hit trees and crashed on a barn. A crew member was killed while all five other occupants were injured.
Crew (149th Squadron):
F/O Francis William Scott Turner, pilot,
P/O Thomas Watson, pilot,
Sgt Anthony Frederick Adrian Freeman, observer, †
Sgt Horace James Weller, copilot,
AC2 John Gerard Hoey, wireless operator,
AC2 Cecil George Barker, air gunner.
Source: http://www.rcawsey.co.uk/Acc1939.htm

Thanks to Anthony Frederick Adrian Freeman and Peter Cannings for the following testimony:
The pilot, Francis William Scott-Turner, told the Coroner that just before 5 pm on Tuesday 29th August the bomber took off to participate in a search for a missing aircraft. Everything was going well and then about an hour into the flight the port side engine caught fire and he carried out the procedure for ‘Fire In The Air’ and prepared the crew for a crash landing, which was probably about two or three miles north-east of Brandon. Sergeant Weller was instructed to bring Pilot Officer Watson out of the nose of the aircraft as soon as possible and bring him toamidships. The rest of the crew were told to sit own and hang on and then the plane came down among some trees. “I picked up Pilot Officer Watson and told him to get out as quickly as possible. I looked out and then was told that Freeman was still in the machine. Walking across the wing and getting back into the machine again through a hatch. I found Freeman on his knees against a step formed by a bomb micelle. We did not think it was advisable to move him until medical assistance arrived. The fire had gone out by this time.” Answering the coroner, he said that Freeman should have stayed where he was because it was the safest place in the machine and he must have moved away from it because of the location of his body. The deceased’s father asked if his son had been thrown from his seat, but the witness said that had not been the case because it looked like he had lowered the rear of his seat in order to evacuate from his position. A member of the jury asked if he was attempting to bail out but the witness said the aircraft was too low.
The co-pilot, Sergeant Weller, told the inquest of how the port engine had developed oil failure near North Walsham and they maintained a height off 600 or 700 feet on the starboard engine alone. When he saw they were low enough to see trees he sat down and hung on to the nearest spar. Weller had seen Freeman in the tail when he was talking to A/C Hoey and he presumed he was still sat there at this time. After the crash he left the aircraft and went straight away to the aircraft’s tail to assist Freeman but when he looked through the rear window he could not see him. He then walked along the aircraft and caught sight of Freeman’s head resting on top of the step. The witness answered the Coroner, and said that it was possible that as soon as Freeman got out of his seat he could have been thrown forward to the front. In the tail there was a celluloid hatch that could be cut away and through the hole he could have escaped. In his opinion the tail was the safest place to be in a crash. Cecil Barker told the inquest that he had changed places with Freeman during the flight but had returned to be amidships to prepare for impact. He had caught a glimpse of Freeman who had turned to face them and assumed he was trying to get out. The Coroner replied, “There must be a tendency, particularly in the case of a young fellow like this, for him to get with someone for whom he feels will give him moral support in the time of emergency. I can understand that and I am sure the jury does.” John Hoey told the Coroner that he had sent out a message just before the crash. Police Constable Churchyard, based in Weeting and serving in the Norfolk Constabulary, told the inquest that the aircraft had landed on top of some pine trees, at a height of about 10 feet and about 350 yards from the Brandon-Weeting road. It had cut a swathe through the trees of 30 yards by 60 yards. He had helped remove the tail of the aircraft with the crew and assisted in the removal of the deceased’s body from the machine and it was taken to Mildenhall by ambulance.
An eyewitness, Mrs Mary Jane Leonard, of Weeting, said she had looked out of her bungalow window and saw the bomber flying too low, with smoke coming from the back of it and there was a crackling noise coming from the engine. It disappeared from view and then there was the sound of a crash. She stopped a passing car and sent them to fetch the Police.
Dr Jenkins, a R.A.F. Medical Officer, said the deceased had suffered broken ribs and a perforated lung. The Coroner expressed hi sympathy to the dead man’s family, “I have said it before, unfortunately, that we who are not in any arm of the Service owe a great debt of gratitude to these men who take risks that we may live in peace.” The jury returned a verdict of Misadventure and the foreman said the jury felt the crew had done their very best under the circumstances. The Coroner thanked the foreman for his kind words. The deceased’s father thanked his son’s colleagues and the R.A.F. Medical Officer.

Crash of a Vickers 290 Wellington I at RAF Mildenhall

Date & Time: Aug 28, 1939
Type of aircraft:
Operator:
Registration:
L4217
Flight Phase:
Flight Type:
Survivors:
Yes
Site:
Schedule:
Mildenhall - Mildenhall
Region:
Crew on board:
6
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On 28AUG1939, the aircraft L4217 crashed at Beck Row on take off for practice Bombing and Gunnery Exercise Burned out. First take off attempt was aborted due to lack of power. On second attempt engines cut after point of no return, the aircraft cleared the boundary fence, then port wing struck a barn, then damaged another barn before demolishing the out houses of a pair of cottages and ended up sideways on to a stone wall alongside the main road to Mildenhall town with a wing blocking the road before the final impact Eric and Navigator P/O Hiller braced themselves against the main spar. As A/C stopped first reaction was to exit via astro hatch but this had jammed, training memories then led us to collect escape axe from fuselage mid section and use it to chop off the rear turret cupola. By this time the front of the aircraft was burning furiously & the smoke plus dust from the buildings made it difficult to see very much. When we did reach the tail the turret was already missing from contact with the wall so out we went. We found that and front gunner had escaped via damaged nose and rear gunner had been thrown out into a bed of nettles! The Captain was convinced that there was another crew man aboard looking in we saw what could be a person it turned out to be engine covers and we beat a hasty retreat via the rear end. It was quite a spectacle with petrol tanks and oxygen cylinders exploding plu the rattle of .303 ammunition exploding. We later found out that A/c Hedges a new arrival on squadron had missed the flight though n the detail. Aircraft Captain sustained a broken finger, Front gunner a Cut arm requiring stitches while we all sustained mild abrasions and were stiff for days the rear gunner also had nettle rash! The following day showed the engines lying in pools of now solidified metal. Nothing else remained of the aircraft forward of the centre section. On inspection we realized that navigator and I had climbed out over the back of rear gunners seat 3 times without thinking of lowering it! Cause of the engine problem was a petrol cock which should have been either fully up or fully down depending on whether using 100 octane or lower value fuel. Was not set for 100 octane required for take off thus engines were starved – this in turn caused a blow back which in turn caused the fire I lost my nerve for flying for some time after that.

Thanks to Peter Cannings for his testimony and full report. His cousin F/Lt Eric F. H. Cannings was on board.

Crash of a Bristol 130 Bombay I at RAF Martlesham Heath: 3 killed

Date & Time: Aug 23, 1939
Type of aircraft:
Operator:
Registration:
L5808
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Martlesham Heath - Martlesham Heath
MSN:
SH.1
YOM:
1935
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
3
Circumstances:
Shortly after take off from RAF Martlesham Heath, while in initial climb, the aircraft stalled, nosed down and crashed in a huge explosion. All three crew members were killed.
Crew:
F/Sgt Cecil Eneder Higgins,
LAC John Reginald Machin,
AC1 Douglas Treadwell.
Probable cause:
Loss of control during initial climb because of wrong setting of the pitch trim elevator.

Crash of a Bristol 142 Blenheim I in Ordford Ness

Date & Time: Dec 14, 1938
Type of aircraft:
Operator:
Registration:
L1201
Flight Phase:
Flight Type:
Survivors:
Yes
Schedule:
Martlesham Heath - Martlesham Heath
MSN:
8484
YOM:
1938
Region:
Crew on board:
3
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
The crew was forced to make an emergency landing when the aircraft belly landed in Ordford Ness. There were no casualties.

Crash of a Handley Page H.P.54 Harrow II at RAF Honington

Date & Time: Nov 24, 1938
Type of aircraft:
Operator:
Registration:
K7002
Flight Type:
Survivors:
Yes
Schedule:
Honington - Honington
Region:
Crew on board:
4
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
0
Circumstances:
On final approach to RAF Honington at night, the aircraft impacted the ground and crashed short of runway. All four crew members were injured and the aircraft was destroyed. For unknown reason, the crew was completing the approach at a too low altitude.

Crash of a Handley Page H.P.50 Heyford III at RAF Stradishall: 2 killed

Date & Time: Nov 14, 1938
Operator:
Registration:
K5194
Flight Type:
Survivors:
No
Schedule:
Scampton – Stradishall
Region:
Crew on board:
2
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
On final approach to RAF Stradishall at night, the airplane impacted trees and crashed in a wooded area short of runway, bursting into flames. The aircraft was destroyed and both pilots were killed.
Crew:
W/Cdr Harry Augustus Smith,
P/O Aubrey Ward Jackson.

Crash of Supermarine Scapa off Felixstowe: 6 killed

Date & Time: Aug 13, 1938
Type of aircraft:
Operator:
Registration:
K7306
Flight Type:
Survivors:
No
Schedule:
Pembroke Dock – Felixstowe
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
1
Pax fatalities:
Other fatalities:
Total fatalities:
6
Circumstances:
On approach to Felixstowe, the float plane crash in unknown circumstances into the sea some 5 km offshore. All six occupants were killed.
Crew:
Sgt David Louis Bissett Cabuzet,
AC1 Peter E. Evans,
AC1 O. T. Edwards,
AC1 Thomas E. Griffiths,
AC1 Keith C. Sherwin.
Passenger:
Mr. Hunter Gray.

Crash of a Handley Page H.P.54 Harrow I in Great Barton: 5 killed

Date & Time: Aug 7, 1938 at 0010 LT
Type of aircraft:
Operator:
Registration:
K6961
Flight Phase:
Flight Type:
Survivors:
No
Site:
Schedule:
Leuchars - Leuchars
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
5
Circumstances:
The crew was performing a night training exercise when the twin engine aircraft, flying at low altitude in marginal weather conditions, impacted a hill and crashed near Great Barton. The airplane was destroyed and all five crew members from the 37th Squadron were killed.
Crew:
F/O John Adam, pilot,
P/O Albert George Gillespie,
P/O Edward Rayment,
AC1 Charles Carter Noxon Suthers,
AC1 Patrick Joseph McGovern.
Probable cause:
Controlled flight into terrain.

Crash of a Handley Page H.P.50 Heyford III at RAF Honington: 2 killed

Date & Time: Dec 16, 1937 at 2120 LT
Operator:
Registration:
K5183
Flight Type:
Survivors:
Yes
Schedule:
Honington - Honington
Region:
Crew on board:
5
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
2
Circumstances:
The crew was completing a local night training flight at RAF Honington. For unknown reasons, the airplane landed hard, went out of control and came to rest upside down. A crew member was killed while three others were injured and one escaped unhurt. Two days later, one of the survivor died from injuries sustained.
Crew:
P/O Thomas Arthur Bunting, †
P/O Basil Gaston Lancelot Betbeder, †
P/O Laurence Herbert McFarlane,
AC1 Ernest Marrows,
AC1 Charles Albert Frederick Kettle.

Crash of a De Havilland DH.60G Moth Major III in Nacton:1 killed

Date & Time: Jun 11, 1937
Type of aircraft:
Registration:
G-ABUI
Flight Phase:
Flight Type:
Survivors:
No
Schedule:
Ipswich - Ipswich
MSN:
5000
YOM:
1934
Location:
Region:
Crew on board:
1
Crew fatalities:
Pax on board:
0
Pax fatalities:
Other fatalities:
Total fatalities:
1
Circumstances:
The pilot departed Ipswich on a local solo flight. En route, the airplane entered an uncontrolled descent and crashed in a wooded area, bursting into flames. The pilot Herbert Samuel Ward was killed.